Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2023-10-13 — TX
Operator
Capturepoint Llc
Cause
Equipment Failure
Commodity
Co2 (Carbon Dioxide)
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$20
Incident datetime
2023-10-13 00:00 UTC
Report number
Location
TX
Narrative
Friday, september 15 at 2:00am ' mike smith received a call from coffeyville resources (cvr) plant control room with a report that the capturepoint launcher barrel was leaking CO2 based on observed cloud and CO2 blowing from the end of the barrel. Cvr had peco (contractor) completing work in a fabrication area approximately 50 yards south of capturepoint fenced area where barrel is located. 2:15am - mike smith arrived at the plant and saw the leak on launcher barrel door o-ring seal appeared to have blown out. 2:20am - 2:30am ' mike smith assessed what was happening. No one was in or around the immediate area. Took pictures and video. The wind was blowing ese 3mph, and it was 62 degrees. 2:40am-3:00am ' mike smith removed lock from kicker valve that was found in closed position. Removed lock from isolation valve that was found open. I closed the isolation valve and opened 3 - vent valves to relieve pressure from launcher barrel. 3:11am - mike smith sent 5 photos to mike godfrey, pipeline supervisor, via text message. 4:43am ' mike smith sent email to christina harvick, director of pipelines and facilities, and to mike godfrey, pipeline supervisor, with the details. 4:45am - 5am - the launcher barrel door was still leaking but wasn't blowing as hard as when initially discovered. The barrel continued to bleed off until about 6:00am when the pressure gauge read (0) zero. 6:52am - mike smith called mike godfrey, pipeline supervisor, and reported to him what was found and how valves were left. Mike godfrey informed mike smith that he would head that direction and repair. Mike smith stayed on site until the other plant operator arrived for his shift and left the plant at approximately 7am. The barrel yale head enclosure viton o-ring was found damaged due to misalignment.
Detailed record list
Report Received Date
2023-10-13 00:00:00
Iyear
2023
Report Number
20230240
Supplemental Number
38839
Report Type
Supplemental Final
Operator Id
39754
Name
Capturepoint Llc
Operator Street Address
1101 Central Expressway, South Suite 150
Operator City Name
Allen
Operator State Abbreviation
TX
Operator Postal Code
75013
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
37.04438
Location Longitude
-95.6076
Commodity Released Type
Co2 (Carbon Dioxide)
Unintentional Release Bbls
256
Intentional Release Bbls
1.28
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
No
Shutdown Explain
Launcher Barrel Isolated And Valves Were Used For A Controlled Blow Down
Communication State Fed Ind
No
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Upstream Action Taken
Valve Closure
Upstream Valve Type Ind
Manual
Downstream Action Taken
Valve Closure
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Coffeyville Pipeline
Onshore State Abbreviation
Ks
Onshore Postal Code
67337
Onshore City Name
Coffeyville
Onshore County Name
Montgomery
Designated Location
Survey Station No.
