HL incident on 2023-09-29 — OK

Operator
Magellan Pipeline Company, Lp
Cause
Material Failure Of Pipe Or Weld
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2023-09-29 00:00 UTC
Report number
Location
OK
Narrative
On september 1st, 2023, at 09:29 a pilot conducting routine air patrol observed dead vegetation in the right-of-way near milepost 181.73 of the #6-12" bettendorf jct - amboy pipeline. An incident investigation was immediately initiated. Operation control confirmed the pipeline was already shutdown and closed the upstream and downstream rovs, isolating the affected segment. Local operation personnel were dispatched to the site who arrived at 10:00 and confirmed signs of distressed vegetation potentially indicative of a release. The nearest up and downstream manual valves were closed 11:45 and 11:30, respectively. Excavation confirmed evidence of a low-rate release that was repaired with a type b sleeve at approximately 18:30 on september 1st, 2023. The affected pipe joint was cut out and replaced on september 8th. The anomaly was sent for metallurgical analysis. The approved restart plan was executed successfully on the 13th and the line was approved to return to normal operations. The line resumed normal operation at 08:00 on september 14th, 2023. The metallurgical report states "the leak was caused by a through-wall flaw located at the fusion line of the erw seam. The leak feature was caused by a localized area of the erw seam that did not have sufficient heat and/or pressure to extrude the oxides that formed along the coil edges prior to seam formation, resulting in an incomplete fusion or black spot defect. Both flaws are pipe mill defects." additionally, per the report "it is most likely that the oxides broke down over time, creating the leak path". Supplemental/final (9/2024): parts a, g and h
Detailed record list
Report Received Date
2023-09-29 00:00:00
Iyear
2023
Report Number
20230231
Supplemental Number
39972
Report Type
Supplemental Final
Operator Id
Name
Magellan Pipeline Company, Lp
Operator Street Address
100 West 5th Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
144
Recovered Bbls
125
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Air Patrol
Operator Type
Contractor Working For The Operator
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
No
Shutdown Explain
Line Was Already Shutdown
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Nrc Rpt Num
Additional Nrc Report Numbers
1378059
Ignite Ind
No
Upstream Action Taken
Valve Closure
Upstream Valve Type Ind
Remotely Controlled
Downstream Action Taken
Valve Closure
Downstream Valve Type Ind
Remotely Controlled
Notify Qualified Indiv Ind
Yes
Oil Spill Removal Org Ind
Yes
Osro Arrived On Site Dt
9/1/2023 14:00
Num Pub Evacuated
0
Pipe Fac Name
#6-12" Bettendorf Jct - Amboy
Segment Name
Line Id 6155
Onshore State Abbreviation
Il
Onshore Postal Code
61250
Onshore City Name
Erie
Onshore County Name
Whiteside
Designated Location
Milepost
Designated Name
181.73
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
36
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Seam
Pipe Diameter
12.75
Pipe Wall Thickness
0.203
Pipe Smys
42000
Pipe Specification
X42
Pipe Seam Type
Erw - Low Frequency
Pipe Manufacturer
Jones And Laughlin
Pipe Coating Type
Coal Tar
Coating Applied Ind
Yes
Installation Year
1958
Manufactured Year
1958
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
Yes
Remediation Ind
Yes
Groundwater Remed Ind
Yes
Water Contam Ind
Yes
Groundwater Contam Ind
Yes
Amount Released
0.1
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
35000
Est Cost Gas Released
600
Est Cost Prop Damage
0
Est Cost Emergency
50000
Est Cost Environmental
975500
Est Cost Other
0
Prpty
1061100
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
383
Mop Psig
770
Mop Cfr Section
Internal Design Pressure �195.406(A)(1)
Maop Established Date
2020-08-06 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
110880
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The pipeline was idle at the time of discovery.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Metallurgical Ind
Yes
Failure Type
Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Other Factor
Yes
Other Factor Details
Oxides Breaking Down Over Time
Pwf Additional Other Ind
Yes
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Cir Trn Wave Mgn Flx Lkg Ind
Yes
Geometry Deformation Ind
