HL incident on 2023-11-16 — IL

Operator
Amoco Oil Co
Cause
Material Failure Of Pipe Or Weld
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,301,000
Incident datetime
2023-11-16 00:00 UTC
Report number
Location
IL
Narrative
At 9:24 p.M. Et, the tulsa control center received a pressure drop at girard station followed by a leak alarm at 9:30 p.M. Et. The line was shutdown at 9:33 p.M. Et. Field crews were mobilized and the leak was identified at mp-138. There were no injuries associated with this incident. An oil spill response organization (osro) was mobilized to support leak response and an incident management team (imt) was stood up to manage the response. Upon excavation of the pipeline, the leak source was determined to be at the site of a repair sleeve, which was installed in 1971 over mechanical damage. The pipeline segment, including the repair sleeve, was cut-out and sent to a laboratory for metallurgical evaluation. The evaluation determined that the carrier pipe failed as a result of a crack initiated from the mechanical damage that grew by a combination of fatigue and brittle propagation until it reached critical size. The failure of the carrier pipe pressurized the repair sleeve. The evaluation further determined that the repair sleeve long seam weld design and underfill of the repair sleeve long seam weld were factors contributing to the ductile failure of a repair sleeve long seam weld.
Detailed record list
Report Received Date
2023-11-16 00:00:00
Iyear
2023
Report Number
20230276
Supplemental Number
39715
Report Type
Supplemental Final
Operator Id
Name
Amoco Oil Co
Operator Street Address
30 S. Wacker Drive
Operator City Name
Chicago
Operator State Abbreviation
IL
Operator Postal Code
60606
Time Zone
Eastern
Daylight Savings Ind
No
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
307
Recovered Bbls
5
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Cpm Leak Detection System
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Communication State Fed Ind
Yes
Party Initiated Communication
Local/state/federal Emergency Responder
Nrc Rpt Num
Additional Nrc Report Numbers
1382212
Ignite Ind
No
Upstream Action Taken
Operational Control
Upstream Oprtnl Cntrl Detail
21:31 Controller Shut Down The Pumps At Whiting And South Bend Stations To Shut Down The Pipeline.
Downstream Action Taken
Valve Closure
Downstream Valve Type Ind
Automatic
Notify Qualified Indiv Ind
Yes
Oil Spill Removal Org Ind
Yes
Osro Arrived On Site Dt
10/18/2023 0:30
Num Pub Evacuated
0
Pipe Fac Name
Whiting To River Rouge
Segment Name
Colon Jct To River Rouge
Onshore State Abbreviation
Mi
Onshore Postal Code
49094
Onshore City Name
Union City
Onshore County Name
Branch
Designated Location
Milepost
Designated Name
138.4
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
36
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Weld, Including Heat-Affected Zone
Weld Subtype
Fillet Weld
Installation Year
1971
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Rupture
Rupture Orient
Longitudinal
Rupture Width
0.2
Rupture Length
4.3
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
Yes
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
15400
Est Cost Gas Released
45500
Est Cost Prop Damage
1301000
Est Cost Emergency
1825500
Est Cost Environmental
1541100
Est Cost Other
0
Prpty
4728500
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
1024
Mop Psig
1438
Mop Cfr Section
Component Design Pressure �195.406(A)(2)
Maop Established Date
1953-01-01 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
Yes
Cpm Conf Ind
Yes
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The pipeline controller responded appropriately to the leak alarm shutting down the pipeline and made the appropriate notifications to get the field technician to respond.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Design-, Construction-, Installation-, Or Fabrication-Related
Metallurgical Ind
Yes
Failure Type
Design-, Construction-, Installation-, Or Fabrication-Related
Mechanical Stress
Yes
Additional Dent Ind
Yes
Collected Data Ind
Yes
Ultrasonic Ind
Yes
Geometry Deformation Ind
Yes
Ultrasonic Recent Year
2022
Ultrasonic Rcnt Propul Method
Free Swimming
Ultrasonic Rcnt Attuned
Wall Measurement
Utra Rcnt Att Metl Resolution
Standard Resolution
Ultr Previous Year
2021
Ultra Prev Propul Method
Free Swimming
Ultra Prev Attuned
Crack
Geometry Recent Year
2022
Geometry Rcnt Propul Method
Free Swimming
Geometry Rcnt Resolution
High Resolution
Geometrt Rcnt Measur Cups
Inside Ili Cups
Geometry Previous Year
2016
Geometry Prev Propul Method
Free Swimming
Geometry Prev Resolution
High Resolution
Geometrt Prev Measur Cups
Inside Ili Cups
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Excvtn Dmg Previous Damage Ind
Yes
Preparer Name
S**** L*** F*********
Preparer Title
Dot Compliance Advisor
Preparer Email
F*****@b*.com
Preparer Telephone
2812173703
Prepared Date
2024-06-25 00:00:00
Local Contact Name
D**** M*******
Local Contact Email
D*************@b*.com
Local Contact Telephone
2193708004
Authorizer Name
T****** S****
Authorizer Telephone
6306061404
Authorizer Title
Compliance Manager
Authorizer Email
T************@b*.com
Narrative
At 9:24 p.M. Et, the tulsa control center received a pressure drop at girard station followed by a leak alarm at 9:30 p.M. Et. The line was shutdown at 9:33 p.M. Et. Field crews were mobilized and the leak was identified at mp-138. There were no injuries associated with this incident. An oil spill response organization (osro) was mobilized to support leak response and an incident management team (imt) was stood up to manage the response. Upon excavation of the pipeline, the leak source was determined to be at the site of a repair sleeve, which was installed in 1971 over mechanical damage. The pipeline segment, including the repair sleeve, was cut-out and sent to a laboratory for metallurgical evaluation. The evaluation determined that the carrier pipe failed as a result of a crack initiated from the mechanical damage that grew by a combination of fatigue and brittle propagation until it reached critical size. The failure of the carrier pipe pressurized the repair sleeve. The evaluation further determined that the repair sleeve long seam weld design and underfill of the repair sleeve long seam weld were factors contributing to the ductile failure of a repair sleeve long seam weld.
