Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2023-11-16 — IL
Operator
Amoco Oil Co
Cause
Material Failure Of Pipe Or Weld
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$1,301,000
Incident datetime
2023-11-16 00:00 UTC
Report number
Location
IL
Narrative
At 9:24 p.M. Et, the tulsa control center received a pressure drop at girard station followed by a leak alarm at 9:30 p.M. Et. The line was shutdown at 9:33 p.M. Et. Field crews were mobilized and the leak was identified at mp-138. There were no injuries associated with this incident. An oil spill response organization (osro) was mobilized to support leak response and an incident management team (imt) was stood up to manage the response. Upon excavation of the pipeline, the leak source was determined to be at the site of a repair sleeve, which was installed in 1971 over mechanical damage. The pipeline segment, including the repair sleeve, was cut-out and sent to a laboratory for metallurgical evaluation. The evaluation determined that the carrier pipe failed as a result of a crack initiated from the mechanical damage that grew by a combination of fatigue and brittle propagation until it reached critical size. The failure of the carrier pipe pressurized the repair sleeve. The evaluation further determined that the repair sleeve long seam weld design and underfill of the repair sleeve long seam weld were factors contributing to the ductile failure of a repair sleeve long seam weld.
Detailed record list
Report Received Date
2023-11-16 00:00:00
Iyear
2023
Report Number
20230276
Supplemental Number
39715
Report Type
Supplemental Final
Operator Id
Name
Amoco Oil Co
Operator Street Address
30 S. Wacker Drive
Operator City Name
Chicago
Operator State Abbreviation
IL
Operator Postal Code
60606
Time Zone
Eastern
Daylight Savings Ind
No
Location Latitude
42.045905
Location Longitude
-85.024635
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
307
Recovered Bbls
5
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Cpm Leak Detection System
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Communication State Fed Ind
Yes
Party Initiated Communication
Local/state/federal Emergency Responder
Nrc Rpt Num
1382037
Additional Nrc Report Numbers
1382212
Ignite Ind
No
Upstream Action Taken
Operational Control
Upstream Oprtnl Cntrl Detail
21:31 Controller Shut Down The Pumps At Whiting And South Bend Stations To Shut Down The Pipeline.
Downstream Action Taken
Valve Closure
Downstream Valve Type Ind
Automatic
Notify Qualified Indiv Ind
Yes
Oil Spill Removal Org Ind
Yes
Osro Arrived On Site Dt
10/18/2023 0:30
Num Pub Evacuated
0
Pipe Fac Name
Whiting To River Rouge
Segment Name
Colon Jct To River Rouge
Onshore State Abbreviation
Mi
Onshore Postal Code
49094
Onshore City Name
Union City
Onshore County Name
Branch
Designated Location
Milepost
Designated Name
138.4
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
36
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Weld, Including Heat-Affected Zone
Weld Subtype
Fillet Weld
Installation Year
1971
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Rupture
Rupture Orient
Longitudinal
Rupture Width
0.2
Rupture Length
4.3
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
Yes
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
15400
Est Cost Gas Released
45500
Est Cost Prop Damage
1301000
Est Cost Emergency
1825500
Est Cost Environmental
1541100
Est Cost Other
0
Prpty
4728500
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
1024
Mop Psig
1438
Mop Cfr Section
Component Design Pressure �195.406(A)(2)
Maop Established Date
1953-01-01 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
Yes
Cpm Conf Ind
Yes
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The pipeline controller responded appropriately to the leak alarm shutting down the pipeline and made the appropriate notifications to get the field technician to respond.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Design-, Construction-, Installation-, Or Fabrication-Related
Metallurgical Ind
Yes
Failure Type
Design-, Construction-, Installation-, Or Fabrication-Related
Mechanical Stress
Yes
Additional Dent Ind
Yes
Collected Data Ind
Yes
Ultrasonic Ind
Yes
Geometry Deformation Ind
Yes
Ultrasonic Recent Year
2022
Ultrasonic Rcnt Propul Method
Free Swimming
Ultrasonic Rcnt Attuned
Wall Measurement
Utra Rcnt Att Metl Resolution
Standard Resolution
Ultr Previous Year
