Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2023-09-13 — TX
Operator
Sunoco Pipeline L.p.
Cause
Material Failure Of Pipe Or Weld
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$104,892
Incident datetime
2023-09-13 00:00 UTC
Report number
Location
TX
Narrative
On 8/15/2023 at approximately 09:15, row maintenance crew identified a suspected release near the hebert to center pipeline. Later that day once the line was exposed, operations determined the leak was coming from the 21023 hebert to center 8-inch line. Approximately 10 barrels of diesel fuel released into the soil. 2 of the 10 barrels migrated into an unnamed tributary of chiamon bayou. Contractor mobilized for cleanup. All product removed from tributary and impacted soil. Visual and dye penetrant inspections showed a pinhole leak at the 6:00 oclock position on a historic repair sleeve fillet weld. The failed pipe section was removed and replaced with 122 ft. Of new pipe. On 8/18/2023 at approximately 01:00, the line was restarted. Company personnel inspected the failed section of pipe and determined the cause of the pinhole leak to be due to incomplete penetration of fillet weld on historic repair sleeve installation. The repair sleeve was installed prior to modern standard practices.
Detailed record list
Report Received Date
2023-09-13 00:00:00
Iyear
2023
Report Number
20230210
Supplemental Number
38728
Report Type
Supplemental Final
Operator Id
18718
Name
Sunoco Pipeline L.p.
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
31.375915
Location Longitude
-94.030011
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
10
Recovered Bbls
10
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Nrc Rpt Num
1376263
Additional Nrc Report Numbers
1376387
Ignite Ind
No
Upstream Action Taken
Valve Closure
Upstream Valve Type Ind
Remotely Controlled
Downstream Action Taken
Valve Closure
Downstream Valve Type Ind
Remotely Controlled
Notify Qualified Indiv Ind
Yes
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Magtex Pipeline
Segment Name
21023.01 Hebert To Center 8-Inch
Onshore State Abbreviation
Tx
Onshore Postal Code
75930
Onshore City Name
Bronson
Onshore County Name
San Augustine
Designated Location
Milepost
Designated Name
93.613
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
20
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Weld, Including Heat-Affected Zone
Weld Subtype
Fillet Weld
Installation Year
Unknown
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Surface Water Remed Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
Yes
Surface Contam Ind
Yes
Amount Released
2
Rel Water Name
Unnamed Tributary To Chiamon Bayou
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
336
Est Cost Prop Damage
104892
Est Cost Emergency
85000
Est Cost Environmental
191692
Est Cost Other
0
Prpty
381920
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
583
Mop Psig
730
Mop Cfr Section
Subpart E Pressure Test �195.406(A)(3)
Maop Established Date
2022-07-28 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
101587
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Design-, Construction-, Installation-, Or Fabrication-Related
Field Exam Ind
Yes
Other Analysis Ind
Yes
Other Analysis Details
Non Destructive Dye Penetrant Analysis
Failure Type
Design-, Construction-, Installation-, Or Fabrication-Related
Other Factor
Yes
Other Factor Details
Pinhole In Historic Repair Sleeve Fillet Weld
Pwf Additional Other Ind
Yes
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Geometry Deformation Ind
Yes
Axial Recent Year
2020
Axial Rcnt Propul Method
Free Swimming
Axial Rcnt Attuned Detect
Metal Loss
Axial Rcnt Atnd Dtct Metal
High Resolution
Axial Previous Year
2015
Axial Prev Propul Method
Free Swimming
Axial Prev Attuned Detect
Metal Loss
Axial Prev Atnd Dtct Metal
High Resolution
Geometry Recent Year
2020
Geometry Rcnt Propul Method
Free Swimming
Geometry Rcnt Resolution
High Resolution
Geometrt Rcnt Measur Cups
Inside Ili Cups
Geometry Previous Year
2015
Geometry Prev Propul Method
Free Swimming
Geometry Prev Resolution
High Resolution
Geometrt Prev Measur Cups
Inside Ili Cups
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
2022
Hydrtst Most Rcnt Pressure
945
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
T*** N*******
Preparer Title
Director - Dot Compliance
Preparer Email
T************@e*************.com
Preparer Telephone
713-989-7126
Prepared Date
2023-11-01 00:00:00
Authorizer Name
T*** N*******
Authorizer Telephone
713-989-7126
Authorizer Title
Director - Dot Compliance
Authorizer Email
T************@e*************.com
Narrative
On 8/15/2023 at approximately 09:15, row maintenance crew identified a suspected release near the hebert to center pipeline. Later that day once the line was exposed, operations determined the leak was coming from the 21023 hebert to center 8-inch line. Approximately 10 barrels of diesel fuel released into the soil. 2 of the 10 barrels migrated into an unnamed tributary of chiamon bayou. Contractor mobilized for cleanup. All product removed from tributary and impacted soil. Visual and dye penetrant inspections showed a pinhole leak at the 6:00 oclock position on a historic repair sleeve fillet weld. The failed pipe section was removed and replaced with 122 ft. Of new pipe. On 8/18/2023 at approximately 01:00, the line was restarted. Company personnel inspected the failed section of pipe and determined the cause of the pinhole leak to be due to incomplete penetration of fillet weld on historic repair sleeve installation. The repair sleeve was installed prior to modern standard practices.