Report Received Date 2023-11-16 00:00:00
Iyear 2023
Report Number 20230276
Supplemental Number 39715
Report Type Supplemental Final
Operator Id 395 PHMSA Enforcement
Name Amoco Oil Co
Operator Street Address 30 S. Wacker Drive
Operator City Name Chicago
Operator State Abbreviation IL
Operator Postal Code 60606
Time Zone Eastern
Daylight Savings Ind No
Location Latitude 42.045905 Google Maps OpenStreetMap
Location Longitude -85.024635 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 307
Recovered Bbls 5
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Cpm Leak Detection System
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind Yes
Communication State Fed Ind Yes
Party Initiated Communication Local/state/federal Emergency Responder
Nrc Rpt Num 1382037 NRC Report How to search
Additional Nrc Report Numbers 1382212
Ignite Ind No
Upstream Action Taken Operational Control
Upstream Oprtnl Cntrl Detail 21:31 Controller Shut Down The Pumps At Whiting And South Bend Stations To Shut Down The Pipeline.
Downstream Action Taken Valve Closure
Downstream Valve Type Ind Automatic
Notify Qualified Indiv Ind Yes
Oil Spill Removal Org Ind Yes
Osro Arrived On Site Dt 10/18/2023 0:30
Num Pub Evacuated 0
Pipe Fac Name Whiting To River Rouge
Segment Name Colon Jct To River Rouge
Onshore State Abbreviation Mi
Onshore Postal Code 49094
Onshore City Name Union City
Onshore County Name Branch
Designated Location Milepost
Designated Name 138.4
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 36
Crossing No
Pipe Facility Type Interstate
Item Involved Weld, Including Heat-Affected Zone
Weld Subtype Fillet Weld
Installation Year 1971
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Rupture
Rupture Orient Longitudinal
Rupture Width 0.2
Rupture Length 4.3
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment Yes
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 15400
Est Cost Gas Released 45500
Est Cost Prop Damage 1301000
Est Cost Emergency 1825500
Est Cost Environmental 1541100
Est Cost Other 0
Prpty 4728500
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 1024
Mop Psig 1438
Mop Cfr Section Component Design Pressure �195.406(A)(2) View CFR 49 §192
Maop Established Date 1953-01-01 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind Yes
Cpm Conf Ind Yes
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The pipeline controller responded appropriately to the leak alarm shutting down the pipeline and made the appropriate notifications to get the field technician to respond.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Material Failure Of Pipe Or Weld
Cause Details Design-, Construction-, Installation-, Or Fabrication-Related
Metallurgical Ind Yes
Failure Type Design-, Construction-, Installation-, Or Fabrication-Related
Mechanical Stress Yes
Additional Dent Ind Yes
Collected Data Ind Yes
Ultrasonic Ind Yes
Geometry Deformation Ind Yes
Ultrasonic Recent Year 2022
Ultrasonic Rcnt Propul Method Free Swimming
Ultrasonic Rcnt Attuned Wall Measurement
Utra Rcnt Att Metl Resolution Standard Resolution
Ultr Previous Year 2021
Ultra Prev Propul Method Free Swimming
Ultra Prev Attuned Crack
Geometry Recent Year 2022
Geometry Rcnt Propul Method Free Swimming
Geometry Rcnt Resolution High Resolution
Geometrt Rcnt Measur Cups Inside Ili Cups
Geometry Previous Year 2016
Geometry Prev Propul Method Free Swimming
Geometry Prev Resolution High Resolution
Geometrt Prev Measur Cups Inside Ili Cups
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Excvtn Dmg Previous Damage Ind Yes
Preparer Name S**** L*** F*********
Preparer Title Dot Compliance Advisor
Preparer Email F*****@b*.com
Preparer Telephone 2812173703
Prepared Date 2024-06-25 00:00:00
Local Contact Name D**** M*******
Local Contact Email D*************@b*.com
Local Contact Telephone 2193708004
Authorizer Name T****** S****
Authorizer Telephone 6306061404
Authorizer Title Compliance Manager
Authorizer Email T************@b*.com
Narrative At 9:24 p.M. Et, the tulsa control center received a pressure drop at girard station followed by a leak alarm at 9:30 p.M. Et. The line was shutdown at 9:33 p.M. Et. Field crews were mobilized and the leak was identified at mp-138. There were no injuries associated with this incident. An oil spill response organization (osro) was mobilized to support leak response and an incident management team (imt) was stood up to manage the response. Upon excavation of the pipeline, the leak source was determined to be at the site of a repair sleeve, which was installed in 1971 over mechanical damage. The pipeline segment, including the repair sleeve, was cut-out and sent to a laboratory for metallurgical evaluation. The evaluation determined that the carrier pipe failed as a result of a crack initiated from the mechanical damage that grew by a combination of fatigue and brittle propagation until it reached critical size. The failure of the carrier pipe pressurized the repair sleeve. The evaluation further determined that the repair sleeve long seam weld design and underfill of the repair sleeve long seam weld were factors contributing to the ductile failure of a repair sleeve long seam weld.

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