HL incident on 2023-11-29 — OK

Operator
Mid-Continent Fractionation And Storage, L.l.c.
Cause
Corrosion Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,000,000
Incident datetime
2023-11-29 00:00 UTC
Report number
Location
OK
Narrative
11/2 8:40am environmental specialist noticed a frost ball in the area and contacted supervisor who confirmed the leak as of 9:20am by use of hazgas monitor. Line segment was isolated shortly thereafter (~9:40am) and open to flare system in which remaining product in line was flared off. Extent of damage was ~10 feet in length with pin hole corrosion as primary cause of release. 3/19/2024 line was put back into service was damage segment was replaced with new pipe.
Detailed record list
Report Received Date
2023-11-29 00:00:00
Iyear
2023
Report Number
20230287
Supplemental Number
39426
Report Type
Supplemental Final
Operator Id
Name
Mid-Continent Fractionation And Storage, L.l.c.
Operator Street Address
One Williams Center P.o. Box 645
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74172
Time Zone
Central
Daylight Savings Ind
No
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
23
Intentional Release Bbls
93
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Communication State Fed Ind
No
Nrc Rpt Num
Additional Nrc Report Numbers
48 Hour Follow Up - 1383399
Ignite Ind
No
Upstream Action Taken
Valve Closure
Upstream Valve Type Ind
Manual
Downstream Action Taken
Valve Closure
Downstream Valve Type Ind
Remotely Controlled
Num Pub Evacuated
0
Pipe Fac Name
Trunk C4 And C21-23 Lateral
Segment Name
843-T-T-T
Onshore State Abbreviation
Ks
Onshore Postal Code
66901
Onshore City Name
Not Within A Municipality
Onshore County Name
Rice
Designated Location
Survey Station No.
Designated Name
1+50
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
108
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Puddle Weld Ind
No
Pipe Diameter
8
Pipe Wall Thickness
0.188
Pipe Smys
35000
Pipe Specification
5l
Pipe Seam Type
Erw - High Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
Cold Applied Tape
Coating Applied Ind
Yes
Installation Year
Unknown
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
1000
Est Cost Prop Damage
1000000
Est Cost Emergency
1400
Est Cost Environmental
2000
Est Cost Other
0
Prpty
1004400
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
438
Mop Psig
740
Mop Cfr Section
Component Design Pressure �195.406(A)(2)
Maop Established Date
2012-06-14 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
1500
Internal Inspection Ind
No
Other Inspection Ind
Yes
Internal Inspection Details
Station Piping. Ili Tool Accommodation Is Not Required.
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Controller's action in this accident could not be a contributing factor as no alarms or alerts occurred requiring a response from the controller.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
External Corrosion
Internal External
External Corrosion
Visual Exam Results
Localized Pitting
Galvanic Corrosion Ind
Yes
Field Exam Basis Ind
Yes
Underground Location
Yes
Under Cathodic Protection Ind
Yes
Cathodic Pro Start Year
2005
Shielding Evident
Yes
Cathodic Survey Type
Yes
Cp Annual Survey Ind
Yes
Cp Annual Survey Year
2023
Prior Damage
Yes
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
2012
Hydrtst Most Rcnt Pressure
1073
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Pwf Construction Ind
Yes
Preparer Name
L***** H***
Preparer Title
Pipeline Safety Manager
Preparer Email
L**********@w*******.com
Preparer Telephone
9182404259
Prepared Date
2024-04-11 00:00:00
Local Contact Name
B**** S*****
Local Contact Email
B***********@w*******.com
Local Contact Telephone
6208342140
Authorizer Name
L***** H***
Authorizer Telephone
9182404259
Authorizer Title
Pipeline Safety Manager
Authorizer Email
L**********@w*******.com
Narrative
11/2 8:40am environmental specialist noticed a frost ball in the area and contacted supervisor who confirmed the leak as of 9:20am by use of hazgas monitor. Line segment was isolated shortly thereafter (~9:40am) and open to flare system in which remaining product in line was flared off. Extent of damage was ~10 feet in length with pin hole corrosion as primary cause of release. 3/19/2024 line was put back into service was damage segment was replaced with new pipe.