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Scraper/pig Trap
Installation Year
2013
Manufactured Year
2013
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
200
Est Cost Prop Damage
20
Est Cost Emergency
5500
Est Cost Environmental
0
Est Cost Other
0
Prpty
5720
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
1527
Mop Psig
2175
Mop Cfr Section
Subpart E Pressure Test �195.406(A)(3)
Maop Established Date
2013-03-31 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
15
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The leak was detected on a launching barrel not on the physical pipeline. The barrel is equipped with a manual pressure gauge.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
O-Ring
Ief Addl Misalignment Ind
Yes
Preparer Name
S******* D********
Preparer Title
Compliance Program Manager
Preparer Email
S*****************@e*********.com
Preparer Telephone
8323865484
Prepared Date
2023-11-20 00:00:00
Local Contact Name
C******** H******
Local Contact Email
C*******@c**************.com
Local Contact Telephone
469-207-9111
Authorizer Name
R***** S*********
Authorizer Telephone
2816688478
Authorizer Title
Senior Vice President Of Operartions
Authorizer Email
B***@c**************.com
Narrative
Friday, september 15 at 2:00am ' mike smith received a call from coffeyville resources (cvr) plant control room with a report that the capturepoint launcher barrel was leaking CO2 based on observed cloud and CO2 blowing from the end of the barrel. Cvr had peco (contractor) completing work in a fabrication area approximately 50 yards south of capturepoint fenced area where barrel is located. 2:15am - mike smith arrived at the plant and saw the leak on launcher barrel door o-ring seal appeared to have blown out. 2:20am - 2:30am ' mike smith assessed what was happening. No one was in or around the immediate area. Took pictures and video. The wind was blowing ese 3mph, and it was 62 degrees. 2:40am-3:00am ' mike smith removed lock from kicker valve that was found in closed position. Removed lock from isolation valve that was found open. I closed the isolation valve and opened 3 - vent valves to relieve pressure from launcher barrel. 3:11am - mike smith sent 5 photos to mike godfrey, pipeline supervisor, via text message. 4:43am ' mike smith sent email to christina harvick, director of pipelines and facilities, and to mike godfrey, pipeline supervisor, with the details. 4:45am - 5am - the launcher barrel door was still leaking but wasn't blowing as hard as when initially discovered. The barrel continued to bleed off until about 6:00am when the pressure gauge read (0) zero. 6:52am - mike smith called mike godfrey, pipeline supervisor, and reported to him what was found and how valves were left. Mike godfrey informed mike smith that he would head that direction and repair. Mike smith stayed on site until the other plant operator arrived for his shift and left the plant at approximately 7am. The barrel yale head enclosure viton o-ring was found damaged due to misalignment.
Report Received Date | 2023-10-13 00:00:00 |
---|---|
Iyear | 2023 |
Report Number | 20230240 |
Supplemental Number | 38839 |
Report Type | Supplemental Final |
Operator Id | 39754 PHMSA Enforcement |
Name | Capturepoint Llc |
Operator Street Address | 1101 Central Expressway, South Suite 150 |
Operator City Name | Allen |
Operator State Abbreviation | TX |
Operator Postal Code | 75013 |
Time Zone | Central |
Daylight Savings Ind | Yes |
Location Latitude | 37.04438 Google Maps OpenStreetMap |
Location Longitude | -95.6076 Google Maps OpenStreetMap |
Commodity Released Type | Co2 (Carbon Dioxide) |
Unintentional Release Bbls | 256 |
Intentional Release Bbls | 1.28 |
Recovered Bbls | 0 |
Fatality Ind | No |
Fatal | 0 |
Injury Ind | No |
Injure | 0 |
Accident Identifier | Notification From Public |
System Part Involved | Onshore Pipeline, Including Valve Sites |
On Off Shore | Onshore |
Status When Identified | Normal Operation, Includes Pauses Between Batches And During Maintenance |
Shutdown Due Accident Ind | No |
Shutdown Explain | Launcher Barrel Isolated And Valves Were Used For A Controlled Blow Down |
Communication State Fed Ind | No |
Nrc Rpt Num | Nrc Notification Not Required NRC Report How to search |
Ignite Ind | No |
Upstream Action Taken | Valve Closure |
Upstream Valve Type Ind | Manual |
Downstream Action Taken | Valve Closure |
Downstream Valve Type Ind | Manual |
Num Pub Evacuated | 0 |
Pipe Fac Name | Coffeyville Pipeline |
Onshore State Abbreviation | Ks |
