Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2023-10-23 — TX
Operator
Centurion Pipeline L.p.
Cause
Notification Issue
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$250,000
Incident datetime
2023-10-23 00:00 UTC
Report number
Location
TX
Narrative
On september 25, 2023, at 10:24am, centurion pipeline, l.P. (cpl) employee was notified by a third party excavator that a bulldozer had struck one of cpl's "slaughter to drumright" right-of-way (row). The employee's supervisor (qualified individual) and control center was notified. The pipeline system was previously shutdown due to reduced tank levels at cpl's cushing station at 10:17am. Cpl personnel arrived on-site at 10:44am and confirmed discovery on the "cushing west to el reno #1" at at 11:10am. Leak was located at approximately mp 61 in oklahoma city, oklahoma in oklahoma county. The company's osro was notified at 11:00am of the leak and arrived on-site at 11:50am. The national response center (nrc) was notified at 12:18am with incident report# 1380056. One thousand, six hundred and eighty-four (1,684) barrels was released and recovered. No injuries, fatalities or fires were associated with this incident. Remediation has been completed on-site. Repairs were completed and segment was returned to service. It was determined that the third party excavator had made the properly one-call ticket and the locate procedures were properly followed. In discussions with cpl's line locator and the excavator, it was determined that the third party excavator's original plans of excavation was too close to cpl's cushing west to el reno #1 to maintain clearance. It was determined that the excavator would revise the excavation plans to include additional cover and cross above cpl's pipeline instead of underneath. The third party excavator was informed that cpl's employee would need to be on-site for any excavation. The excavator did not make notification to cpl on the day of the incident and cpl was not on-site. On the day of the incident, it was determined that excavator's point of contact had not followed the modified plans nor was aware that there was an excavation crew on site. Supplemental report filed on november 21, 2023: updated part a5: location of accident's coordinates. Updated part a17 and included shutdown and restart times. Permanent repairs have been scheduled for late november 2023 and no further actions will be required.
Detailed record list
Report Received Date
2023-10-23 00:00:00
Iyear
2023
Report Number
20230245
Supplemental Number
38841
Report Type
Supplemental Final
Operator Id
31888
Name
Centurion Pipeline L.p.
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
35.657572
Location Longitude
-97.582892
Commodity Released Type
Crude Oil
Unintentional Release Bbls
1684
Recovered Bbls
1684
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Third Party That Caused The Accident
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Communication State Fed Ind
No
Nrc Rpt Num
1380056
Additional Nrc Report Numbers
1380263
Ignite Ind
No
Upstream Action Taken
Operational Control
Upstream Oprtnl Cntrl Detail
Block Valves Previously Closed Due To Routine Pause Of Product Flow.
Downstream Action Taken
Valve Closure
Downstream Valve Type Ind
Remotely Controlled
Notify Qualified Indiv Ind
Yes
Oil Spill Removal Org Ind
Yes
Osro Arrived On Site Dt
9/25/2023 11:50
Num Pub Evacuated
0
Pipe Fac Name
Slaughter To Drumright #1
Segment Name
Cushing West To El Reno #1
Onshore State Abbreviation
Ok
Onshore Postal Code
73012
Onshore City Name
Oklahoma City
Onshore County Name
Oklahoma
Designated Location
Milepost
Designated Name
Mp 61
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
30
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Puddle Weld Ind
No
Pipe Diameter
16
Pipe Wall Thickness
0.25
Pipe Smys
35000
Pipe Specification
Api 5l X-52
Pipe Seam Type
Erw - High Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
Other
Pipe Coating Details
Polywrap
Coating Applied Ind
Yes
Installation Year
1943
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Mechanical Puncture
Puncture Axial
3.5
Puncture Circum
2.5
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Est Cost Oper Paid
1000
Est Cost Gas Released
9000
Est Cost Prop Damage
250000
Est Cost Emergency
240000
Est Cost Environmental
600000
Est Cost Other
0
Prpty
1100000
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
70
Mop Psig
787
Mop Cfr Section
Internal Design Pressure �195.406(A)(1)
Maop Established Date
2016-10-25 00:00:00
Maop Reversal Flow Ind
Bi-Directional
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The pipeline segment was already shutdown and the leak was not detectable by scada.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
Yes
One Call System Ind
Yes
State Law Exempt Ind
No
Notify Cga Dirt
Yes
Private Row Ind
Yes
Private Subtype
Private Landowner
Joint Trench Ind
No
Cross Bore Ind
No
Depth Of Grade
18� � 36�
Excavator Type
Developer
Excavator Equipment
Bulldozer
Work Performed
Site Development
One Call Notified Ind
Yes
One Call Ticket Num