Report Received Date 2023-11-29 00:00:00
Iyear 2023
Report Number 20230287
Supplemental Number 39426
Report Type Supplemental Final
Operator Id 31816 PHMSA Enforcement
Name Mid-Continent Fractionation And Storage, L.l.c.
Operator Street Address One Williams Center P.o. Box 645
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74172
Time Zone Central
Daylight Savings Ind No
Location Latitude 38.370282 Google Maps OpenStreetMap
Location Longitude -98.075563 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls 23
Intentional Release Bbls 93
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind Yes
Communication State Fed Ind No
Nrc Rpt Num 1383265 NRC Report How to search
Additional Nrc Report Numbers 48 Hour Follow Up - 1383399
Ignite Ind No
Upstream Action Taken Valve Closure
Upstream Valve Type Ind Manual
Downstream Action Taken Valve Closure
Downstream Valve Type Ind Remotely Controlled
Num Pub Evacuated 0
Pipe Fac Name Trunk C4 And C21-23 Lateral
Segment Name 843-T-T-T
Onshore State Abbreviation Ks
Onshore Postal Code 66901
Onshore City Name Not Within A Municipality
Onshore County Name Rice
Designated Location Survey Station No.
Designated Name 1+50
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 108
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Puddle Weld Ind No
Pipe Diameter 8
Pipe Wall Thickness 0.188
Pipe Smys 35000
Pipe Specification 5l
Pipe Seam Type Erw - High Frequency
Pipe Manufacturer Unknown
Pipe Coating Type Cold Applied Tape
Coating Applied Ind Yes
Installation Year Unknown
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 1000
Est Cost Prop Damage 1000000
Est Cost Emergency 1400
Est Cost Environmental 2000
Est Cost Other 0
Prpty 1004400
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 438
Mop Psig 740
Mop Cfr Section Component Design Pressure �195.406(A)(2) View CFR 49 §192
Maop Established Date 2012-06-14 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 1500
Internal Inspection Ind No
Other Inspection Ind Yes
Internal Inspection Details Station Piping. Ili Tool Accommodation Is Not Required.
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Controller's action in this accident could not be a contributing factor as no alarms or alerts occurred requiring a response from the controller.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details External Corrosion
Internal External External Corrosion
Visual Exam Results Localized Pitting
Galvanic Corrosion Ind Yes
Field Exam Basis Ind Yes
Underground Location Yes
Under Cathodic Protection Ind Yes
Cathodic Pro Start Year 2005
Shielding Evident Yes
Cathodic Survey Type Yes
Cp Annual Survey Ind Yes
Cp Annual Survey Year 2023
Prior Damage Yes
Collected Data Ind No
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 2012
Hydrtst Most Rcnt Pressure 1073
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Pwf Construction Ind Yes
Preparer Name L***** H***
Preparer Title Pipeline Safety Manager
Preparer Email L**********@w*******.com
Preparer Telephone 9182404259
Prepared Date 2024-04-11 00:00:00
Local Contact Name B**** S*****
Local Contact Email B***********@w*******.com
Local Contact Telephone 6208342140
Authorizer Name L***** H***
Authorizer Telephone 9182404259
Authorizer Title Pipeline Safety Manager
Authorizer Email L**********@w*******.com
Narrative 11/2 8:40am environmental specialist noticed a frost ball in the area and contacted supervisor who confirmed the leak as of 9:20am by use of hazgas monitor. Line segment was isolated shortly thereafter (~9:40am) and open to flare system in which remaining product in line was flared off. Extent of damage was ~10 feet in length with pin hole corrosion as primary cause of release. 3/19/2024 line was put back into service was damage segment was replaced with new pipe.

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