Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2023-09-07 — TX
Operator
Kinder Morgan Crude And Condensate Llc
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$53,500
Incident datetime
2023-09-07 00:00 UTC
Report number
Location
TX
Narrative
On august 20, 2023, a control room vapor alarm sounded at 0804 for the kmcc karnes pump station. The local operator was contacted and dispatched to the site and witnessed product leaking from a pin hole on the side of a strainer pot. The operator closed the valve and leak stopped. 21.4 bbls. Leaked into containment and 2 gallons sprayed outside containment. A vacuum truck was called to begin clean-up efforts, which were completed that evening. On august 28, 2023, it was determined the cost would exceed $50,000. The nrc was contacted and report 1377471 was taken. The following day, august 29, 2023, a 48-hour update was given to the nrc and report 1377624 was taken. On november 8, 2023, the investigation to determine the cause of the release was completed. The source of the release was a pinhole/corrosion pit that had completely penetrated the wall of strainer pot #502 caused by corrosion. The corrosion was caused by 1) the presence of corrosion-causing mechanisms (water, chlorides, oxygen, microbiologically influenced corrosion, iron sulfide); 2) the presence of dead-leg piping; and 3) the lack of direct chemical treatment upstream of this piping section. Changes have been made to this narrative. The wrong date was inadvertently entered for the nrc notification. The wrong time was also entered incorrectly in part a, question 21a. Both have been corrected.
Detailed record list
Report Received Date
2023-09-07 00:00:00
Iyear
2023
Report Number
20230209
Supplemental Number
38929
Report Type
Supplemental Final
Operator Id
32678
Name
Kinder Morgan Crude And Condensate Llc
Operator Street Address
1001 Louisiana St., Suite 1000
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
29.030131
Location Longitude
-97.789485
Commodity Released Type
Crude Oil
Unintentional Release Bbls
21.4
Recovered Bbls
21.4
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Or Pack Calculations)
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Status When Identified
Routine Shutdown
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Nrc Rpt Num
1377471
Additional Nrc Report Numbers
1377624
Ignite Ind
No
Notify Qualified Indiv Ind
Yes
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Karnes Pump Station
Segment Name
Opods-527
Onshore State Abbreviation
Tx
Onshore Postal Code
78151
Onshore City Name
Runge
Onshore County Name
Karnes
Designated Location
Survey Station No.
Designated Name
0+00
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Filter/strainer/separator
Installation Year
2014
Manufactured Year
2014
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
4
Est Cost Prop Damage
53500
Est Cost Emergency
2000
Est Cost Environmental
0
Est Cost Other
0
Prpty
55504
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
14
Mop Psig
285
Mop Cfr Section
Component Design Pressure �195.406(A)(2)
Maop Established Date
2014-08-27 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
There was a pinhole in the strainer pot that was not associated with the controller.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Corrosive Commodity Ind
Yes
Int Metallurgical Basis Ind
Yes
Int Dead Leg Loc Ind
Yes
Int Other Loc Ind
Yes
Corrosion Location Details
The Leak Location Was In The Body Of The Carbon-Steel Strainer. It Was Located Opposite The Inlet Of The Strainer..
Corrosion Inhibitors
No
Corrosion Lining
No
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
Yes
Preparer Name
S*** C*******
Preparer Title
Specialist-Technical Compliance Code St Ii
Preparer Email
S************@k***********.com
Preparer Telephone
7134204277
Prepared Date
2023-12-08 00:00:00
Local Contact Name
S*** S******
Local Contact Email
S***********@k***********.com
Local Contact Telephone
7134203219
Authorizer Name
D******* S*******
Authorizer Telephone
7134206496
Authorizer Title
Manager Codes And Standards
Authorizer Email
D****************@k***********.com
Narrative
On august 20, 2023, a control room vapor alarm sounded at 0804 for the kmcc karnes pump station. The local operator was contacted and dispatched to the site and witnessed product leaking from a pin hole on the side of a strainer pot. The operator closed the valve and leak stopped. 21.4 bbls. Leaked into containment and 2 gallons sprayed outside containment. A vacuum truck was called to begin clean-up efforts, which were completed that evening. On august 28, 2023, it was determined the cost would exceed $50,000. The nrc was contacted and report 1377471 was taken. The following day, august 29, 2023, a 48-hour update was given to the nrc and report 1377624 was taken. On november 8, 2023, the investigation to determine the cause of the release was completed. The source of the release was a pinhole/corrosion pit that had completely penetrated the wall of strainer pot #502 caused by corrosion. The corrosion was caused by 1) the presence of corrosion-causing mechanisms (water, chlorides, oxygen, microbiologically influenced corrosion, iron sulfide); 2) the presence of dead-leg piping; and 3) the lack of direct chemical treatment upstream of this piping section. Changes have been made to this narrative. The wrong date was inadvertently entered for the nrc notification. The wrong time was also entered incorrectly in part a, question 21a. Both have been corrected.
