HL incident on 2023-11-28 — TX

Operator
Lambda Energy Gathering Llc
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$41,711
Incident datetime
2023-11-28 00:00 UTC
Report number
Location
TX
Narrative
Odor complaint generated response and investigation revealed leak on pipeline right-of-way. Lambda response personnel and osro's dispatched to area. System shut-in and isolated. Notifications made to nrc and local agencies. Drain down of segment, temporary repair with engineered clamp and sleeves, system pressure reduction until leak investigation is complete and permanent repairs made. This report is a supplemental correction as aprt of our 30-day submittal requirement.
Detailed record list
Report Received Date
2023-11-28 00:00:00
Iyear
2023
Report Number
20230284
Supplemental Number
38882
Report Type
Supplemental Final
Operator Id
Name
Lambda Energy Gathering Llc
Operator Street Address
12012 Wickchester Ln Suite 300
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77079
Time Zone
Eastern
Daylight Savings Ind
No
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
82
Recovered Bbls
32
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Emergency Responder
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Nrc Rpt Num
Additional Nrc Report Numbers
1382909
Ignite Ind
No
Upstream Action Taken
Valve Closure
Upstream Valve Type Ind
Manual
Downstream Action Taken
Valve Closure
Downstream Valve Type Ind
Manual
Notify Qualified Indiv Ind
Yes
Oil Spill Removal Org Ind
Yes
Osro Arrived On Site Dt
10/27/2023 11:30
Num Pub Evacuated
0
Pipe Fac Name
Lambda Energy Gathering Llc
Segment Name
Otsego 16-Inch
Onshore State Abbreviation
Mi
Onshore Postal Code
49646
Onshore City Name
Kalkaska
Onshore County Name
Kalkaska
Designated Location
Milepost
Designated Name
0
Federal
No
Location Type
Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
48
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Puddle Weld Ind
No
Pipe Diameter
16
Pipe Wall Thickness
0.281
Pipe Smys
52000
Pipe Specification
Api 5lx-52
Pipe Seam Type
Erw - High Frequency
Pipe Manufacturer
Republic Steel Corporation
Pipe Coating Type
Extruded Polyehylene
Coating Applied Ind
No
Installation Year
1973
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
Yes
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
28240
Est Cost Prop Damage
41711
Est Cost Emergency
147335
Est Cost Environmental
152665
Est Cost Other
0
Prpty
369951
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
74
Mop Psig
365
Mop Cfr Section
Mop Cfr Section Details
Low Stress - 20% Smys
Maop Established Date
2004-12-01 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
42768
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
=< 20% Smys Regulated Gathering
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
System pressure remained above low pressure alarm.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
External Corrosion
Internal External
External Corrosion
Visual Exam Results
Localized Pitting
Other Corrosion Ind
Yes
Corrosion Type Details
Leak Is Under Investigation With Affected Piece Scheduled To Be Sent To Metallurgical Laboratory For Analysis And Positive Identification.
Other Basis Ind
Yes
Corrosion Basis Details
Under Investigation.
Underground Location
Yes
Under Cathodic Protection Ind
Yes
Cathodic Pro Start Year
1973
Shielding Evident
No
Cathodic Survey Type
Yes
Cp Annual Survey Ind
Yes
Close Interval Survey Ind
Yes
Cp Annual Survey Year
2023
Close Interval Survey Year
2019
Other Cp Survey Details
Ecda Completed In 2022 & 2023 (Following Leak Incident).
Prior Damage
No
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Geometry Deformation Ind
Yes
Axial Recent Year
2022
Axial Rcnt Propul Method
Free Swimming
Axial Rcnt Attuned Detect
Metal Loss
Axial Rcnt Atnd Dtct Metal
High Resolution
Axial Previous Year
2018
Axial Prev Propul Method
Free Swimming
Axial Prev Attuned Detect
Metal Loss
Axial Prev Atnd Dtct Metal
High Resolution
Geometry Recent Year
2022
Geometry Rcnt Propul Method
Free Swimming
Geometry Rcnt Resolution
High Resolution
Geometrt Rcnt Measur Cups
Inside Ili Cups
Geometry Previous Year
2018
Geometry Prev Propul Method
Free Swimming
Geometry Prev Resolution
High Resolution
Geometrt Prev Measur Cups
Inside Ili Cups
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
Yes, But The Point Of The Accident Was Not Identified As A Dig Site
Direct Asmnt Pnt Not Idntf Yr
2023
Asmnt Ecda Rcnt Ind
Yes
Asmnt Ecda Rcnt Year
2023
Asmnt Other Rcnt Ind
Yes
Asmnt Other Type
Scanned
Asmnt Other Rcnt Year
2023
Non Destructive Exam Ind
No
Preparer Name
J**** M******
Preparer Title
Plant And Pipeline Manager
Preparer Email
J*******@l**************.com
Preparer Telephone
2312586422
Prepared Date
2023-11-30 00:00:00
Local Contact Name
J**** M******
Local Contact Email
J*******@l**************.com
Local Contact Telephone
2312586422
Authorizer Name
J**** M******
Authorizer Telephone
2312586422
Authorizer Title
Plant And Pipeline Manager
Authorizer Email
J*******@l**************.com
Narrative
Odor complaint generated response and investigation revealed leak on pipeline right-of-way. Lambda response personnel and osro's dispatched to area. System shut-in and isolated. Notifications made to nrc and local agencies. Drain down of segment, temporary repair with engineered clamp and sleeves, system pressure reduction until leak investigation is complete and permanent repairs made. This report is a supplemental correction as aprt of our 30-day submittal requirement.