Yes
Other Tool Tech Ind
Yes
Axial Recent Year
2020
Axial Rcnt Propul Method
Free Swimming
Axial Rcnt Attuned Detect
Metal Loss
Axial Rcnt Atnd Dtct Metal
High Resolution
Axial Previous Year
2010
Axial Prev Propul Method
Free Swimming
Axial Prev Attuned Detect
Metal Loss
Axial Prev Atnd Dtct Metal
High Resolution
Circ Wave Recent Year
2015
Circ Wv Rcnt Propul Method
Free Swimming
Circ Wv Rcnt Resolution
High Resolution
Geometry Recent Year
2020
Geometry Rcnt Propul Method
Free Swimming
Geometry Rcnt Resolution
High Resolution
Geometrt Rcnt Measur Cups
No Cups
Geometry Previous Year
2015
Geometry Prev Propul Method
Free Swimming
Geometry Prev Resolution
High Resolution
Geometrt Prev Measur Cups
No Cups
Other Tool
Helical Mfl
Other Recent Year
2020
Other Rcnt Propul Method
Free Swimming
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
1989
Hydrtst Most Rcnt Pressure
1212
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
C******* R******
Preparer Title
Strategic Data Engineer
Preparer Email
C***************@m*********.com
Preparer Telephone
9185747065
Prepared Date
2024-08-02 00:00:00
Authorizer Name
T***** K***
Authorizer Telephone
9185747191
Authorizer Title
Supv. Integrity Mgmt And Regulatory Compliance
Authorizer Email
T**********@m*********.com
Narrative
On september 1st, 2023, at 09:29 a pilot conducting routine air patrol observed dead vegetation in the right-of-way near milepost 181.73 of the #6-12" bettendorf jct - amboy pipeline. An incident investigation was immediately initiated. Operation control confirmed the pipeline was already shutdown and closed the upstream and downstream rovs, isolating the affected segment. Local operation personnel were dispatched to the site who arrived at 10:00 and confirmed signs of distressed vegetation potentially indicative of a release. The nearest up and downstream manual valves were closed 11:45 and 11:30, respectively. Excavation confirmed evidence of a low-rate release that was repaired with a type b sleeve at approximately 18:30 on september 1st, 2023. The affected pipe joint was cut out and replaced on september 8th. The anomaly was sent for metallurgical analysis. The approved restart plan was executed successfully on the 13th and the line was approved to return to normal operations. The line resumed normal operation at 08:00 on september 14th, 2023. The metallurgical report states "the leak was caused by a through-wall flaw located at the fusion line of the erw seam. The leak feature was caused by a localized area of the erw seam that did not have sufficient heat and/or pressure to extrude the oxides that formed along the coil edges prior to seam formation, resulting in an incomplete fusion or black spot defect. Both flaws are pipe mill defects." additionally, per the report "it is most likely that the oxides broke down over time, creating the leak path". Supplemental/final (9/2024): parts a, g and h
Report Received Date 2023-09-29 00:00:00
Iyear 2023
Report Number 20230231
Supplemental Number 39972
Report Type Supplemental Final
Operator Id 22610 PHMSA Enforcement
Name Magellan Pipeline Company, Lp
Operator Street Address 100 West 5th Street
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74103
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 41.689546 Google Maps OpenStreetMap
Location Longitude -90.138655 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 144
Recovered Bbls 125
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Air Patrol
Operator Type Contractor Working For The Operator
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind No
Shutdown Explain Line Was Already Shutdown
Communication State Fed Ind Yes
Party Initiated Communication Operator
Nrc Rpt Num 1377938 NRC Report How to search
Additional Nrc Report Numbers 1378059
Ignite Ind No
Upstream Action Taken Valve Closure
Upstream Valve Type Ind Remotely Controlled
Downstream Action Taken Valve Closure
Downstream Valve Type Ind Remotely Controlled
Notify Qualified Indiv Ind Yes
Oil Spill Removal Org Ind Yes
Osro Arrived On Site Dt 9/1/2023 14:00
Num Pub Evacuated 0
Pipe Fac Name #6-12" Bettendorf Jct - Amboy
Segment Name Line Id 6155
Onshore State Abbreviation Il
Onshore Postal Code 61250
Onshore City Name Erie
Onshore County Name Whiteside
Designated Location Milepost
Designated Name 181.73
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 36
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Seam
