HL incident on 2023-11-04 — TX

Operator
Enterprise Crude Pipeline Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$7,000
Incident datetime
2023-11-04 00:00 UTC
Report number
Location
TX
Narrative
On 10/5/2023 at 15:05 cst, enterprise pipeline technician discovered a crude leak from a stem of a head gate valve at cedar pump station, 1 barrels of oil reached the ground. The leak was isolated and soil remediated. The packing gland was replaced and valve went to normal operations.
Detailed record list
Report Received Date
2023-11-04 00:00:00
Iyear
2023
Report Number
20230262
Supplemental Number
38749
Report Type
Original Final
Operator Id
Name
Enterprise Crude Pipeline Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
1
Recovered Bbls
1
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Communication State Fed Ind
No
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Notify Qualified Indiv Ind
Yes
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Cedar Pump Station
Segment Name
S15
Onshore State Abbreviation
Tx
Onshore Postal Code
75860
Onshore City Name
Teague
Onshore County Name
Freestone
Designated Location
Milepost
Designated Name
0+00
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Mainline
Valve Mainline Type
Gate
Valve Manufacturer
Spx M&j
Installation Year
2013
Manufactured Year
2013
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
85
Est Cost Prop Damage
7000
Est Cost Emergency
0
Est Cost Environmental
30000
Est Cost Other
0
Prpty
37085
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
1300
Mop Psig
1480
Mop Cfr Section
Four Hour Test Or Operation �195.406(A)(5)
Maop Established Date
2013-12-31 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Internal packing gland failed.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Other Equipment Failure
Eq Failure Type
Other Equipment Failure
Failure Details
Packing Gland Of Valve Stem Failed
Eq Additional Other Ind
Yes
Eq Additional Other Details
Packing Gland Worn Out
Preparer Name
M****** K********
Preparer Title
Pipeline Compliance Engineer
Preparer Email
M*********@e****.com
Preparer Telephone
7133816791
Prepared Date
2023-11-04 00:00:00
Authorizer Name
S**** D****
Authorizer Telephone
713-381-5585
Authorizer Title
Senior Pipeline Compliance Manager
Authorizer Email
S******@e****.com
Narrative
On 10/5/2023 at 15:05 cst, enterprise pipeline technician discovered a crude leak from a stem of a head gate valve at cedar pump station, 1 barrels of oil reached the ground. The leak was isolated and soil remediated. The packing gland was replaced and valve went to normal operations.
Report Received Date 2023-11-04 00:00:00
Iyear 2023
Report Number 20230262
Supplemental Number 38749
Report Type Original Final
Operator Id 30829 PHMSA Enforcement
Name Enterprise Crude Pipeline Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 31.532208 Google Maps OpenStreetMap
Location Longitude -96.185686 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 1
Recovered Bbls 1
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind Yes
Communication State Fed Ind No
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Notify Qualified Indiv Ind Yes
Oil Spill Removal Org Ind No
Num Pub Evacuated 0
Pipe Fac Name Cedar Pump Station
Segment Name S15
Onshore State Abbreviation Tx
Onshore Postal Code 75860
Onshore City Name Teague
Onshore County Name Freestone
Designated Location Milepost
Designated Name 0+00
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Mainline
Valve Mainline Type Gate
Valve Manufacturer Spx M&j
Installation Year 2013
Manufactured Year 2013
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 85
Est Cost Prop Damage 7000
Est Cost Emergency 0
Est Cost Environmental 30000
Est Cost Other 0
Prpty 37085
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 1300
Mop Psig 1480
Mop Cfr Section Four Hour Test Or Operation �195.406(A)(5) View CFR 49 §192
Maop Established Date 2013-12-31 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Internal packing gland failed.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Other Equipment Failure
Eq Failure Type Other Equipment Failure
Failure Details Packing Gland Of Valve Stem Failed
Eq Additional Other Ind Yes
Eq Additional Other Details Packing Gland Worn Out
Preparer Name M****** K********
Preparer Title Pipeline Compliance Engineer
Preparer Email M*********@e****.com
Preparer Telephone 7133816791
Prepared Date 2023-11-04 00:00:00
Authorizer Name S**** D****
Authorizer Telephone 713-381-5585
Authorizer Title Senior Pipeline Compliance Manager
Authorizer Email S******@e****.com
Narrative On 10/5/2023 at 15:05 cst, enterprise pipeline technician discovered a crude leak from a stem of a head gate valve at cedar pump station, 1 barrels of oil reached the ground. The leak was isolated and soil remediated. The packing gland was replaced and valve went to normal operations.

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