Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2023-11-21 — TX
Operator
Centurion Pipeline L.p.
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$0
Incident datetime
2023-11-21 00:00 UTC
Report number
Location
TX
Narrative
On october 25, 2023, at approximately 11:05 am cst, a centurion pipeline, l.P. (cpl) employee discovered a leak in cpl's midland station near midland, texas. Cpl determined the source of the leak to be a station sump and promptly isolated the leak. Thirty-six (36) barrels of crude oil was released and was contained completely on-site. The contaminated soil will be remediated on-site. No injuries, fatalities or fires were associated with this incident. Cpl reported the leak to the texas railroad commission, office of pipeline safety at 12:05 pm cst on october 25, 2023. Associated incident # is 2939. A notification to the national response center (nrc) was not required but made on october 25, 2023 at 12:00 cst. Associated nrc# for the initial call was 1382630. An updated 48-hour notification was made on october 27, 2023 at 8:05 am cst. Associated nrc# is 1382782. The system was operational at 12:30 pm cst but was not restarted until the 5:44 pm cst. At the time of this writing, no repairs were required and the root cause failure analysis will be completed and the resulting information submitted via supplemental report(s). Supplemental report filed on march 13, 2024: during the root cause analysis, cpl determined that the associated pump had a setting to the debounce timer that was not set to the atypical setting for the associated pump. There is no preset requirement for the debounce timer but increased duration of the debounce timer would allow for greater flexibility in the system to recover and allow for proper mitigative actions by operations personnel.
Detailed record list
Report Received Date
2023-11-21 00:00:00
Iyear
2023
Report Number
20230281
Supplemental Number
39319
Report Type
Supplemental Final
Operator Id
31888
Name
Centurion Pipeline L.p.
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Time Zone
Central
Daylight Savings Ind
No
Location Latitude
32.004507
Location Longitude
-102.03968
Commodity Released Type
Crude Oil
Unintentional Release Bbls
36
Recovered Bbls
36
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Communication State Fed Ind
No
Nrc Rpt Num
1382630
Additional Nrc Report Numbers
1382782
Ignite Ind
No
Notify Qualified Indiv Ind
Yes
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Midland Station
Segment Name
Mtf Sump
Onshore State Abbreviation
Tx
Onshore Postal Code
79706
Onshore City Name
Not Within A Municipality
Onshore County Name
Midland
Designated Location
Milepost
Designated Name
Midland Sta.
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
In Underground Enclosed Space (E.g. Vault)
Depth Of Cover
Unknown
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Sump
Installation Year
2020
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Overfill Or Overflow
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
546
Est Cost Prop Damage
0
Est Cost Emergency
3000
Est Cost Environmental
31000
Est Cost Other
0
Prpty
34546
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
309
Mop Psig
1480
Mop Cfr Section
Subpart E Pressure Test �195.406(A)(3)
Maop Established Date
2020-10-21 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Operation Type
Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Overflow Other Ind
Other
Overflow Other Details
Associated Pump's Debounce Timer Setting Was Updated To Atypical Operational Settings.
Related Other Ind
Yes
Operation Related Details
There Is No Procedural Issue As The Debounce Timer Does Not Have A Specific Setting For Sump Pumps At Installation And Should Be Modified At The Discretion Of Operations Personnel.
Category Type
Construction
Operator Qualification Ind
No
Preparer Name
Y*** T*
Preparer Title
Senior Dot Compliance Specialist
Preparer Email
Y******@e*************.com
Preparer Telephone
281-748-8205
Prepared Date
2024-03-13 00:00:00
Authorizer Name
T***** D*****
Authorizer Telephone
281-808-9234
Authorizer Title
Dot Compliance Manager
Authorizer Email
T************@e*************.com
Narrative
On october 25, 2023, at approximately 11:05 am cst, a centurion pipeline, l.P. (cpl) employee discovered a leak in cpl's midland station near midland, texas. Cpl determined the source of the leak to be a station sump and promptly isolated the leak. Thirty-six (36) barrels of crude oil was released and was contained completely on-site. The contaminated soil will be remediated on-site. No injuries, fatalities or fires were associated with this incident. Cpl reported the leak to the texas railroad commission, office of pipeline safety at 12:05 pm cst on october 25, 2023. Associated incident # is 2939. A notification to the national response center (nrc) was not required but made on october 25, 2023 at 12:00 cst. Associated nrc# for the initial call was 1382630. An updated 48-hour notification was made on october 27, 2023 at 8:05 am cst. Associated nrc# is 1382782. The system was operational at 12:30 pm cst but was not restarted until the 5:44 pm cst. At the time of this writing, no repairs were required and the root cause failure analysis will be completed and the resulting information submitted via supplemental report(s). Supplemental report filed on march 13, 2024: during the root cause analysis, cpl determined that the associated pump had a setting to the debounce timer that was not set to the atypical setting for the associated pump. There is no preset requirement for the debounce timer but increased duration of the debounce timer would allow for greater flexibility in the system to recover and allow for proper mitigative actions by operations personnel.