2021
Ultra Prev Propul Method
Free Swimming
Ultra Prev Attuned
Crack
Geometry Recent Year
2022
Geometry Rcnt Propul Method
Free Swimming
Geometry Rcnt Resolution
High Resolution
Geometrt Rcnt Measur Cups
Inside Ili Cups
Geometry Previous Year
2016
Geometry Prev Propul Method
Free Swimming
Geometry Prev Resolution
High Resolution
Geometrt Prev Measur Cups
Inside Ili Cups
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Excvtn Dmg Previous Damage Ind
Yes
Preparer Name
S**** L*** F*********
Preparer Title
Dot Compliance Advisor
Preparer Email
F*****@b*.com
Preparer Telephone
2812173703
Prepared Date
2024-06-25 00:00:00
Local Contact Name
D**** M*******
Local Contact Email
D*************@b*.com
Local Contact Telephone
2193708004
Authorizer Name
T****** S****
Authorizer Telephone
6306061404
Authorizer Title
Compliance Manager
Authorizer Email
T************@b*.com
Narrative
At 9:24 p.M. Et, the tulsa control center received a pressure drop at girard station followed by a leak alarm at 9:30 p.M. Et. The line was shutdown at 9:33 p.M. Et. Field crews were mobilized and the leak was identified at mp-138. There were no injuries associated with this incident. An oil spill response organization (osro) was mobilized to support leak response and an incident management team (imt) was stood up to manage the response. Upon excavation of the pipeline, the leak source was determined to be at the site of a repair sleeve, which was installed in 1971 over mechanical damage. The pipeline segment, including the repair sleeve, was cut-out and sent to a laboratory for metallurgical evaluation. The evaluation determined that the carrier pipe failed as a result of a crack initiated from the mechanical damage that grew by a combination of fatigue and brittle propagation until it reached critical size. The failure of the carrier pipe pressurized the repair sleeve. The evaluation further determined that the repair sleeve long seam weld design and underfill of the repair sleeve long seam weld were factors contributing to the ductile failure of a repair sleeve long seam weld.
Report Received Date | 2023-11-16 00:00:00 |
---|---|
Iyear | 2023 |
Report Number | 20230276 |
Supplemental Number | 39715 |
Report Type | Supplemental Final |
Operator Id | 395 PHMSA Enforcement |
Name | Amoco Oil Co |
Operator Street Address | 30 S. Wacker Drive |
Operator City Name | Chicago |
Operator State Abbreviation | IL |
Operator Postal Code | 60606 |
Time Zone | Eastern |
Daylight Savings Ind | No |
Location Latitude | 42.045905 Google Maps OpenStreetMap |
Location Longitude | -85.024635 Google Maps OpenStreetMap |
Commodity Released Type | Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions |
Commodity Subtype | Gasoline (Non-Ethanol) |
Unintentional Release Bbls | 307 |
Recovered Bbls | 5 |
Fatality Ind | No |
Fatal | 0 |
Injury Ind | No |
Injure | 0 |
Accident Identifier | Cpm Leak Detection System |
System Part Involved | Onshore Pipeline, Including Valve Sites |
On Off Shore | Onshore |
Status When Identified | Normal Operation, Includes Pauses Between Batches And During Maintenance |
Shutdown Due Accident Ind | Yes |
Communication State Fed Ind | Yes |
Party Initiated Communication | Local/state/federal Emergency Responder |
Nrc Rpt Num | 1382037 NRC Report How to search |
Additional Nrc Report Numbers | 1382212 |
Ignite Ind | No |
Upstream Action Taken | Operational Control |
Upstream Oprtnl Cntrl Detail | 21:31 Controller Shut Down The Pumps At Whiting And South Bend Stations To Shut Down The Pipeline. |
Downstream Action Taken | Valve Closure |
Downstream Valve Type Ind | Automatic |
Notify Qualified Indiv Ind | Yes |
Oil Spill Removal Org Ind | Yes |
Osro Arrived On Site Dt | 10/18/2023 0:30 |
Num Pub Evacuated | 0 |
Pipe Fac Name | Whiting To River Rouge |
Segment Name | Colon Jct To River Rouge |
Onshore State Abbreviation | Mi |
Onshore Postal Code | 49094 |
Onshore City Name | Union City |
Onshore County Name | Branch |
Designated Location | Milepost |
Designated Name | 138.4 |
Federal | No |
Location Type | Pipeline Right-Of-Way |
Incident Area Type | Underground |
Incident Area Subtype | Under Soil |
Depth Of Cover | 36 |
Crossing | No |
Pipe Facility Type | Interstate |
Item Involved | Weld, Including Heat-Affected Zone |
Weld Subtype | Fillet Weld |
Installation Year | 1971 |
Manufactured Year | Unknown |
Material Involved | Carbon Steel |
Release Type | Rupture |
