HL incident on 2023-11-13 — TX

Operator
Exxonmobil Oil Corporation
Cause
Corrosion Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$34,000
Incident datetime
2023-11-13 00:00 UTC
Report number
Location
TX
Narrative
At 9:12 a.M. On october 15, 2023, the operations control center (occ) received a call from arkema stating there was a release occurring from mc-49a ethylene line on the right-of-way outside of arkema. Immediately after being notified by arkema, occ alerted the on-duty beaumont operations first line supervisor (fls). The operation fls performed a visual inspection of the pipeline. The source of the release was located at 9:38 am. The operations fls called for additional personnel to assist in isolating the segment. Manual valve #40736 was closed by 11:00 am; this successfully isolated the segment from source pressure. The isolated section of the pipe was flared down until line pressure reached 0 psi. During this event, 250 pounds (2.04 barrels) of ethylene were released due to atmospheric corrosion located around a pinhole at the bottom of the aboveground 6" pipe. At the time of the release, the pipeline was inactive. The investigation has concluded. Operations replaced the pipe segment impacted by the atmospheric corrosion. Additionally, a valve has been installed to clarify the demarcation point.
Detailed record list
Report Received Date
2023-11-13 00:00:00
Iyear
2023
Report Number
20230269
Supplemental Number
39035
Report Type
Supplemental Final
Operator Id
Name
Exxonmobil Oil Corporation
Operator Street Address
2775 Gulf States Road
Operator City Name
Beaumont
Operator State Abbreviation
TX
Operator Postal Code
77704
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Ethylene
Unintentional Release Bbls
2.04
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Other
Accident Details
Notification From Third Party
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
No
Shutdown Explain
Pipeline Flow Was Paused Prior To Release; Affected Segment Was Isolated.
Communication State Fed Ind
No
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Upstream Action Taken
Valve Closure
Upstream Valve Type Ind
Manual
Downstream Action Taken
Operational Control
Downstream Oprtnl Cntrl Detail
Downstream Manual Valve Was Already Closed Prior To Release Due To Operational Downtime.
Num Pub Evacuated
0
Pipe Fac Name
Mc-49a Boap To Arkema Ethylene
Segment Name
Mc-49a
Onshore State Abbreviation
Tx
Onshore Postal Code
77705
Onshore City Name
Beaumont
Onshore County Name
Jefferson
Designated Location
Survey Station No.
Designated Name
18+00
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Aboveground
Incident Area Subtype
Other
Incident Area Details
Aboveground Elevated Pipe Rack
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Puddle Weld Ind
No
Pipe Diameter
6.625
Pipe Wall Thickness
0.188
Pipe Smys
52000
Pipe Specification
Api 5l X52
Pipe Seam Type
Erw - Low Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
Paint
Coating Applied Ind
Unknown
Installation Year
1966
Manufactured Year
1966
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
55
Est Cost Prop Damage
34000
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Est Cost Other Details
Flare/heater Truck, Materials, Crew, Nitrogen
Prpty
34055
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
1270
Mop Psig
1440
Mop Cfr Section
Component Design Pressure �195.406(A)(2)
Maop Established Date
2017-04-20 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Internal Inspection Ind
No
Tight Mitered Ind
Yes
Operation Complications Ind
Yes
Other Complications Ind
Yes
Inspect Comp Details
Tight Bends As Part Of Station Piping
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Operations control center did not conduct an investigation of the controller actions because the controller responded appropriately per the emergency response procedure.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
External Corrosion
Internal External
External Corrosion
Visual Exam Results
Localized Pitting
Atmosphere Corrosion Ind
Yes
Field Exam Basis Ind
Yes
Underground Location
No
Externally Coated
Yes
Prior Damage
Yes
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
2017
Hydrtst Most Rcnt Pressure
1440
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
K**** B******
Preparer Title
Pipeline Safety Advisor
Preparer Email
K************@e*********.com
Preparer Telephone
281-409-2853
Prepared Date
2024-01-03 00:00:00
Authorizer Name
L**** B******
Authorizer Telephone
(346) 474-9151
Authorizer Title
Regulatory Compliance Supervisor
Authorizer Email
L**************@e*********.com
Narrative
At 9:12 a.M. On october 15, 2023, the operations control center (occ) received a call from arkema stating there was a release occurring from mc-49a ethylene line on the right-of-way outside of arkema. Immediately after being notified by arkema, occ alerted the on-duty beaumont operations first line supervisor (fls). The operation fls performed a visual inspection of the pipeline. The source of the release was located at 9:38 am. The operations fls called for additional personnel to assist in isolating the segment. Manual valve #40736 was closed by 11:00 am; this successfully isolated the segment from source pressure. The isolated section of the pipe was flared down until line pressure reached 0 psi. During this event, 250 pounds (2.04 barrels) of ethylene were released due to atmospheric corrosion located around a pinhole at the bottom of the aboveground 6" pipe. At the time of the release, the pipeline was inactive. The investigation has concluded. Operations replaced the pipe segment impacted by the atmospheric corrosion. Additionally, a valve has been installed to clarify the demarcation point.