Report Received Date | 2023-11-21 00:00:00 |
---|---|
Iyear | 2023 |
Report Number | 20230281 |
Supplemental Number | 39319 |
Report Type | Supplemental Final |
Operator Id | 31888 PHMSA Enforcement |
Name | Centurion Pipeline L.p. |
Operator Street Address | 1300 Main Street |
Operator City Name | Houston |
Operator State Abbreviation | TX |
Operator Postal Code | 77002 |
Time Zone | Central |
Daylight Savings Ind | No |
Location Latitude | 32.004507 Google Maps OpenStreetMap |
Location Longitude | -102.03968 Google Maps OpenStreetMap |
Commodity Released Type | Crude Oil |
Unintentional Release Bbls | 36 |
Recovered Bbls | 36 |
Fatality Ind | No |
Fatal | 0 |
Injury Ind | No |
Injure | 0 |
Accident Identifier | Local Operating Personnel, Including Contractors |
Operator Type | Operator Employee |
System Part Involved | Onshore Terminal/tank Farm Equipment And Piping |
On Off Shore | Onshore |
Status When Identified | Normal Operation, Includes Pauses Between Batches And During Maintenance |
Shutdown Due Accident Ind | Yes |
Communication State Fed Ind | No |
Nrc Rpt Num | 1382630 NRC Report How to search |
Additional Nrc Report Numbers | 1382782 |
Ignite Ind | No |
Notify Qualified Indiv Ind | Yes |
Oil Spill Removal Org Ind | No |
Num Pub Evacuated | 0 |
Pipe Fac Name | Midland Station |
Segment Name | Mtf Sump |
Onshore State Abbreviation | Tx |
Onshore Postal Code | 79706 |
Onshore City Name | Not Within A Municipality |
Onshore County Name | Midland |
Designated Location | Milepost |
Designated Name | Midland Sta. |
Federal | No |
Location Type | Totally Contained On Operator-Controlled Property |
Incident Area Type | Underground |
Incident Area Subtype | In Underground Enclosed Space (E.g. Vault) |
Depth Of Cover | Unknown |
Crossing | No |
Pipe Facility Type | Intrastate |
Item Involved | Sump |
Installation Year | 2020 |
Manufactured Year | Unknown |
Material Involved | Carbon Steel |
Release Type | Overfill Or Overflow |
Wildlife Impact Ind | No |
Soil Contamination | Yes |
Long Term Assessment | No |
Remediation Ind | Yes |
Soil Remed Ind | Yes |
Water Contam Ind | No |
Could Be Hca | No |
Commodity Reached Hca | No |
Est Cost Oper Paid | 0 |
Est Cost Gas Released | 546 |
Est Cost Prop Damage | 0 |
Est Cost Emergency | 3000 |
Est Cost Environmental | 31000 |
Est Cost Other | 0 |
Prpty | 34546 |
Num Persons Hosp Not Ovnght | 0 |
Num Injured Treated By Emt | 0 |
Num Resident Building Affctd | 0 |
Num Business Building Affctd | 0 |
Accident Psig | 309 |
Mop Psig | 1480 |
Mop Cfr Section | Subpart E Pressure Test �195.406(A)(3) View CFR 49 §192 |
Maop Established Date | 2020-10-21 00:00:00 |
Maop Reversal Flow Ind | No |
Accident Pressure | Pressure Did Not Exceed Mop |
Pressure Restriction Ind | No |
Pipeline Function | > 20% Smys Regulated Transmission |
Scada In Place Ind | No |
Cpm In Place Ind | No |
Investigation Status | No, the facility was not monitored by a controller(s) at the time of the accident |
Employee Drug Test Ind | No |
Contractor Drug Test Ind | No |
Cause | Incorrect Operation |
Cause Details | Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow |
Operation Type | Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow |
Overflow Other Ind | Other |
Overflow Other Details | Associated Pump's Debounce Timer Setting Was Updated To Atypical Operational Settings. |
Related Other Ind | Yes |
Operation Related Details | There Is No Procedural Issue As The Debounce Timer Does Not Have A Specific Setting For Sump Pumps At Installation And Should Be Modified At The Discretion Of Operations Personnel. |
Category Type | Construction |
Operator Qualification Ind | No |
Preparer Name | Y*** T* |
Preparer Title | Senior Dot Compliance Specialist |
Preparer Email | Y******@e*************.com |
Preparer Telephone | 281-748-8205 |
Prepared Date | 2024-03-13 00:00:00 |
Authorizer Name | T***** D***** |
Authorizer Telephone | 281-808-9234 |
Authorizer Title | Dot Compliance Manager |
Authorizer Email | T************@e*************.com |
Narrative | On october 25, 2023, at approximately 11:05 am cst, a centurion pipeline, l.P. (cpl) employee discovered a leak in cpl's midland station near midland, texas. Cpl determined the source of the leak to be a station sump and promptly isolated the leak. Thirty-six (36) barrels of crude oil was released and was contained completely on-site. The contaminated soil will be remediated on-site. No injuries, fatalities or fires were associated with this incident. Cpl reported the leak to the texas railroad commission, office of pipeline safety at 12:05 pm cst on october 25, 2023. Associated incident # is 2939. A notification to the national response center (nrc) was not required but made on october 25, 2023 at 12:00 cst. Associated nrc# for the initial call was 1382630. An updated 48-hour notification was made on october 27, 2023 at 8:05 am cst. Associated nrc# is 1382782. The system was operational at 12:30 pm cst but was not restarted until the 5:44 pm cst. At the time of this writing, no repairs were required and the root cause failure analysis will be completed and the resulting information submitted via supplemental report(s). Supplemental report filed on march 13, 2024: during the root cause analysis, cpl determined that the associated pump had a setting to the debounce timer that was not set to the atypical setting for the associated pump. There is no preset requirement for the debounce timer but increased duration of the debounce timer would allow for greater flexibility in the system to recover and allow for proper mitigative actions by operations personnel. |
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