HL incident on 2023-09-13 — TX

Operator
Sunoco Pipeline L.p.
Cause
Material Failure Of Pipe Or Weld
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$104,892
Incident datetime
2023-09-13 00:00 UTC
Report number
Location
TX
Narrative
On 8/15/2023 at approximately 09:15, row maintenance crew identified a suspected release near the hebert to center pipeline. Later that day once the line was exposed, operations determined the leak was coming from the 21023 hebert to center 8-inch line. Approximately 10 barrels of diesel fuel released into the soil. 2 of the 10 barrels migrated into an unnamed tributary of chiamon bayou. Contractor mobilized for cleanup. All product removed from tributary and impacted soil. Visual and dye penetrant inspections showed a pinhole leak at the 6:00 oclock position on a historic repair sleeve fillet weld. The failed pipe section was removed and replaced with 122 ft. Of new pipe. On 8/18/2023 at approximately 01:00, the line was restarted. Company personnel inspected the failed section of pipe and determined the cause of the pinhole leak to be due to incomplete penetration of fillet weld on historic repair sleeve installation. The repair sleeve was installed prior to modern standard practices.
Detailed record list
Report Received Date
2023-09-13 00:00:00
Iyear
2023
Report Number
20230210
Supplemental Number
38728
Report Type
Supplemental Final
Operator Id
Name
Sunoco Pipeline L.p.
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
10
Recovered Bbls
10
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Nrc Rpt Num
Additional Nrc Report Numbers
1376387
Ignite Ind
No
Upstream Action Taken
Valve Closure
Upstream Valve Type Ind
Remotely Controlled
Downstream Action Taken
Valve Closure
Downstream Valve Type Ind
Remotely Controlled
Notify Qualified Indiv Ind
Yes
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Magtex Pipeline
Segment Name
21023.01 Hebert To Center 8-Inch
Onshore State Abbreviation
Tx
Onshore Postal Code
75930
Onshore City Name
Bronson
Onshore County Name
San Augustine
Designated Location
Milepost
Designated Name
93.613
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
20
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Weld, Including Heat-Affected Zone
Weld Subtype
Fillet Weld
Installation Year
Unknown
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Surface Water Remed Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
Yes
Surface Contam Ind
Yes
Amount Released
2
Rel Water Name
Unnamed Tributary To Chiamon Bayou
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
336
Est Cost Prop Damage
104892
Est Cost Emergency
85000
Est Cost Environmental
191692
Est Cost Other
0
Prpty
381920
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
583
Mop Psig
730
Mop Cfr Section
Subpart E Pressure Test �195.406(A)(3)
Maop Established Date
2022-07-28 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
101587
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Design-, Construction-, Installation-, Or Fabrication-Related
Field Exam Ind
Yes
Other Analysis Ind
Yes
Other Analysis Details
Non Destructive Dye Penetrant Analysis
Failure Type
Design-, Construction-, Installation-, Or Fabrication-Related
Other Factor
Yes
Other Factor Details
Pinhole In Historic Repair Sleeve Fillet Weld
Pwf Additional Other Ind
Yes
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Geometry Deformation Ind
Yes
Axial Recent Year
2020
Axial Rcnt Propul Method
Free Swimming
Axial Rcnt Attuned Detect
Metal Loss
Axial Rcnt Atnd Dtct Metal
High Resolution
Axial Previous Year
2015
Axial Prev Propul Method
Free Swimming
Axial Prev Attuned Detect
Metal Loss
Axial Prev Atnd Dtct Metal
High Resolution
Geometry Recent Year
2020
Geometry Rcnt Propul Method
Free Swimming
Geometry Rcnt Resolution
High Resolution
Geometrt Rcnt Measur Cups
Inside Ili Cups
Geometry Previous Year
2015
Geometry Prev Propul Method
Free Swimming
Geometry Prev Resolution
High Resolution
Geometrt Prev Measur Cups
Inside Ili Cups
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
2022
Hydrtst Most Rcnt Pressure
945
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
T*** N*******
Preparer Title
Director - Dot Compliance
Preparer Email
T************@e*************.com
Preparer Telephone
713-989-7126
Prepared Date
2023-11-01 00:00:00
Authorizer Name
T*** N*******
Authorizer Telephone
713-989-7126
Authorizer Title
Director - Dot Compliance
Authorizer Email
T************@e*************.com
Narrative
On 8/15/2023 at approximately 09:15, row maintenance crew identified a suspected release near the hebert to center pipeline. Later that day once the line was exposed, operations determined the leak was coming from the 21023 hebert to center 8-inch line. Approximately 10 barrels of diesel fuel released into the soil. 2 of the 10 barrels migrated into an unnamed tributary of chiamon bayou. Contractor mobilized for cleanup. All product removed from tributary and impacted soil. Visual and dye penetrant inspections showed a pinhole leak at the 6:00 oclock position on a historic repair sleeve fillet weld. The failed pipe section was removed and replaced with 122 ft. Of new pipe. On 8/18/2023 at approximately 01:00, the line was restarted. Company personnel inspected the failed section of pipe and determined the cause of the pinhole leak to be due to incomplete penetration of fillet weld on historic repair sleeve installation. The repair sleeve was installed prior to modern standard practices.
