HL incident on 2023-09-18 — TX

Operator
Exxonmobil Pipeline Company Llc
Cause
Material Failure Of Pipe Or Weld
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$100,000
Incident datetime
2023-09-18 00:00 UTC
Report number
Location
TX
Narrative
Background: the working foreman was at tank #909 dike area to inspect a prv. He observed discoloration of stones and wetness around the tank chime. He opened the double bottom telltale valve and found product present. He notified the supervisor and absorbent booms were deployed around the tank chime and it was confirmed that the tank dike drain valve was closed. Approximately 5 gallons of trans mix (gasoline & diesel) was released to soil inside the tank dike. Immediate corrective actions: tank #909 was isolated, and two layers of absorbent boom were placed around the tank. A project was executed to de-inventory, clean and gas free tank #909 to allow for an internal API 653 inspection. Preventing re-occurrence: an API 653 internal inspection was completed, and all necessary repairs were made to the tank bottom per API 650 standards.
Detailed record list
Report Received Date
2023-09-18 00:00:00
Iyear
2023
Report Number
20230218
Supplemental Number
38560
Report Type
Original Final
Operator Id
Name
Exxonmobil Pipeline Company Llc
Operator Street Address
22777 Springwoods Village Parkway E2.2b-Emp
Operator City Name
Spring
Operator State Abbreviation
TX
Operator Postal Code
77389
Time Zone
Central
Daylight Savings Ind
No
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Mixture Of Refined Products (Transmix Or Other Mixture)
Unintentional Release Bbls
0.12
Recovered Bbls
0.12
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
System Part Involved
Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
No
Shutdown Explain
Pipeline Was Not Flowing At The Time Of Incident
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Nrc Rpt Num
Additional Nrc Report Numbers
1377175
Ignite Ind
No
Notify Qualified Indiv Ind
Yes
Oil Spill Removal Org Ind
Yes
Osro Arrived On Site Dt
8/22/2023 15:35
Num Pub Evacuated
0
Pipe Fac Name
Lockport Terminal
Segment Name
Tank #909
Onshore State Abbreviation
Il
Onshore Postal Code
60441
Onshore City Name
Lockport
Onshore County Name
Will County
Designated Location
Milepost
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tank/vessel
Tank Vessel Subtype
Double Bottom System
Tank Type
Atmospheric
Safe Fill Level
24.5
Safe Fill Level Exceeded Ind
No
Api Std Out Of Service Year
2011
Api Std In Service Year
2021
Installation Year
1971
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Crack
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
20
Est Cost Prop Damage
100000
Est Cost Emergency
10000
Est Cost Environmental
50000
Est Cost Other
0
Prpty
160020
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
5
Pressure Restriction Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Small seep from the double bottom and there was no indication of a leak in the control room.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Design-, Construction-, Installation-, Or Fabrication-Related
Field Exam Ind
Yes
Other Analysis Ind
Yes
Other Analysis Details
Tank Floor Mfl Scan As Part Of Api 653
Failure Type
Design-, Construction-, Installation-, Or Fabrication-Related
Other Factor
Yes
Other Factor Details
Weld Spacing
Additional Crack Ind
Yes
Pwf Fabrication Ind
Yes
Preparer Name
R***** P S**********
Preparer Title
Dot Pipeline Safety Advisor
Preparer Email
R*******************@e*********.com
Preparer Telephone
618-267-9641
Prepared Date
2023-09-13 00:00:00
Local Contact Name
R***** P S**********
Local Contact Email
R*******************@e*********.com
Local Contact Telephone
618-267-9641
Authorizer Name
L**** B******
Authorizer Telephone
281-382-6003
Authorizer Title
Regulatory Compliance Supervisor
Authorizer Email
L**************@e*********.com
Narrative
Background: the working foreman was at tank #909 dike area to inspect a prv. He observed discoloration of stones and wetness around the tank chime. He opened the double bottom telltale valve and found product present. He notified the supervisor and absorbent booms were deployed around the tank chime and it was confirmed that the tank dike drain valve was closed. Approximately 5 gallons of trans mix (gasoline & diesel) was released to soil inside the tank dike. Immediate corrective actions: tank #909 was isolated, and two layers of absorbent boom were placed around the tank. A project was executed to de-inventory, clean and gas free tank #909 to allow for an internal API 653 inspection. Preventing re-occurrence: an API 653 internal inspection was completed, and all necessary repairs were made to the tank bottom per API 650 standards.