2.30925e+13
White Lined Ind
Yes
Locator Type
Facility Owner
Visible Marks
Yes
Service Interruption
Yes
Service Interruption Hours
14
Root Cause Category
Notification Issue
Root Cause Type
Excavator Failed To Maintain Clearance After Verifying Marks
Preparer Name
Y*** T*
Preparer Title
Senior Dot Compliance Specialist
Preparer Email
Y******@e*************.com
Preparer Telephone
713-989-7895
Prepared Date
2023-11-21 00:00:00
Authorizer Name
T***** D*****
Authorizer Telephone
713-989-7863
Authorizer Title
Dot Compliance Manager
Authorizer Email
T************@e*************.com
Narrative
On september 25, 2023, at 10:24am, centurion pipeline, l.P. (cpl) employee was notified by a third party excavator that a bulldozer had struck one of cpl's "slaughter to drumright" right-of-way (row). The employee's supervisor (qualified individual) and control center was notified. The pipeline system was previously shutdown due to reduced tank levels at cpl's cushing station at 10:17am. Cpl personnel arrived on-site at 10:44am and confirmed discovery on the "cushing west to el reno #1" at at 11:10am. Leak was located at approximately mp 61 in oklahoma city, oklahoma in oklahoma county. The company's osro was notified at 11:00am of the leak and arrived on-site at 11:50am. The national response center (nrc) was notified at 12:18am with incident report# 1380056. One thousand, six hundred and eighty-four (1,684) barrels was released and recovered. No injuries, fatalities or fires were associated with this incident. Remediation has been completed on-site. Repairs were completed and segment was returned to service. It was determined that the third party excavator had made the properly one-call ticket and the locate procedures were properly followed. In discussions with cpl's line locator and the excavator, it was determined that the third party excavator's original plans of excavation was too close to cpl's cushing west to el reno #1 to maintain clearance. It was determined that the excavator would revise the excavation plans to include additional cover and cross above cpl's pipeline instead of underneath. The third party excavator was informed that cpl's employee would need to be on-site for any excavation. The excavator did not make notification to cpl on the day of the incident and cpl was not on-site. On the day of the incident, it was determined that excavator's point of contact had not followed the modified plans nor was aware that there was an excavation crew on site. Supplemental report filed on november 21, 2023: updated part a5: location of accident's coordinates. Updated part a17 and included shutdown and restart times. Permanent repairs have been scheduled for late november 2023 and no further actions will be required.
Report Received Date | 2023-10-23 00:00:00 |
---|---|
Iyear | 2023 |
Report Number | 20230245 |
Supplemental Number | 38841 |
Report Type | Supplemental Final |
Operator Id | 31888 PHMSA Enforcement |
Name | Centurion Pipeline L.p. |
Operator Street Address | 1300 Main Street |
Operator City Name | Houston |
Operator State Abbreviation | TX |
Operator Postal Code | 77002 |
Time Zone | Central |
Daylight Savings Ind | Yes |
Location Latitude | 35.657572 Google Maps OpenStreetMap |
Location Longitude | -97.582892 Google Maps OpenStreetMap |
Commodity Released Type | Crude Oil |
Unintentional Release Bbls | 1684 |
Recovered Bbls | 1684 |
Fatality Ind | No |
Fatal | 0 |
Injury Ind | No |
Injure | 0 |
Accident Identifier | Notification From Third Party That Caused The Accident |
System Part Involved | Onshore Pipeline, Including Valve Sites |
On Off Shore | Onshore |
Status When Identified | Normal Operation, Includes Pauses Between Batches And During Maintenance |
Shutdown Due Accident Ind | Yes |
Communication State Fed Ind | No |
Nrc Rpt Num | 1380056 NRC Report How to search |
Additional Nrc Report Numbers | 1380263 |
Ignite Ind | No |
Upstream Action Taken | Operational Control |
Upstream Oprtnl Cntrl Detail | Block Valves Previously Closed Due To Routine Pause Of Product Flow. |
Downstream Action Taken | Valve Closure |
Downstream Valve Type Ind | Remotely Controlled |
Notify Qualified Indiv Ind | Yes |
Oil Spill Removal Org Ind | Yes |
Osro Arrived On Site Dt | 9/25/2023 11:50 |
Num Pub Evacuated | 0 |
Pipe Fac Name | Slaughter To Drumright #1 |
Segment Name | Cushing West To El Reno #1 |
Onshore State Abbreviation | Ok |
Onshore Postal Code | 73012 |
Onshore City Name | Oklahoma City |
Onshore County Name | Oklahoma |
Designated Location | Milepost |
Designated Name | Mp 61 |
Federal | No |
Location Type | Pipeline Right-Of-Way |
Incident Area Type | Underground |
Incident Area Subtype | Under Soil |
Depth Of Cover | 30 |
Crossing | No |
Pipe Facility Type | Interstate |
Item Involved | Pipe |
Pipe Type | Pipe Body |
Puddle Weld Ind | No |
Pipe Diameter | 16 |
Pipe Wall Thickness | 0.25 |
Pipe Smys | 35000 |
Pipe Specification | Api 5l X-52 |
Pipe Seam Type | Erw - High Frequency |
Pipe Manufacturer | Unknown |
Pipe Coating Type | Other |
Pipe Coating Details | Polywrap |