Report Received Date 2023-09-13 00:00:00
Iyear 2023
Report Number 20230210
Supplemental Number 38728
Report Type Supplemental Final
Operator Id 18718 PHMSA Enforcement
Name Sunoco Pipeline L.p.
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 31.375915 Google Maps OpenStreetMap
Location Longitude -94.030011 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 10
Recovered Bbls 10
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind Yes
Communication State Fed Ind Yes
Party Initiated Communication Operator
Nrc Rpt Num 1376263 NRC Report How to search
Additional Nrc Report Numbers 1376387
Ignite Ind No
Upstream Action Taken Valve Closure
Upstream Valve Type Ind Remotely Controlled
Downstream Action Taken Valve Closure
Downstream Valve Type Ind Remotely Controlled
Notify Qualified Indiv Ind Yes
Oil Spill Removal Org Ind No
Num Pub Evacuated 0
Pipe Fac Name Magtex Pipeline
Segment Name 21023.01 Hebert To Center 8-Inch
Onshore State Abbreviation Tx
Onshore Postal Code 75930
Onshore City Name Bronson
Onshore County Name San Augustine
Designated Location Milepost
Designated Name 93.613
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 20
Crossing No
Pipe Facility Type Intrastate
Item Involved Weld, Including Heat-Affected Zone
Weld Subtype Fillet Weld
Installation Year Unknown
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Surface Water Remed Ind Yes
Soil Remed Ind Yes
Water Contam Ind Yes
Surface Contam Ind Yes
Amount Released 2
Rel Water Name Unnamed Tributary To Chiamon Bayou
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 336
Est Cost Prop Damage 104892
Est Cost Emergency 85000
Est Cost Environmental 191692
Est Cost Other 0
Prpty 381920
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 583
Mop Psig 730
Mop Cfr Section Subpart E Pressure Test �195.406(A)(3) View CFR 49 §192
Maop Established Date 2022-07-28 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 101587
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Material Failure Of Pipe Or Weld
Cause Details Design-, Construction-, Installation-, Or Fabrication-Related
Field Exam Ind Yes
Other Analysis Ind Yes
Other Analysis Details Non Destructive Dye Penetrant Analysis
Failure Type Design-, Construction-, Installation-, Or Fabrication-Related
Other Factor Yes
Other Factor Details Pinhole In Historic Repair Sleeve Fillet Weld
Pwf Additional Other Ind Yes
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Geometry Deformation Ind Yes
Axial Recent Year 2020
Axial Rcnt Propul Method Free Swimming
Axial Rcnt Attuned Detect Metal Loss
Axial Rcnt Atnd Dtct Metal High Resolution
Axial Previous Year 2015
Axial Prev Propul Method Free Swimming
Axial Prev Attuned Detect Metal Loss
Axial Prev Atnd Dtct Metal High Resolution
Geometry Recent Year 2020
Geometry Rcnt Propul Method Free Swimming
Geometry Rcnt Resolution High Resolution
Geometrt Rcnt Measur Cups Inside Ili Cups
Geometry Previous Year 2015
Geometry Prev Propul Method Free Swimming
Geometry Prev Resolution High Resolution
Geometrt Prev Measur Cups Inside Ili Cups
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 2022
Hydrtst Most Rcnt Pressure 945
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name T*** N*******
Preparer Title Director - Dot Compliance
Preparer Email T************@e*************.com
Preparer Telephone 713-989-7126
Prepared Date 2023-11-01 00:00:00
Authorizer Name T*** N*******
Authorizer Telephone 713-989-7126
Authorizer Title Director - Dot Compliance
Authorizer Email T************@e*************.com
Narrative On 8/15/2023 at approximately 09:15, row maintenance crew identified a suspected release near the hebert to center pipeline. Later that day once the line was exposed, operations determined the leak was coming from the 21023 hebert to center 8-inch line. Approximately 10 barrels of diesel fuel released into the soil. 2 of the 10 barrels migrated into an unnamed tributary of chiamon bayou. Contractor mobilized for cleanup. All product removed from tributary and impacted soil. Visual and dye penetrant inspections showed a pinhole leak at the 6:00 oclock position on a historic repair sleeve fillet weld. The failed pipe section was removed and replaced with 122 ft. Of new pipe. On 8/18/2023 at approximately 01:00, the line was restarted. Company personnel inspected the failed section of pipe and determined the cause of the pinhole leak to be due to incomplete penetration of fillet weld on historic repair sleeve installation. The repair sleeve was installed prior to modern standard practices.

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