Pipe Diameter 12.75
Pipe Wall Thickness 0.203
Pipe Smys 42000
Pipe Specification X42
Pipe Seam Type Erw - Low Frequency
Pipe Manufacturer Jones And Laughlin
Pipe Coating Type Coal Tar
Coating Applied Ind Yes
Installation Year 1958
Manufactured Year 1958
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment Yes
Remediation Ind Yes
Groundwater Remed Ind Yes
Water Contam Ind Yes
Groundwater Contam Ind Yes
Amount Released 0.1
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 35000
Est Cost Gas Released 600
Est Cost Prop Damage 0
Est Cost Emergency 50000
Est Cost Environmental 975500
Est Cost Other 0
Prpty 1061100
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 383
Mop Psig 770
Mop Cfr Section Internal Design Pressure �195.406(A)(1) View CFR 49 §192
Maop Established Date 2020-08-06 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 110880
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The pipeline was idle at the time of discovery.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Material Failure Of Pipe Or Weld
Cause Details Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Metallurgical Ind Yes
Failure Type Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Other Factor Yes
Other Factor Details Oxides Breaking Down Over Time
Pwf Additional Other Ind Yes
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Cir Trn Wave Mgn Flx Lkg Ind Yes
Geometry Deformation Ind Yes
Other Tool Tech Ind Yes
Axial Recent Year 2020
Axial Rcnt Propul Method Free Swimming
Axial Rcnt Attuned Detect Metal Loss
Axial Rcnt Atnd Dtct Metal High Resolution
Axial Previous Year 2010
Axial Prev Propul Method Free Swimming
Axial Prev Attuned Detect Metal Loss
Axial Prev Atnd Dtct Metal High Resolution
Circ Wave Recent Year 2015
Circ Wv Rcnt Propul Method Free Swimming
Circ Wv Rcnt Resolution High Resolution
Geometry Recent Year 2020
Geometry Rcnt Propul Method Free Swimming
Geometry Rcnt Resolution High Resolution
Geometrt Rcnt Measur Cups No Cups
Geometry Previous Year 2015
Geometry Prev Propul Method Free Swimming
Geometry Prev Resolution High Resolution
Geometrt Prev Measur Cups No Cups
Other Tool Helical Mfl
Other Recent Year 2020
Other Rcnt Propul Method Free Swimming
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 1989
Hydrtst Most Rcnt Pressure 1212
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name C******* R******
Preparer Title Strategic Data Engineer
Preparer Email C***************@m*********.com
Preparer Telephone 9185747065
Prepared Date 2024-08-02 00:00:00
Authorizer Name T***** K***
Authorizer Telephone 9185747191
Authorizer Title Supv. Integrity Mgmt And Regulatory Compliance
Authorizer Email T**********@m*********.com
Narrative On september 1st, 2023, at 09:29 a pilot conducting routine air patrol observed dead vegetation in the right-of-way near milepost 181.73 of the #6-12" bettendorf jct - amboy pipeline. An incident investigation was immediately initiated. Operation control confirmed the pipeline was already shutdown and closed the upstream and downstream rovs, isolating the affected segment. Local operation personnel were dispatched to the site who arrived at 10:00 and confirmed signs of distressed vegetation potentially indicative of a release. The nearest up and downstream manual valves were closed 11:45 and 11:30, respectively. Excavation confirmed evidence of a low-rate release that was repaired with a type b sleeve at approximately 18:30 on september 1st, 2023. The affected pipe joint was cut out and replaced on september 8th. The anomaly was sent for metallurgical analysis. The approved restart plan was executed successfully on the 13th and the line was approved to return to normal operations. The line resumed normal operation at 08:00 on september 14th, 2023. The metallurgical report states "the leak was caused by a through-wall flaw located at the fusion line of the erw seam. The leak feature was caused by a localized area of the erw seam that did not have sufficient heat and/or pressure to extrude the oxides that formed along the coil edges prior to seam formation, resulting in an incomplete fusion or black spot defect. Both flaws are pipe mill defects." additionally, per the report "it is most likely that the oxides broke down over time, creating the leak path". Supplemental/final (9/2024): parts a, g and h

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