Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2023-11-03 — OK
Operator
Magellan Pipeline Company, Lp
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$5,000
Incident datetime
2023-11-03 00:00 UTC
Report number
Location
OK
Narrative
On october 4th, 2023 at 14:30 operations personnel at olathe station performing preventative maintenance activities discovered product leaking from the valve stem of mov2 on the paola - kansas city #5-12" pipeline. The line was shut down and kept open into the kansas city terminal to allow product to drain downstream. Clean-up activities were initiated. Further investigation found an o-ring had failed. To prevent a re-occurrence the 1950 installed valve was replaced by a valve with injectable packing. 5/2024 supplemental/final: part d
Detailed record list
Report Received Date
2023-11-03 00:00:00
Iyear
2023
Report Number
20230261
Supplemental Number
39737
Report Type
Supplemental Final
Operator Id
22610
Name
Magellan Pipeline Company, Lp
Operator Street Address
100 West 5th Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
38.882684
Location Longitude
-94.744141
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
50
Recovered Bbls
50
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Notify Qualified Indiv Ind
Yes
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Olathe Station
Segment Name
Fac Id 543
Onshore State Abbreviation
Ks
Onshore Postal Code
66062
Onshore City Name
Olathe
Onshore County Name
Johnson
Designated Location
Milepost
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
In Underground Enclosed Space (E.g. Vault)
Depth Of Cover
36
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Mainline
Valve Mainline Type
Gate
Valve Manufacturer
Wkm
Installation Year
1950
Manufactured Year
1950
Material Involved
Material Other Than Carbon Steel
Material Details
O-Ring
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
7560
Est Cost Prop Damage
5000
Est Cost Emergency
10000
Est Cost Environmental
0
Est Cost Other
0
Prpty
22560
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
190.5
Mop Psig
1186
Mop Cfr Section
Internal Design Pressure �195.406(A)(1)
Maop Established Date
2023-03-20 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The event was not caused by or contributed to from the ops control controller, and the event was below detectable thresholds within the scada/ cpm systems.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
O-Ring
Eq Additional Other Ind
Yes
Eq Additional Other Details
Normal Wear
Preparer Name
C******* R******
Preparer Title
Strategic Data Engineer
Preparer Email
C***************@o****.com
Preparer Telephone
9185747065
Prepared Date
2024-07-01 00:00:00
Authorizer Name
T***** K***
Authorizer Telephone
9185747191
Authorizer Title
Supv. Integrity Mgmt And Regulatory Compliance
Authorizer Email
T**********@o****.com
Narrative
On october 4th, 2023 at 14:30 operations personnel at olathe station performing preventative maintenance activities discovered product leaking from the valve stem of mov2 on the paola - kansas city #5-12" pipeline. The line was shut down and kept open into the kansas city terminal to allow product to drain downstream. Clean-up activities were initiated. Further investigation found an o-ring had failed. To prevent a re-occurrence the 1950 installed valve was replaced by a valve with injectable packing. 5/2024 supplemental/final: part d
Report Received Date | 2023-11-03 00:00:00 |
---|---|
Iyear | 2023 |
Report Number | 20230261 |
Supplemental Number | 39737 |
Report Type | Supplemental Final |
Operator Id | 22610 PHMSA Enforcement |
Name | Magellan Pipeline Company, Lp |
Operator Street Address | 100 West 5th Street |
Operator City Name | Tulsa |
Operator State Abbreviation | OK |
Operator Postal Code | 74103 |
Time Zone | Central |
Daylight Savings Ind | Yes |
Location Latitude | 38.882684 Google Maps OpenStreetMap |
Location Longitude | -94.744141 Google Maps OpenStreetMap |
Commodity Released Type | Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions |
Commodity Subtype | Gasoline (Non-Ethanol) |
Unintentional Release Bbls | 50 |
Recovered Bbls | 50 |
Fatality Ind | No |