Report Received Date 2023-11-13 00:00:00
Iyear 2023
Report Number 20230269
Supplemental Number 39035
Report Type Supplemental Final
Operator Id 12634 PHMSA Enforcement
Name Exxonmobil Oil Corporation
Operator Street Address 2775 Gulf States Road
Operator City Name Beaumont
Operator State Abbreviation TX
Operator Postal Code 77704
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 30.05933 Google Maps OpenStreetMap
Location Longitude -94.05926 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details Ethylene
Unintentional Release Bbls 2.04
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Other
Accident Details Notification From Third Party
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind No
Shutdown Explain Pipeline Flow Was Paused Prior To Release; Affected Segment Was Isolated.
Communication State Fed Ind No
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Upstream Action Taken Valve Closure
Upstream Valve Type Ind Manual
Downstream Action Taken Operational Control
Downstream Oprtnl Cntrl Detail Downstream Manual Valve Was Already Closed Prior To Release Due To Operational Downtime.
Num Pub Evacuated 0
Pipe Fac Name Mc-49a Boap To Arkema Ethylene
Segment Name Mc-49a
Onshore State Abbreviation Tx
Onshore Postal Code 77705
Onshore City Name Beaumont
Onshore County Name Jefferson
Designated Location Survey Station No.
Designated Name 18+00
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Aboveground
Incident Area Subtype Other
Incident Area Details Aboveground Elevated Pipe Rack
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Puddle Weld Ind No
Pipe Diameter 6.625
Pipe Wall Thickness 0.188
Pipe Smys 52000
Pipe Specification Api 5l X52
Pipe Seam Type Erw - Low Frequency
Pipe Manufacturer Unknown
Pipe Coating Type Paint
Coating Applied Ind Unknown
Installation Year 1966
Manufactured Year 1966
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 55
Est Cost Prop Damage 34000
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Est Cost Other Details Flare/heater Truck, Materials, Crew, Nitrogen
Prpty 34055
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 1270
Mop Psig 1440
Mop Cfr Section Component Design Pressure �195.406(A)(2) View CFR 49 §192
Maop Established Date 2017-04-20 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Internal Inspection Ind No
Tight Mitered Ind Yes
Operation Complications Ind Yes
Other Complications Ind Yes
Inspect Comp Details Tight Bends As Part Of Station Piping
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Operations control center did not conduct an investigation of the controller actions because the controller responded appropriately per the emergency response procedure.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details External Corrosion
Internal External External Corrosion
Visual Exam Results Localized Pitting
Atmosphere Corrosion Ind Yes
Field Exam Basis Ind Yes
Underground Location No
Externally Coated Yes
Prior Damage Yes
Collected Data Ind No
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 2017
Hydrtst Most Rcnt Pressure 1440
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name K**** B******
Preparer Title Pipeline Safety Advisor
Preparer Email K************@e*********.com
Preparer Telephone 281-409-2853
Prepared Date 2024-01-03 00:00:00
Authorizer Name L**** B******
Authorizer Telephone (346) 474-9151
Authorizer Title Regulatory Compliance Supervisor
Authorizer Email L**************@e*********.com
Narrative At 9:12 a.M. On october 15, 2023, the operations control center (occ) received a call from arkema stating there was a release occurring from mc-49a ethylene line on the right-of-way outside of arkema. Immediately after being notified by arkema, occ alerted the on-duty beaumont operations first line supervisor (fls). The operation fls performed a visual inspection of the pipeline. The source of the release was located at 9:38 am. The operations fls called for additional personnel to assist in isolating the segment. Manual valve #40736 was closed by 11:00 am; this successfully isolated the segment from source pressure. The isolated section of the pipe was flared down until line pressure reached 0 psi. During this event, 250 pounds (2.04 barrels) of ethylene were released due to atmospheric corrosion located around a pinhole at the bottom of the aboveground 6" pipe. At the time of the release, the pipeline was inactive. The investigation has concluded. Operations replaced the pipe segment impacted by the atmospheric corrosion. Additionally, a valve has been installed to clarify the demarcation point.

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