Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2023-10-27 — TX
Operator
Harvest Midstream Company
Cause
Material Failure Of Pipe Or Weld
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$10,000
Incident datetime
2023-10-27 00:00 UTC
Report number
Location
TX
Narrative
The harvest operator arrived at three rivers station and upon arrival discovered oil near pump. It appeared to be from a spray mist blown across the pump and motor. The harvest operator notified the control room to shut down the pump and close the upstream and downstream valves. While depressurizing the pipe, a small crack started leaking from the weld-o-let. Corrective actions to minimize recoccurance- harvest will remove 1' flanged ball valves on mainline pumps at three rivers station and replace with blind flanges. This will remove the excess weight on the 1' piping. Harvest will complete an evaluation of 1' piping with similar design to p-5100 mainline pump at three rivers station using suitable ndt methods.
Detailed record list
Report Received Date
2023-10-27 00:00:00
Iyear
2023
Report Number
20230252
Supplemental Number
38785
Report Type
Supplemental Final
Operator Id
30782
Name
Harvest Midstream Company
Operator Street Address
1111 Travis
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
28.408377
Location Longitude
-98.211549
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.76
Recovered Bbls
0.76
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Communication State Fed Ind
No
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Notify Qualified Indiv Ind
Yes
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Three Rivers Station
Segment Name
P 5100 Discharge
Onshore State Abbreviation
Tx
Onshore Postal Code
78071
Onshore City Name
Three Rivers
Onshore County Name
Live Oak
Designated Location
Milepost
Designated Name
Station
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Puddle Weld Ind
No
Pipe Diameter
1
Pipe Wall Thickness
0.159
Pipe Smys
35000
Pipe Specification
Astm A106 Grade B
Pipe Seam Type
Seamless
Pipe Manufacturer
Unknown
Pipe Coating Type
Paint
Coating Applied Ind
Unknown
Installation Year
2012
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Crack
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
72
Est Cost Prop Damage
10000
Est Cost Emergency
3000
Est Cost Environmental
0
Est Cost Other
0
Prpty
13072
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
1243
Mop Psig
1950
Mop Cfr Section
Subpart E Pressure Test �195.406(A)(3)
Maop Established Date
2012-07-06 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The leak was too small for the control room to detect.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Design-, Construction-, Installation-, Or Fabrication-Related
Metallurgical Ind
Yes
Failure Type
Design-, Construction-, Installation-, Or Fabrication-Related
Fatigue Vibr Related
Yes
Failure Subtype
Other
Fatigue Vibr Related Other
Fatigue Due To The Weight Of The Valve
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Pwf Design Ind
Yes
Preparer Name
T*** S* B****
Preparer Title
Regulatory Compliance Specialist
Preparer Email
T******@h***************.com
Preparer Telephone
7132892688
Prepared Date
2023-11-10 00:00:00
Local Contact Name
T*** B****
Local Contact Email
T******@h***************.com
Local Contact Telephone
7132892688
Authorizer Name
L***** F*****
Authorizer Telephone
8326038532
Authorizer Title
Director Of Integrity And Compliance
Authorizer Email
L************@h***************.com
Narrative
The harvest operator arrived at three rivers station and upon arrival discovered oil near pump. It appeared to be from a spray mist blown across the pump and motor. The harvest operator notified the control room to shut down the pump and close the upstream and downstream valves. While depressurizing the pipe, a small crack started leaking from the weld-o-let. Corrective actions to minimize recoccurance- harvest will remove 1' flanged ball valves on mainline pumps at three rivers station and replace with blind flanges. This will remove the excess weight on the 1' piping. Harvest will complete an evaluation of 1' piping with similar design to p-5100 mainline pump at three rivers station using suitable ndt methods.