Onshore Postal Code | 67337 |
Onshore City Name | Coffeyville |
Onshore County Name | Montgomery |
Designated Location | Survey Station No. |
Designated Name | 0 |
Federal | No |
Location Type | Totally Contained On Operator-Controlled Property |
Incident Area Type | Aboveground |
Incident Area Subtype | Typical Aboveground Facility Piping Or Appurtenance |
Crossing | No |
Pipe Facility Type | Interstate |
Item Involved | Scraper/pig Trap |
Installation Year | 2013 |
Manufactured Year | 2013 |
Material Involved | Carbon Steel |
Release Type | Leak |
Leak Type | Seal Or Packing |
Wildlife Impact Ind | No |
Soil Contamination | No |
Long Term Assessment | No |
Remediation Ind | No |
Water Contam Ind | No |
Could Be Hca | Yes |
Commodity Reached Hca | Yes |
Other Pop Ind | Yes |
Other Pop Yes No | Yes |
Est Cost Oper Paid | 0 |
Est Cost Gas Released | 200 |
Est Cost Prop Damage | 20 |
Est Cost Emergency | 5500 |
Est Cost Environmental | 0 |
Est Cost Other | 0 |
Prpty | 5720 |
Num Persons Hosp Not Ovnght | 0 |
Num Injured Treated By Emt | 0 |
Num Resident Building Affctd | 0 |
Num Business Building Affctd | 0 |
Accident Psig | 1527 |
Mop Psig | 2175 |
Mop Cfr Section | Subpart E Pressure Test �195.406(A)(3) View CFR 49 §192 |
Maop Established Date | 2013-03-31 00:00:00 |
Maop Reversal Flow Ind | No |
Accident Pressure | Pressure Did Not Exceed Mop |
Pressure Restriction Ind | No |
Length Segment Isolated | 15 |
Internal Inspection Ind | Yes |
Operation Complications Ind | No |
Pipeline Function | > 20% Smys Regulated Transmission |
Scada In Place Ind | Yes |
Scada Operating Ind | Yes |
Scada Functional Ind | Yes |
Scada Detection Ind | No |
Scada Conf Ind | No |
Cpm In Place Ind | No |
Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
Investigation Status Details | The leak was detected on a launching barrel not on the physical pipeline. The barrel is equipped with a manual pressure gauge. |
Employee Drug Test Ind | No |
Contractor Drug Test Ind | No |
Cause | Equipment Failure |
Cause Details | Non-Threaded Connection Failure |
Eq Failure Type | Non-Threaded Connection Failure |
Other Non Threaded Ind | O-Ring |
Ief Addl Misalignment Ind | Yes |
Preparer Name | S******* D******** |
Preparer Title | Compliance Program Manager |
Preparer Email | S*****************@e*********.com |
Preparer Telephone | 8323865484 |
Prepared Date | 2023-11-20 00:00:00 |
Local Contact Name | C******** H****** |
Local Contact Email | C*******@c**************.com |
Local Contact Telephone | 469-207-9111 |
Authorizer Name | R***** S********* |
Authorizer Telephone | 2816688478 |
Authorizer Title | Senior Vice President Of Operartions |
Authorizer Email | B***@c**************.com |
Narrative | Friday, september 15 at 2:00am ' mike smith received a call from coffeyville resources (cvr) plant control room with a report that the capturepoint launcher barrel was leaking CO2 based on observed cloud and CO2 blowing from the end of the barrel. Cvr had peco (contractor) completing work in a fabrication area approximately 50 yards south of capturepoint fenced area where barrel is located. 2:15am - mike smith arrived at the plant and saw the leak on launcher barrel door o-ring seal appeared to have blown out. 2:20am - 2:30am ' mike smith assessed what was happening. No one was in or around the immediate area. Took pictures and video. The wind was blowing ese 3mph, and it was 62 degrees. 2:40am-3:00am ' mike smith removed lock from kicker valve that was found in closed position. Removed lock from isolation valve that was found open. I closed the isolation valve and opened 3 - vent valves to relieve pressure from launcher barrel. 3:11am - mike smith sent 5 photos to mike godfrey, pipeline supervisor, via text message. 4:43am ' mike smith sent email to christina harvick, director of pipelines and facilities, and to mike godfrey, pipeline supervisor, with the details. 4:45am - 5am - the launcher barrel door was still leaking but wasn't blowing as hard as when initially discovered. The barrel continued to bleed off until about 6:00am when the pressure gauge read (0) zero. 6:52am - mike smith called mike godfrey, pipeline supervisor, and reported to him what was found and how valves were left. Mike godfrey informed mike smith that he would head that direction and repair. Mike smith stayed on site until the other plant operator arrived for his shift and left the plant at approximately 7am. The barrel yale head enclosure viton o-ring was found damaged due to misalignment. |
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