Report Received Date 2023-11-28 00:00:00
Iyear 2023
Report Number 20230284
Supplemental Number 38882
Report Type Supplemental Final
Operator Id 40028 PHMSA Enforcement
Name Lambda Energy Gathering Llc
Operator Street Address 12012 Wickchester Ln Suite 300
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77079
Time Zone Eastern
Daylight Savings Ind No
Location Latitude 44.5119 Google Maps OpenStreetMap
Location Longitude -84.4703 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 82
Recovered Bbls 32
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Emergency Responder
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind Yes
Nrc Rpt Num 1382792 NRC Report How to search
Additional Nrc Report Numbers 1382909
Ignite Ind No
Upstream Action Taken Valve Closure
Upstream Valve Type Ind Manual
Downstream Action Taken Valve Closure
Downstream Valve Type Ind Manual
Notify Qualified Indiv Ind Yes
Oil Spill Removal Org Ind Yes
Osro Arrived On Site Dt 10/27/2023 11:30
Num Pub Evacuated 0
Pipe Fac Name Lambda Energy Gathering Llc
Segment Name Otsego 16-Inch
Onshore State Abbreviation Mi
Onshore Postal Code 49646
Onshore City Name Kalkaska
Onshore County Name Kalkaska
Designated Location Milepost
Designated Name 0
Federal No
Location Type Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 48
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Puddle Weld Ind No
Pipe Diameter 16
Pipe Wall Thickness 0.281
Pipe Smys 52000
Pipe Specification Api 5lx-52
Pipe Seam Type Erw - High Frequency
Pipe Manufacturer Republic Steel Corporation
Pipe Coating Type Extruded Polyehylene
Coating Applied Ind No
Installation Year 1973
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment Yes
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 28240
Est Cost Prop Damage 41711
Est Cost Emergency 147335
Est Cost Environmental 152665
Est Cost Other 0
Prpty 369951
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 74
Mop Psig 365
Mop Cfr Section Other View CFR 49 §192
Mop Cfr Section Details Low Stress - 20% Smys
Maop Established Date 2004-12-01 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 42768
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function =< 20% Smys Regulated Gathering
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details System pressure remained above low pressure alarm.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details External Corrosion
Internal External External Corrosion
Visual Exam Results Localized Pitting
Other Corrosion Ind Yes
Corrosion Type Details Leak Is Under Investigation With Affected Piece Scheduled To Be Sent To Metallurgical Laboratory For Analysis And Positive Identification.
Other Basis Ind Yes
Corrosion Basis Details Under Investigation.
Underground Location Yes
Under Cathodic Protection Ind Yes
Cathodic Pro Start Year 1973
Shielding Evident No
Cathodic Survey Type Yes
Cp Annual Survey Ind Yes
Close Interval Survey Ind Yes
Cp Annual Survey Year 2023
Close Interval Survey Year 2019
Other Cp Survey Details Ecda Completed In 2022 & 2023 (Following Leak Incident).
Prior Damage No
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Geometry Deformation Ind Yes
Axial Recent Year 2022
Axial Rcnt Propul Method Free Swimming
Axial Rcnt Attuned Detect Metal Loss
Axial Rcnt Atnd Dtct Metal High Resolution
Axial Previous Year 2018
Axial Prev Propul Method Free Swimming
Axial Prev Attuned Detect Metal Loss
Axial Prev Atnd Dtct Metal High Resolution
Geometry Recent Year 2022
Geometry Rcnt Propul Method Free Swimming
Geometry Rcnt Resolution High Resolution
Geometrt Rcnt Measur Cups Inside Ili Cups
Geometry Previous Year 2018
Geometry Prev Propul Method Free Swimming
Geometry Prev Resolution High Resolution
Geometrt Prev Measur Cups Inside Ili Cups
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted Yes, But The Point Of The Accident Was Not Identified As A Dig Site
Direct Asmnt Pnt Not Idntf Yr 2023
Asmnt Ecda Rcnt Ind Yes
Asmnt Ecda Rcnt Year 2023
Asmnt Other Rcnt Ind Yes
Asmnt Other Type Scanned
Asmnt Other Rcnt Year 2023
Non Destructive Exam Ind No
Preparer Name J**** M******
Preparer Title Plant And Pipeline Manager
Preparer Email J*******@l**************.com
Preparer Telephone 2312586422
Prepared Date 2023-11-30 00:00:00
Local Contact Name J**** M******
Local Contact Email J*******@l**************.com
Local Contact Telephone 2312586422
Authorizer Name J**** M******
Authorizer Telephone 2312586422
Authorizer Title Plant And Pipeline Manager
Authorizer Email J*******@l**************.com
Narrative Odor complaint generated response and investigation revealed leak on pipeline right-of-way. Lambda response personnel and osro's dispatched to area. System shut-in and isolated. Notifications made to nrc and local agencies. Drain down of segment, temporary repair with engineered clamp and sleeves, system pressure reduction until leak investigation is complete and permanent repairs made. This report is a supplemental correction as aprt of our 30-day submittal requirement.

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