Report Received Date | 2023-09-13 00:00:00 |
---|---|
Iyear | 2023 |
Report Number | 20230210 |
Supplemental Number | 38728 |
Report Type | Supplemental Final |
Operator Id | 18718 PHMSA Enforcement |
Name | Sunoco Pipeline L.p. |
Operator Street Address | 1300 Main Street |
Operator City Name | Houston |
Operator State Abbreviation | TX |
Operator Postal Code | 77002 |
Time Zone | Central |
Daylight Savings Ind | Yes |
Location Latitude | 31.375915 Google Maps OpenStreetMap |
Location Longitude | -94.030011 Google Maps OpenStreetMap |
Commodity Released Type | Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions |
Commodity Subtype | Diesel, Fuel Oil, Kerosene, Jet Fuel |
Unintentional Release Bbls | 10 |
Recovered Bbls | 10 |
Fatality Ind | No |
Fatal | 0 |
Injury Ind | No |
Injure | 0 |
Accident Identifier | Local Operating Personnel, Including Contractors |
Operator Type | Operator Employee |
System Part Involved | Onshore Pipeline, Including Valve Sites |
On Off Shore | Onshore |
Status When Identified | Normal Operation, Includes Pauses Between Batches And During Maintenance |
Shutdown Due Accident Ind | Yes |
Communication State Fed Ind | Yes |
Party Initiated Communication | Operator |
Nrc Rpt Num | 1376263 NRC Report How to search |
Additional Nrc Report Numbers | 1376387 |
Ignite Ind | No |
Upstream Action Taken | Valve Closure |
Upstream Valve Type Ind | Remotely Controlled |
Downstream Action Taken | Valve Closure |
Downstream Valve Type Ind | Remotely Controlled |
Notify Qualified Indiv Ind | Yes |
Oil Spill Removal Org Ind | No |
Num Pub Evacuated | 0 |
Pipe Fac Name | Magtex Pipeline |
Segment Name | 21023.01 Hebert To Center 8-Inch |
Onshore State Abbreviation | Tx |
Onshore Postal Code | 75930 |
Onshore City Name | Bronson |
Onshore County Name | San Augustine |
Designated Location | Milepost |
Designated Name | 93.613 |
Federal | No |
Location Type | Pipeline Right-Of-Way |
Incident Area Type | Underground |
Incident Area Subtype | Under Soil |
Depth Of Cover | 20 |
Crossing | No |
Pipe Facility Type | Intrastate |
Item Involved | Weld, Including Heat-Affected Zone |
Weld Subtype | Fillet Weld |
Installation Year | Unknown |
Manufactured Year | Unknown |
Material Involved | Carbon Steel |
Release Type | Leak |
Leak Type | Pinhole |
Wildlife Impact Ind | No |
Soil Contamination | Yes |
Long Term Assessment | No |
Remediation Ind | Yes |
Surface Water Remed Ind | Yes |
Soil Remed Ind | Yes |
Water Contam Ind | Yes |
Surface Contam Ind | Yes |
Amount Released | 2 |
Rel Water Name | Unnamed Tributary To Chiamon Bayou |
Could Be Hca | No |
Commodity Reached Hca | No |
Est Cost Oper Paid | 0 |
Est Cost Gas Released | 336 |
Est Cost Prop Damage | 104892 |
Est Cost Emergency | 85000 |
Est Cost Environmental | 191692 |
Est Cost Other | 0 |
Prpty | 381920 |
Num Persons Hosp Not Ovnght | 0 |
Num Injured Treated By Emt | 0 |
Num Resident Building Affctd | 0 |
Num Business Building Affctd | 0 |
Accident Psig | 583 |
Mop Psig | 730 |
Mop Cfr Section | Subpart E Pressure Test �195.406(A)(3) View CFR 49 §192 |
Maop Established Date | 2022-07-28 00:00:00 |
Maop Reversal Flow Ind | No |
Accident Pressure | Pressure Did Not Exceed Mop |
Pressure Restriction Ind | No |
Length Segment Isolated | 101587 |
Internal Inspection Ind | Yes |
Operation Complications Ind | No |