Rupture Orient | Longitudinal |
Rupture Width | 0.2 |
Rupture Length | 4.3 |
Wildlife Impact Ind | No |
Soil Contamination | Yes |
Long Term Assessment | Yes |
Remediation Ind | No |
Water Contam Ind | No |
Could Be Hca | Yes |
Commodity Reached Hca | No |
Est Cost Oper Paid | 15400 |
Est Cost Gas Released | 45500 |
Est Cost Prop Damage | 1301000 |
Est Cost Emergency | 1825500 |
Est Cost Environmental | 1541100 |
Est Cost Other | 0 |
Prpty | 4728500 |
Num Persons Hosp Not Ovnght | 0 |
Num Injured Treated By Emt | 0 |
Num Resident Building Affctd | 0 |
Num Business Building Affctd | 0 |
Accident Psig | 1024 |
Mop Psig | 1438 |
Mop Cfr Section | Component Design Pressure �195.406(A)(2) View CFR 49 §192 |
Maop Established Date | 1953-01-01 00:00:00 |
Maop Reversal Flow Ind | No |
Accident Pressure | Pressure Did Not Exceed Mop |
Pressure Restriction Ind | No |
Internal Inspection Ind | Yes |
Operation Complications Ind | No |
Pipeline Function | > 20% Smys Regulated Transmission |
Scada In Place Ind | Yes |
Scada Operating Ind | Yes |
Scada Functional Ind | Yes |
Scada Detection Ind | Yes |
Scada Conf Ind | Yes |
Cpm In Place Ind | Yes |
Cpm Operating Ind | Yes |
Cpm Functional Ind | Yes |
Cpm Detection Ind | Yes |
Cpm Conf Ind | Yes |
Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
Investigation Status Details | The pipeline controller responded appropriately to the leak alarm shutting down the pipeline and made the appropriate notifications to get the field technician to respond. |
Employee Drug Test Ind | No |
Contractor Drug Test Ind | No |
Cause | Material Failure Of Pipe Or Weld |
Cause Details | Design-, Construction-, Installation-, Or Fabrication-Related |
Metallurgical Ind | Yes |
Failure Type | Design-, Construction-, Installation-, Or Fabrication-Related |
Mechanical Stress | Yes |
Additional Dent Ind | Yes |
Collected Data Ind | Yes |
Ultrasonic Ind | Yes |
Geometry Deformation Ind | Yes |
Ultrasonic Recent Year | 2022 |
Ultrasonic Rcnt Propul Method | Free Swimming |
Ultrasonic Rcnt Attuned | Wall Measurement |
Utra Rcnt Att Metl Resolution | Standard Resolution |
Ultr Previous Year | 2021 |
Ultra Prev Propul Method | Free Swimming |
Ultra Prev Attuned | Crack |
Geometry Recent Year | 2022 |
Geometry Rcnt Propul Method | Free Swimming |
Geometry Rcnt Resolution | High Resolution |
Geometrt Rcnt Measur Cups | Inside Ili Cups |
Geometry Previous Year | 2016 |
Geometry Prev Propul Method | Free Swimming |
Geometry Prev Resolution | High Resolution |
Geometrt Prev Measur Cups | Inside Ili Cups |
Has Hydrtst Conduc Before Ind | No |
Direct Asmnt Conducted | No |
Non Destructive Exam Ind | No |
Excvtn Dmg Previous Damage Ind | Yes |
Preparer Name | S**** L*** F********* |
Preparer Title | Dot Compliance Advisor |
Preparer Email | F*****@b*.com |
Preparer Telephone | 2812173703 |
Prepared Date | 2024-06-25 00:00:00 |
Local Contact Name | D**** M******* |
Local Contact Email | D*************@b*.com |
Local Contact Telephone | 2193708004 |
Authorizer Name | T****** S**** |
Authorizer Telephone | 6306061404 |
Authorizer Title | Compliance Manager |
Authorizer Email | T************@b*.com |
Narrative | At 9:24 p.M. Et, the tulsa control center received a pressure drop at girard station followed by a leak alarm at 9:30 p.M. Et. The line was shutdown at 9:33 p.M. Et. Field crews were mobilized and the leak was identified at mp-138. There were no injuries associated with this incident. An oil spill response organization (osro) was mobilized to support leak response and an incident management team (imt) was stood up to manage the response. Upon excavation of the pipeline, the leak source was determined to be at the site of a repair sleeve, which was installed in 1971 over mechanical damage. The pipeline segment, including the repair sleeve, was cut-out and sent to a laboratory for metallurgical evaluation. The evaluation determined that the carrier pipe failed as a result of a crack initiated from the mechanical damage that grew by a combination of fatigue and brittle propagation until it reached critical size. The failure of the carrier pipe pressurized the repair sleeve. The evaluation further determined that the repair sleeve long seam weld design and underfill of the repair sleeve long seam weld were factors contributing to the ductile failure of a repair sleeve long seam weld. |
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