Report Received Date 2023-09-18 00:00:00
Iyear 2023
Report Number 20230218
Supplemental Number 38560
Report Type Original Final
Operator Id 4906 PHMSA Enforcement
Name Exxonmobil Pipeline Company Llc
Operator Street Address 22777 Springwoods Village Parkway E2.2b-Emp
Operator City Name Spring
Operator State Abbreviation TX
Operator Postal Code 77389
Time Zone Central
Daylight Savings Ind No
Location Latitude 41.6508294 Google Maps OpenStreetMap
Location Longitude -88.043011 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Mixture Of Refined Products (Transmix Or Other Mixture)
Unintentional Release Bbls 0.12
Recovered Bbls 0.12
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
System Part Involved Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind No
Shutdown Explain Pipeline Was Not Flowing At The Time Of Incident
Communication State Fed Ind Yes
Party Initiated Communication Operator
Nrc Rpt Num 1376950 NRC Report How to search
Additional Nrc Report Numbers 1377175
Ignite Ind No
Notify Qualified Indiv Ind Yes
Oil Spill Removal Org Ind Yes
Osro Arrived On Site Dt 8/22/2023 15:35
Num Pub Evacuated 0
Pipe Fac Name Lockport Terminal
Segment Name Tank #909
Onshore State Abbreviation Il
Onshore Postal Code 60441
Onshore City Name Lockport
Onshore County Name Will County
Designated Location Milepost
Designated Name 0
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Tank, Including Attached Appurtenances
Crossing No
Pipe Facility Type Interstate
Item Involved Tank/vessel
Tank Vessel Subtype Double Bottom System
Tank Type Atmospheric
Safe Fill Level 24.5
Safe Fill Level Exceeded Ind No
Api Std Out Of Service Year 2011
Api Std In Service Year 2021
Installation Year 1971
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Crack
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 20
Est Cost Prop Damage 100000
Est Cost Emergency 10000
Est Cost Environmental 50000
Est Cost Other 0
Prpty 160020
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 5
Pressure Restriction Ind No
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Small seep from the double bottom and there was no indication of a leak in the control room.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Material Failure Of Pipe Or Weld
Cause Details Design-, Construction-, Installation-, Or Fabrication-Related
Field Exam Ind Yes
Other Analysis Ind Yes
Other Analysis Details Tank Floor Mfl Scan As Part Of Api 653
Failure Type Design-, Construction-, Installation-, Or Fabrication-Related
Other Factor Yes
Other Factor Details Weld Spacing
Additional Crack Ind Yes
Pwf Fabrication Ind Yes
Preparer Name R***** P S**********
Preparer Title Dot Pipeline Safety Advisor
Preparer Email R*******************@e*********.com
Preparer Telephone 618-267-9641
Prepared Date 2023-09-13 00:00:00
Local Contact Name R***** P S**********
Local Contact Email R*******************@e*********.com
Local Contact Telephone 618-267-9641
Authorizer Name L**** B******
Authorizer Telephone 281-382-6003
Authorizer Title Regulatory Compliance Supervisor
Authorizer Email L**************@e*********.com
Narrative Background: the working foreman was at tank #909 dike area to inspect a prv. He observed discoloration of stones and wetness around the tank chime. He opened the double bottom telltale valve and found product present. He notified the supervisor and absorbent booms were deployed around the tank chime and it was confirmed that the tank dike drain valve was closed. Approximately 5 gallons of trans mix (gasoline & diesel) was released to soil inside the tank dike. Immediate corrective actions: tank #909 was isolated, and two layers of absorbent boom were placed around the tank. A project was executed to de-inventory, clean and gas free tank #909 to allow for an internal API 653 inspection. Preventing re-occurrence: an API 653 internal inspection was completed, and all necessary repairs were made to the tank bottom per API 650 standards.

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