HL incident on 2023-11-03 — OK

Operator
Magellan Pipeline Company, Lp
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$5,000
Incident datetime
2023-11-03 00:00 UTC
Report number
Location
OK
Narrative
On october 4th, 2023 at 14:30 operations personnel at olathe station performing preventative maintenance activities discovered product leaking from the valve stem of mov2 on the paola - kansas city #5-12" pipeline. The line was shut down and kept open into the kansas city terminal to allow product to drain downstream. Clean-up activities were initiated. Further investigation found an o-ring had failed. To prevent a re-occurrence the 1950 installed valve was replaced by a valve with injectable packing. 5/2024 supplemental/final: part d
Detailed record list
Report Received Date
2023-11-03 00:00:00
Iyear
2023
Report Number
20230261
Supplemental Number
39737
Report Type
Supplemental Final
Operator Id
Name
Magellan Pipeline Company, Lp
Operator Street Address
100 West 5th Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
50
Recovered Bbls
50
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Notify Qualified Indiv Ind
Yes
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Olathe Station
Segment Name
Fac Id 543
Onshore State Abbreviation
Ks
Onshore Postal Code
66062
Onshore City Name
Olathe
Onshore County Name
Johnson
Designated Location
Milepost
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
In Underground Enclosed Space (E.g. Vault)
Depth Of Cover
36
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Mainline
Valve Mainline Type
Gate
Valve Manufacturer
Wkm
Installation Year
1950
Manufactured Year
1950
Material Involved
Material Other Than Carbon Steel
Material Details
O-Ring
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
7560
Est Cost Prop Damage
5000
Est Cost Emergency
10000
Est Cost Environmental
0
Est Cost Other
0
Prpty
22560
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
190.5
Mop Psig
1186
Mop Cfr Section
Internal Design Pressure �195.406(A)(1)
Maop Established Date
2023-03-20 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The event was not caused by or contributed to from the ops control controller, and the event was below detectable thresholds within the scada/ cpm systems.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
O-Ring
Eq Additional Other Ind
Yes
Eq Additional Other Details
Normal Wear
Preparer Name
C******* R******
Preparer Title
Strategic Data Engineer
Preparer Email
C***************@o****.com
Preparer Telephone
9185747065
Prepared Date
2024-07-01 00:00:00
Authorizer Name
T***** K***
Authorizer Telephone
9185747191
Authorizer Title
Supv. Integrity Mgmt And Regulatory Compliance
Authorizer Email
T**********@o****.com
Narrative
On october 4th, 2023 at 14:30 operations personnel at olathe station performing preventative maintenance activities discovered product leaking from the valve stem of mov2 on the paola - kansas city #5-12" pipeline. The line was shut down and kept open into the kansas city terminal to allow product to drain downstream. Clean-up activities were initiated. Further investigation found an o-ring had failed. To prevent a re-occurrence the 1950 installed valve was replaced by a valve with injectable packing. 5/2024 supplemental/final: part d
Report Received Date 2023-11-03 00:00:00
Iyear 2023
Report Number 20230261
Supplemental Number 39737
Report Type Supplemental Final
Operator Id 22610 PHMSA Enforcement
Name Magellan Pipeline Company, Lp
Operator Street Address 100 West 5th Street
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74103
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 38.882684 Google Maps OpenStreetMap
Location Longitude -94.744141 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 50
Recovered Bbls 50
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind Yes
Communication State Fed Ind Yes
Party Initiated Communication Operator
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Notify Qualified Indiv Ind Yes
Oil Spill Removal Org Ind No
Num Pub Evacuated 0
Pipe Fac Name Olathe Station
Segment Name Fac Id 543
Onshore State Abbreviation Ks
Onshore Postal Code 66062
Onshore City Name Olathe
Onshore County Name Johnson
Designated Location Milepost
Designated Name 0
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype In Underground Enclosed Space (E.g. Vault)
Depth Of Cover 36
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Mainline
Valve Mainline Type Gate
Valve Manufacturer Wkm
Installation Year 1950
Manufactured Year 1950
Material Involved Material Other Than Carbon Steel
Material Details O-Ring
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 7560
Est Cost Prop Damage 5000
Est Cost Emergency 10000
Est Cost Environmental 0
Est Cost Other 0
Prpty 22560
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 190.5
Mop Psig 1186
Mop Cfr Section Internal Design Pressure �195.406(A)(1) View CFR 49 §192
Maop Established Date 2023-03-20 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The event was not caused by or contributed to from the ops control controller, and the event was below detectable thresholds within the scada/ cpm systems.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind O-Ring
Eq Additional Other Ind Yes
Eq Additional Other Details Normal Wear
Preparer Name C******* R******
Preparer Title Strategic Data Engineer
Preparer Email C***************@o****.com
Preparer Telephone 9185747065
Prepared Date 2024-07-01 00:00:00
Authorizer Name T***** K***
Authorizer Telephone 9185747191
Authorizer Title Supv. Integrity Mgmt And Regulatory Compliance
Authorizer Email T**********@o****.com
Narrative On october 4th, 2023 at 14:30 operations personnel at olathe station performing preventative maintenance activities discovered product leaking from the valve stem of mov2 on the paola - kansas city #5-12" pipeline. The line was shut down and kept open into the kansas city terminal to allow product to drain downstream. Clean-up activities were initiated. Further investigation found an o-ring had failed. To prevent a re-occurrence the 1950 installed valve was replaced by a valve with injectable packing. 5/2024 supplemental/final: part d

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