Coating Applied Ind | Yes |
Installation Year | 1943 |
Manufactured Year | Unknown |
Material Involved | Carbon Steel |
Release Type | Mechanical Puncture |
Puncture Axial | 3.5 |
Puncture Circum | 2.5 |
Wildlife Impact Ind | No |
Soil Contamination | Yes |
Long Term Assessment | No |
Remediation Ind | Yes |
Soil Remed Ind | Yes |
Water Contam Ind | No |
Could Be Hca | Yes |
Commodity Reached Hca | Yes |
Other Pop Ind | Yes |
Other Pop Yes No | Yes |
Est Cost Oper Paid | 1000 |
Est Cost Gas Released | 9000 |
Est Cost Prop Damage | 250000 |
Est Cost Emergency | 240000 |
Est Cost Environmental | 600000 |
Est Cost Other | 0 |
Prpty | 1100000 |
Num Persons Hosp Not Ovnght | 0 |
Num Injured Treated By Emt | 0 |
Num Resident Building Affctd | 0 |
Num Business Building Affctd | 0 |
Accident Psig | 70 |
Mop Psig | 787 |
Mop Cfr Section | Internal Design Pressure �195.406(A)(1) View CFR 49 §192 |
Maop Established Date | 2016-10-25 00:00:00 |
Maop Reversal Flow Ind | Bi-Directional |
Accident Pressure | Pressure Did Not Exceed Mop |
Pressure Restriction Ind | No |
Internal Inspection Ind | Yes |
Operation Complications Ind | No |
Pipeline Function | > 20% Smys Regulated Transmission |
Scada In Place Ind | Yes |
Scada Operating Ind | Yes |
Scada Functional Ind | Yes |
Scada Detection Ind | No |
Scada Conf Ind | No |
Cpm In Place Ind | Yes |
Cpm Operating Ind | Yes |
Cpm Functional Ind | Yes |
Cpm Detection Ind | No |
Cpm Conf Ind | No |
Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
Investigation Status Details | The pipeline segment was already shutdown and the leak was not detectable by scada. |
Employee Drug Test Ind | No |
Contractor Drug Test Ind | No |
Cause | Excavation Damage |
Cause Details | Excavation Damage By Third Party |
Ex Party Type | Excavation Damage By Third Party |
Prior Notification Ind | Yes |
One Call System Ind | Yes |
State Law Exempt Ind | No |
Notify Cga Dirt | Yes |
Private Row Ind | Yes |
Private Subtype | Private Landowner |
Joint Trench Ind | No |
Cross Bore Ind | No |
Depth Of Grade | 18� � 36� |
Excavator Type | Developer |
Excavator Equipment | Bulldozer |
Work Performed | Site Development |
One Call Notified Ind | Yes |
One Call Ticket Num | 2.30925e+13 |
White Lined Ind | Yes |
Locator Type | Facility Owner |
Visible Marks | Yes |
Service Interruption | Yes |
Service Interruption Hours | 14 |
Root Cause Category | Notification Issue |
Root Cause Type | Excavator Failed To Maintain Clearance After Verifying Marks |
Preparer Name | Y*** T* |
Preparer Title | Senior Dot Compliance Specialist |
Preparer Email | Y******@e*************.com |
Preparer Telephone | 713-989-7895 |
Prepared Date | 2023-11-21 00:00:00 |
Authorizer Name | T***** D***** |
Authorizer Telephone | 713-989-7863 |
Authorizer Title | Dot Compliance Manager |
Authorizer Email | T************@e*************.com |
Narrative | On september 25, 2023, at 10:24am, centurion pipeline, l.P. (cpl) employee was notified by a third party excavator that a bulldozer had struck one of cpl's "slaughter to drumright" right-of-way (row). The employee's supervisor (qualified individual) and control center was notified. The pipeline system was previously shutdown due to reduced tank levels at cpl's cushing station at 10:17am. Cpl personnel arrived on-site at 10:44am and confirmed discovery on the "cushing west to el reno #1" at at 11:10am. Leak was located at approximately mp 61 in oklahoma city, oklahoma in oklahoma county. The company's osro was notified at 11:00am of the leak and arrived on-site at 11:50am. The national response center (nrc) was notified at 12:18am with incident report# 1380056. One thousand, six hundred and eighty-four (1,684) barrels was released and recovered. No injuries, fatalities or fires were associated with this incident. Remediation has been completed on-site. Repairs were completed and segment was returned to service. It was determined that the third party excavator had made the properly one-call ticket and the locate procedures were properly followed. In discussions with cpl's line locator and the excavator, it was determined that the third party excavator's original plans of excavation was too close to cpl's cushing west to el reno #1 to maintain clearance. It was determined that the excavator would revise the excavation plans to include additional cover and cross above cpl's pipeline instead of underneath. The third party excavator was informed that cpl's employee would need to be on-site for any excavation. The excavator did not make notification to cpl on the day of the incident and cpl was not on-site. On the day of the incident, it was determined that excavator's point of contact had not followed the modified plans nor was aware that there was an excavation crew on site. Supplemental report filed on november 21, 2023: updated part a5: location of accident's coordinates. Updated part a17 and included shutdown and restart times. Permanent repairs have been scheduled for late november 2023 and no further actions will be required. |
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