Fatal | 0 |
Injury Ind | No |
Injure | 0 |
Accident Identifier | Local Operating Personnel, Including Contractors |
Operator Type | Operator Employee |
System Part Involved | Onshore Pump/meter Station Equipment And Piping |
On Off Shore | Onshore |
Status When Identified | Normal Operation, Includes Pauses Between Batches And During Maintenance |
Shutdown Due Accident Ind | Yes |
Communication State Fed Ind | Yes |
Party Initiated Communication | Operator |
Nrc Rpt Num | Nrc Notification Not Required NRC Report How to search |
Ignite Ind | No |
Notify Qualified Indiv Ind | Yes |
Oil Spill Removal Org Ind | No |
Num Pub Evacuated | 0 |
Pipe Fac Name | Olathe Station |
Segment Name | Fac Id 543 |
Onshore State Abbreviation | Ks |
Onshore Postal Code | 66062 |
Onshore City Name | Olathe |
Onshore County Name | Johnson |
Designated Location | Milepost |
Designated Name | 0 |
Federal | No |
Location Type | Totally Contained On Operator-Controlled Property |
Incident Area Type | Underground |
Incident Area Subtype | In Underground Enclosed Space (E.g. Vault) |
Depth Of Cover | 36 |
Crossing | No |
Pipe Facility Type | Interstate |
Item Involved | Valve |
Valve Type | Mainline |
Valve Mainline Type | Gate |
Valve Manufacturer | Wkm |
Installation Year | 1950 |
Manufactured Year | 1950 |
Material Involved | Material Other Than Carbon Steel |
Material Details | O-Ring |
Release Type | Leak |
Leak Type | Seal Or Packing |
Wildlife Impact Ind | No |
Soil Contamination | No |
Long Term Assessment | No |
Remediation Ind | No |
Water Contam Ind | No |
Could Be Hca | Yes |
Commodity Reached Hca | Yes |
High Pop Ind | Yes |
High Pop Yes No | Yes |
Est Cost Oper Paid | 0 |
Est Cost Gas Released | 7560 |
Est Cost Prop Damage | 5000 |
Est Cost Emergency | 10000 |
Est Cost Environmental | 0 |
Est Cost Other | 0 |
Prpty | 22560 |
Num Persons Hosp Not Ovnght | 0 |
Num Injured Treated By Emt | 0 |
Num Resident Building Affctd | 0 |
Num Business Building Affctd | 0 |
Accident Psig | 190.5 |
Mop Psig | 1186 |
Mop Cfr Section | Internal Design Pressure �195.406(A)(1) View CFR 49 §192 |
Maop Established Date | 2023-03-20 00:00:00 |
Maop Reversal Flow Ind | No |
Accident Pressure | Pressure Did Not Exceed Mop |
Pressure Restriction Ind | No |
Pipeline Function | > 20% Smys Regulated Transmission |
Scada In Place Ind | Yes |
Scada Operating Ind | Yes |
Scada Functional Ind | Yes |
Scada Detection Ind | No |
Scada Conf Ind | No |
Cpm In Place Ind | Yes |
Cpm Operating Ind | Yes |
Cpm Functional Ind | Yes |
Cpm Detection Ind | No |
Cpm Conf Ind | No |
Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
Investigation Status Details | The event was not caused by or contributed to from the ops control controller, and the event was below detectable thresholds within the scada/ cpm systems. |
Employee Drug Test Ind | No |
Contractor Drug Test Ind | No |
Cause | Equipment Failure |
Cause Details | Non-Threaded Connection Failure |
Eq Failure Type | Non-Threaded Connection Failure |
Other Non Threaded Ind | O-Ring |
Eq Additional Other Ind | Yes |
Eq Additional Other Details | Normal Wear |
Preparer Name | C******* R****** |
Preparer Title | Strategic Data Engineer |
Preparer Email | C***************@o****.com |
Preparer Telephone | 9185747065 |
Prepared Date | 2024-07-01 00:00:00 |
Authorizer Name | T***** K*** |
Authorizer Telephone | 9185747191 |
Authorizer Title | Supv. Integrity Mgmt And Regulatory Compliance |
Authorizer Email | T**********@o****.com |
Narrative | On october 4th, 2023 at 14:30 operations personnel at olathe station performing preventative maintenance activities discovered product leaking from the valve stem of mov2 on the paola - kansas city #5-12" pipeline. The line was shut down and kept open into the kansas city terminal to allow product to drain downstream. Clean-up activities were initiated. Further investigation found an o-ring had failed. To prevent a re-occurrence the 1950 installed valve was replaced by a valve with injectable packing. 5/2024 supplemental/final: part d |
External Resources
PHMSA pipeline safety insights.
Product
Features
Company
All rights reserved. Copyright © by ClearPHMSA