HL incident on 2023-11-15 — TX

Operator
Western Midstream Partners, Lp
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$15,000
Incident datetime
2023-11-15 00:00 UTC
Report number
Location
TX
Narrative
Received notification from nearby operator of leak. Pinhole leak formed in the line allowing an estimated 17.21 bbls. Of oil to be released to the ground. Line repaired 10/24 and placed back in service.
Detailed record list
Report Received Date
2023-11-15 00:00:00
Iyear
2023
Report Number
20230275
Supplemental Number
39156
Report Type
Supplemental Final
Operator Id
Name
Western Midstream Partners, Lp
Operator Street Address
9950 Woodloch Forest Dr Suite 2800
Operator City Name
The Woodlands
Operator State Abbreviation
TX
Operator Postal Code
77380
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
17.21
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Communication State Fed Ind
No
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Upstream Action Taken
Valve Closure
Upstream Valve Type Ind
Manual
Downstream Action Taken
Valve Closure
Downstream Valve Type Ind
Manual
Notify Qualified Indiv Ind
Yes
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Dbm Oil Services Llc
Segment Name
Rotf Common Oil Header 12"
Onshore State Abbreviation
Tx
Onshore Postal Code
79754
Onshore City Name
Not Within A Municipality
Onshore County Name
Loving
Designated Location
Survey Station No.
Designated Name
392+19'
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Puddle Weld Ind
No
Pipe Diameter
12
Pipe Wall Thickness
0.375
Pipe Smys
52000
Pipe Specification
Api 5l
Pipe Seam Type
Erw - High Frequency
Pipe Manufacturer
Axis
Pipe Coating Type
Fusion Bonded Epoxy(Fbe)
Coating Applied Ind
No
Installation Year
2019
Manufactured Year
2019
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
Under Investigation
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
15000
Est Cost Emergency
0
Est Cost Environmental
10000
Est Cost Other
0
Prpty
25000
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
372
Mop Psig
1440
Mop Cfr Section
Subpart E Pressure Test �195.406(A)(3)
Maop Established Date
2019-05-04 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
1572
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Leak size was too small to be detected by controller
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Microbiological Ind
Yes
Int Metallurgical Basis Ind
Yes
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
Yes
Corrosion Lining
Yes
Cleaning Dewatering
Yes
Corrosion Coupons
Yes
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Geometry Deformation Ind
Yes
Axial Recent Year
2023
Axial Rcnt Propul Method
Free Swimming
Axial Rcnt Attuned Detect
Metal Loss
Axial Rcnt Atnd Dtct Metal
High Resolution
Geometry Recent Year
2023
Geometry Rcnt Propul Method
Free Swimming
Geometry Rcnt Resolution
High Resolution
Geometrt Rcnt Measur Cups
No Cups
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
S***** W****
Preparer Title
Dot Advisor
Preparer Email
S***********@w***************.com
Preparer Telephone
3467865148
Prepared Date
2024-02-05 00:00:00
Local Contact Name
D*** A*******
Local Contact Email
D************@w***************.com
Local Contact Telephone
4322474560
Authorizer Name
C**** T*****
Authorizer Telephone
4322474158
Authorizer Title
Supervisor Operations
Authorizer Email
C***********@w***************.com
Narrative
Received notification from nearby operator of leak. Pinhole leak formed in the line allowing an estimated 17.21 bbls. Of oil to be released to the ground. Line repaired 10/24 and placed back in service.
Report Received Date 2023-11-15 00:00:00
Iyear 2023
Report Number 20230275
Supplemental Number 39156
Report Type Supplemental Final
Operator Id 473 PHMSA Enforcement
Name Western Midstream Partners, Lp
Operator Street Address 9950 Woodloch Forest Dr Suite 2800
Operator City Name The Woodlands
Operator State Abbreviation TX
Operator Postal Code 77380
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 31.751294 Google Maps OpenStreetMap
Location Longitude -103.629923 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 17.21
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Public
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind Yes
Communication State Fed Ind No
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Upstream Action Taken Valve Closure
Upstream Valve Type Ind Manual
Downstream Action Taken Valve Closure
Downstream Valve Type Ind Manual
Notify Qualified Indiv Ind Yes
Oil Spill Removal Org Ind No
Num Pub Evacuated 0
Pipe Fac Name Dbm Oil Services Llc
Segment Name Rotf Common Oil Header 12"
Onshore State Abbreviation Tx
Onshore Postal Code 79754
Onshore City Name Not Within A Municipality
Onshore County Name Loving
Designated Location Survey Station No.
Designated Name 392+19'
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Puddle Weld Ind No
Pipe Diameter 12
Pipe Wall Thickness 0.375
Pipe Smys 52000
Pipe Specification Api 5l
Pipe Seam Type Erw - High Frequency
Pipe Manufacturer Axis
Pipe Coating Type Fusion Bonded Epoxy(Fbe)
Coating Applied Ind No
Installation Year 2019
Manufactured Year 2019
Material Involved Carbon Steel
Release Type Leak
Leak Type Other
Leak Type Other Under Investigation
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 15000
Est Cost Emergency 0
Est Cost Environmental 10000
Est Cost Other 0
Prpty 25000
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 372
Mop Psig 1440
Mop Cfr Section Subpart E Pressure Test �195.406(A)(3) View CFR 49 §192
Maop Established Date 2019-05-04 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 1572
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Leak size was too small to be detected by controller
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Localized Pitting
Int Microbiological Ind Yes
Int Metallurgical Basis Ind Yes
Int Low Point Pipe Loc Ind Yes
Corrosion Inhibitors Yes
Corrosion Lining Yes
Cleaning Dewatering Yes
Corrosion Coupons Yes
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Geometry Deformation Ind Yes
Axial Recent Year 2023
Axial Rcnt Propul Method Free Swimming
Axial Rcnt Attuned Detect Metal Loss
Axial Rcnt Atnd Dtct Metal High Resolution
Geometry Recent Year 2023
Geometry Rcnt Propul Method Free Swimming
Geometry Rcnt Resolution High Resolution
Geometrt Rcnt Measur Cups No Cups
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name S***** W****
Preparer Title Dot Advisor
Preparer Email S***********@w***************.com
Preparer Telephone 3467865148
Prepared Date 2024-02-05 00:00:00
Local Contact Name D*** A*******
Local Contact Email D************@w***************.com
Local Contact Telephone 4322474560
Authorizer Name C**** T*****
Authorizer Telephone 4322474158
Authorizer Title Supervisor Operations
Authorizer Email C***********@w***************.com
Narrative Received notification from nearby operator of leak. Pinhole leak formed in the line allowing an estimated 17.21 bbls. Of oil to be released to the ground. Line repaired 10/24 and placed back in service.

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