Report Received Date | 2023-10-27 00:00:00 |
---|---|
Iyear | 2023 |
Report Number | 20230252 |
Supplemental Number | 38785 |
Report Type | Supplemental Final |
Operator Id | 30782 PHMSA Enforcement |
Name | Harvest Midstream Company |
Operator Street Address | 1111 Travis |
Operator City Name | Houston |
Operator State Abbreviation | TX |
Operator Postal Code | 77002 |
Time Zone | Central |
Daylight Savings Ind | Yes |
Location Latitude | 28.408377 Google Maps OpenStreetMap |
Location Longitude | -98.211549 Google Maps OpenStreetMap |
Commodity Released Type | Crude Oil |
Unintentional Release Bbls | 0.76 |
Recovered Bbls | 0.76 |
Fatality Ind | No |
Fatal | 0 |
Injury Ind | No |
Injure | 0 |
Accident Identifier | Local Operating Personnel, Including Contractors |
Operator Type | Operator Employee |
System Part Involved | Onshore Pump/meter Station Equipment And Piping |
On Off Shore | Onshore |
Status When Identified | Normal Operation, Includes Pauses Between Batches And During Maintenance |
Shutdown Due Accident Ind | Yes |
Communication State Fed Ind | No |
Nrc Rpt Num | Nrc Notification Not Required NRC Report How to search |
Ignite Ind | No |
Notify Qualified Indiv Ind | Yes |
Oil Spill Removal Org Ind | No |
Num Pub Evacuated | 0 |
Pipe Fac Name | Three Rivers Station |
Segment Name | P 5100 Discharge |
Onshore State Abbreviation | Tx |
Onshore Postal Code | 78071 |
Onshore City Name | Three Rivers |
Onshore County Name | Live Oak |
Designated Location | Milepost |
Designated Name | Station |
Federal | No |
Location Type | Totally Contained On Operator-Controlled Property |
Incident Area Type | Aboveground |
Incident Area Subtype | Typical Aboveground Facility Piping Or Appurtenance |
Crossing | No |
Pipe Facility Type | Intrastate |
Item Involved | Pipe |
Pipe Type | Pipe Body |
Puddle Weld Ind | No |
Pipe Diameter | 1 |
Pipe Wall Thickness | 0.159 |
Pipe Smys | 35000 |
Pipe Specification | Astm A106 Grade B |
Pipe Seam Type | Seamless |
Pipe Manufacturer | Unknown |
Pipe Coating Type | Paint |
Coating Applied Ind | Unknown |
Installation Year | 2012 |
Manufactured Year | Unknown |
Material Involved | Carbon Steel |
Release Type | Leak |
Leak Type | Crack |
Wildlife Impact Ind | No |
Soil Contamination | Yes |
Long Term Assessment | No |
Remediation Ind | No |
Water Contam Ind | No |
Could Be Hca | No |
Commodity Reached Hca | No |
Est Cost Oper Paid | 0 |
Est Cost Gas Released | 72 |
Est Cost Prop Damage | 10000 |
Est Cost Emergency | 3000 |
Est Cost Environmental | 0 |
Est Cost Other | 0 |
Prpty | 13072 |
Num Persons Hosp Not Ovnght | 0 |
Num Injured Treated By Emt | 0 |
Num Resident Building Affctd | 0 |
Num Business Building Affctd | 0 |
Accident Psig | 1243 |
Mop Psig | 1950 |
Mop Cfr Section | Subpart E Pressure Test �195.406(A)(3) View CFR 49 §192 |
Maop Established Date | 2012-07-06 00:00:00 |
Maop Reversal Flow Ind | No |
Accident Pressure | Pressure Did Not Exceed Mop |
Pressure Restriction Ind | No |
Pipeline Function | > 20% Smys Regulated Transmission |
Scada In Place Ind | Yes |
Scada Operating Ind | Yes |
Scada Functional Ind | Yes |
Scada Detection Ind | No |
Scada Conf Ind | No |
Cpm In Place Ind | Yes |
Cpm Operating Ind | Yes |
Cpm Functional Ind | Yes |
Cpm Detection Ind | No |
Cpm Conf Ind | No |
Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
Investigation Status Details | The leak was too small for the control room to detect. |
Employee Drug Test Ind | No |
Contractor Drug Test Ind | No |
Cause | Material Failure Of Pipe Or Weld |
Cause Details | Design-, Construction-, Installation-, Or Fabrication-Related |
Metallurgical Ind | Yes |
Failure Type | Design-, Construction-, Installation-, Or Fabrication-Related |
Fatigue Vibr Related | Yes |
Failure Subtype | Other |
Fatigue Vibr Related Other | Fatigue Due To The Weight Of The Valve |
Collected Data Ind | No |
Has Hydrtst Conduc Before Ind | No |
Direct Asmnt Conducted | No |
Non Destructive Exam Ind | No |
Pwf Design Ind | Yes |
Preparer Name | T*** S* B**** |
Preparer Title | Regulatory Compliance Specialist |
Preparer Email | T******@h***************.com |
Preparer Telephone | 7132892688 |
Prepared Date | 2023-11-10 00:00:00 |
Local Contact Name | T*** B**** |
Local Contact Email | T******@h***************.com |
Local Contact Telephone | 7132892688 |
Authorizer Name | L***** F***** |
Authorizer Telephone | 8326038532 |
Authorizer Title | Director Of Integrity And Compliance |
Authorizer Email | L************@h***************.com |
Narrative | The harvest operator arrived at three rivers station and upon arrival discovered oil near pump. It appeared to be from a spray mist blown across the pump and motor. The harvest operator notified the control room to shut down the pump and close the upstream and downstream valves. While depressurizing the pipe, a small crack started leaking from the weld-o-let. Corrective actions to minimize recoccurance- harvest will remove 1' flanged ball valves on mainline pumps at three rivers station and replace with blind flanges. This will remove the excess weight on the 1' piping. Harvest will complete an evaluation of 1' piping with similar design to p-5100 mainline pump at three rivers station using suitable ndt methods. |
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