Pipeline Function | > 20% Smys Regulated Transmission |
Scada In Place Ind | Yes |
Scada Operating Ind | Yes |
Scada Functional Ind | Yes |
Scada Detection Ind | No |
Scada Conf Ind | No |
Cpm In Place Ind | Yes |
Cpm Operating Ind | Yes |
Cpm Functional Ind | Yes |
Cpm Detection Ind | No |
Cpm Conf Ind | No |
Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
Investigation Status Details | A review of the accident determined that there were no control room actions that contributed to the event. |
Employee Drug Test Ind | No |
Contractor Drug Test Ind | No |
Cause | Material Failure Of Pipe Or Weld |
Cause Details | Design-, Construction-, Installation-, Or Fabrication-Related |
Field Exam Ind | Yes |
Other Analysis Ind | Yes |
Other Analysis Details | Non Destructive Dye Penetrant Analysis |
Failure Type | Design-, Construction-, Installation-, Or Fabrication-Related |
Other Factor | Yes |
Other Factor Details | Pinhole In Historic Repair Sleeve Fillet Weld |
Pwf Additional Other Ind | Yes |
Collected Data Ind | Yes |
Axial Magnetic Flx Lkg Ind | Yes |
Geometry Deformation Ind | Yes |
Axial Recent Year | 2020 |
Axial Rcnt Propul Method | Free Swimming |
Axial Rcnt Attuned Detect | Metal Loss |
Axial Rcnt Atnd Dtct Metal | High Resolution |
Axial Previous Year | 2015 |
Axial Prev Propul Method | Free Swimming |
Axial Prev Attuned Detect | Metal Loss |
Axial Prev Atnd Dtct Metal | High Resolution |
Geometry Recent Year | 2020 |
Geometry Rcnt Propul Method | Free Swimming |
Geometry Rcnt Resolution | High Resolution |
Geometrt Rcnt Measur Cups | Inside Ili Cups |
Geometry Previous Year | 2015 |
Geometry Prev Propul Method | Free Swimming |
Geometry Prev Resolution | High Resolution |
Geometrt Prev Measur Cups | Inside Ili Cups |
Has Hydrtst Conduc Before Ind | Yes |
Hydrtst Most Rcnt Year | 2022 |
Hydrtst Most Rcnt Pressure | 945 |
Direct Asmnt Conducted | No |
Non Destructive Exam Ind | No |
Preparer Name | T*** N******* |
Preparer Title | Director - Dot Compliance |
Preparer Email | T************@e*************.com |
Preparer Telephone | 713-989-7126 |
Prepared Date | 2023-11-01 00:00:00 |
Authorizer Name | T*** N******* |
Authorizer Telephone | 713-989-7126 |
Authorizer Title | Director - Dot Compliance |
Authorizer Email | T************@e*************.com |
Narrative | On 8/15/2023 at approximately 09:15, row maintenance crew identified a suspected release near the hebert to center pipeline. Later that day once the line was exposed, operations determined the leak was coming from the 21023 hebert to center 8-inch line. Approximately 10 barrels of diesel fuel released into the soil. 2 of the 10 barrels migrated into an unnamed tributary of chiamon bayou. Contractor mobilized for cleanup. All product removed from tributary and impacted soil. Visual and dye penetrant inspections showed a pinhole leak at the 6:00 oclock position on a historic repair sleeve fillet weld. The failed pipe section was removed and replaced with 122 ft. Of new pipe. On 8/18/2023 at approximately 01:00, the line was restarted. Company personnel inspected the failed section of pipe and determined the cause of the pinhole leak to be due to incomplete penetration of fillet weld on historic repair sleeve installation. The repair sleeve was installed prior to modern standard practices. |
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