HL incident on 2023-10-27 — TX

Operator
Harvest Midstream Company
Cause
Material Failure Of Pipe Or Weld
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$10,000
Incident datetime
2023-10-27 00:00 UTC
Report number
Location
TX
Narrative
The harvest operator arrived at three rivers station and upon arrival discovered oil near pump. It appeared to be from a spray mist blown across the pump and motor. The harvest operator notified the control room to shut down the pump and close the upstream and downstream valves. While depressurizing the pipe, a small crack started leaking from the weld-o-let. Corrective actions to minimize recoccurance- harvest will remove 1' flanged ball valves on mainline pumps at three rivers station and replace with blind flanges. This will remove the excess weight on the 1' piping. Harvest will complete an evaluation of 1' piping with similar design to p-5100 mainline pump at three rivers station using suitable ndt methods.
Detailed record list
Report Received Date
2023-10-27 00:00:00
Iyear
2023
Report Number
20230252
Supplemental Number
38785
Report Type
Supplemental Final
Operator Id
Name
Harvest Midstream Company
Operator Street Address
1111 Travis
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.76
Recovered Bbls
0.76
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Communication State Fed Ind
No
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Notify Qualified Indiv Ind
Yes
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Three Rivers Station
Segment Name
P 5100 Discharge
Onshore State Abbreviation
Tx
Onshore Postal Code
78071
Onshore City Name
Three Rivers
Onshore County Name
Live Oak
Designated Location
Milepost
Designated Name
Station
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Puddle Weld Ind
No
Pipe Diameter
1
Pipe Wall Thickness
0.159
Pipe Smys
35000
Pipe Specification
Astm A106 Grade B
Pipe Seam Type
Seamless
Pipe Manufacturer
Unknown
Pipe Coating Type
Paint
Coating Applied Ind
Unknown
Installation Year
2012
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Crack
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
72
Est Cost Prop Damage
10000
Est Cost Emergency
3000
Est Cost Environmental
0
Est Cost Other
0
Prpty
13072
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
1243
Mop Psig
1950
Mop Cfr Section
Subpart E Pressure Test �195.406(A)(3)
Maop Established Date
2012-07-06 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The leak was too small for the control room to detect.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Design-, Construction-, Installation-, Or Fabrication-Related
Metallurgical Ind
Yes
Failure Type
Design-, Construction-, Installation-, Or Fabrication-Related
Fatigue Vibr Related
Yes
Failure Subtype
Other
Fatigue Vibr Related Other
Fatigue Due To The Weight Of The Valve
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Pwf Design Ind
Yes
Preparer Name
T*** S* B****
Preparer Title
Regulatory Compliance Specialist
Preparer Email
T******@h***************.com
Preparer Telephone
7132892688
Prepared Date
2023-11-10 00:00:00
Local Contact Name
T*** B****
Local Contact Email
T******@h***************.com
Local Contact Telephone
7132892688
Authorizer Name
L***** F*****
Authorizer Telephone
8326038532
Authorizer Title
Director Of Integrity And Compliance
Authorizer Email
L************@h***************.com
Narrative
The harvest operator arrived at three rivers station and upon arrival discovered oil near pump. It appeared to be from a spray mist blown across the pump and motor. The harvest operator notified the control room to shut down the pump and close the upstream and downstream valves. While depressurizing the pipe, a small crack started leaking from the weld-o-let. Corrective actions to minimize recoccurance- harvest will remove 1' flanged ball valves on mainline pumps at three rivers station and replace with blind flanges. This will remove the excess weight on the 1' piping. Harvest will complete an evaluation of 1' piping with similar design to p-5100 mainline pump at three rivers station using suitable ndt methods.
Report Received Date 2023-10-27 00:00:00
Iyear 2023
Report Number 20230252
Supplemental Number 38785
Report Type Supplemental Final
Operator Id 30782 PHMSA Enforcement
Name Harvest Midstream Company
Operator Street Address 1111 Travis
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 28.408377 Google Maps OpenStreetMap
Location Longitude -98.211549 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.76
Recovered Bbls 0.76
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind Yes
Communication State Fed Ind No
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Notify Qualified Indiv Ind Yes
Oil Spill Removal Org Ind No
Num Pub Evacuated 0
Pipe Fac Name Three Rivers Station
Segment Name P 5100 Discharge
Onshore State Abbreviation Tx
Onshore Postal Code 78071
Onshore City Name Three Rivers
Onshore County Name Live Oak
Designated Location Milepost
Designated Name Station
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Puddle Weld Ind No
Pipe Diameter 1
Pipe Wall Thickness 0.159
Pipe Smys 35000
Pipe Specification Astm A106 Grade B
Pipe Seam Type Seamless
Pipe Manufacturer Unknown
Pipe Coating Type Paint
Coating Applied Ind Unknown
Installation Year 2012
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Crack
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 72
Est Cost Prop Damage 10000
Est Cost Emergency 3000
Est Cost Environmental 0
Est Cost Other 0
Prpty 13072
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 1243
Mop Psig 1950
Mop Cfr Section Subpart E Pressure Test �195.406(A)(3) View CFR 49 §192
Maop Established Date 2012-07-06 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The leak was too small for the control room to detect.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Material Failure Of Pipe Or Weld
Cause Details Design-, Construction-, Installation-, Or Fabrication-Related
Metallurgical Ind Yes
Failure Type Design-, Construction-, Installation-, Or Fabrication-Related
Fatigue Vibr Related Yes
Failure Subtype Other
Fatigue Vibr Related Other Fatigue Due To The Weight Of The Valve
Collected Data Ind No
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Pwf Design Ind Yes
Preparer Name T*** S* B****
Preparer Title Regulatory Compliance Specialist
Preparer Email T******@h***************.com
Preparer Telephone 7132892688
Prepared Date 2023-11-10 00:00:00
Local Contact Name T*** B****
Local Contact Email T******@h***************.com
Local Contact Telephone 7132892688
Authorizer Name L***** F*****
Authorizer Telephone 8326038532
Authorizer Title Director Of Integrity And Compliance
Authorizer Email L************@h***************.com
Narrative The harvest operator arrived at three rivers station and upon arrival discovered oil near pump. It appeared to be from a spray mist blown across the pump and motor. The harvest operator notified the control room to shut down the pump and close the upstream and downstream valves. While depressurizing the pipe, a small crack started leaking from the weld-o-let. Corrective actions to minimize recoccurance- harvest will remove 1' flanged ball valves on mainline pumps at three rivers station and replace with blind flanges. This will remove the excess weight on the 1' piping. Harvest will complete an evaluation of 1' piping with similar design to p-5100 mainline pump at three rivers station using suitable ndt methods.

All rights reserved. Copyright © by ClearPHMSA