Report Received Date | 2023-09-07 00:00:00 |
---|---|
Iyear | 2023 |
Report Number | 20230209 |
Supplemental Number | 38929 |
Report Type | Supplemental Final |
Operator Id | 32678 PHMSA Enforcement |
Name | Kinder Morgan Crude And Condensate Llc |
Operator Street Address | 1001 Louisiana St., Suite 1000 |
Operator City Name | Houston |
Operator State Abbreviation | TX |
Operator Postal Code | 77002 |
Time Zone | Central |
Daylight Savings Ind | Yes |
Location Latitude | 29.030131 Google Maps OpenStreetMap |
Location Longitude | -97.789485 Google Maps OpenStreetMap |
Commodity Released Type | Crude Oil |
Unintentional Release Bbls | 21.4 |
Recovered Bbls | 21.4 |
Fatality Ind | No |
Fatal | 0 |
Injury Ind | No |
Injure | 0 |
Accident Identifier | Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Or Pack Calculations) |
System Part Involved | Onshore Pump/meter Station Equipment And Piping |
On Off Shore | Onshore |
Status When Identified | Routine Shutdown |
Communication State Fed Ind | Yes |
Party Initiated Communication | Operator |
Nrc Rpt Num | 1377471 NRC Report How to search |
Additional Nrc Report Numbers | 1377624 |
Ignite Ind | No |
Notify Qualified Indiv Ind | Yes |
Oil Spill Removal Org Ind | No |
Num Pub Evacuated | 0 |
Pipe Fac Name | Karnes Pump Station |
Segment Name | Opods-527 |
Onshore State Abbreviation | Tx |
Onshore Postal Code | 78151 |
Onshore City Name | Runge |
Onshore County Name | Karnes |
Designated Location | Survey Station No. |
Designated Name | 0+00 |
Federal | No |
Location Type | Totally Contained On Operator-Controlled Property |
Incident Area Type | Aboveground |
Incident Area Subtype | Typical Aboveground Facility Piping Or Appurtenance |
Crossing | No |
Pipe Facility Type | Intrastate |
Item Involved | Filter/strainer/separator |
Installation Year | 2014 |
Manufactured Year | 2014 |
Material Involved | Carbon Steel |
Release Type | Leak |
Leak Type | Pinhole |
Wildlife Impact Ind | No |
Soil Contamination | No |
Long Term Assessment | No |
Remediation Ind | No |
Water Contam Ind | No |
Could Be Hca | Yes |
Commodity Reached Hca | No |
Est Cost Oper Paid | 0 |
Est Cost Gas Released | 4 |
Est Cost Prop Damage | 53500 |
Est Cost Emergency | 2000 |
Est Cost Environmental | 0 |
Est Cost Other | 0 |
Prpty | 55504 |
Num Persons Hosp Not Ovnght | 0 |
Num Injured Treated By Emt | 0 |
Num Resident Building Affctd | 0 |
Num Business Building Affctd | 0 |
Accident Psig | 14 |
Mop Psig | 285 |
Mop Cfr Section | Component Design Pressure �195.406(A)(2) View CFR 49 §192 |
Maop Established Date | 2014-08-27 00:00:00 |
Maop Reversal Flow Ind | No |
Accident Pressure | Pressure Did Not Exceed Mop |
Pressure Restriction Ind | No |
Pipeline Function | > 20% Smys Regulated Transmission |
Scada In Place Ind | Yes |
Scada Operating Ind | Yes |
Scada Functional Ind | Yes |
Scada Detection Ind | Yes |
Scada Conf Ind | Yes |
Cpm In Place Ind | No |
Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
Investigation Status Details | There was a pinhole in the strainer pot that was not associated with the controller. |
Employee Drug Test Ind | No |
Contractor Drug Test Ind | No |
Cause | Corrosion Failure |
Cause Details | Internal Corrosion |
Internal External | Internal Corrosion |
Int Visual Exam Results | Localized Pitting |
Int Corrosive Commodity Ind | Yes |
Int Metallurgical Basis Ind | Yes |
Int Dead Leg Loc Ind | Yes |
Int Other Loc Ind | Yes |
Corrosion Location Details | The Leak Location Was In The Body Of The Carbon-Steel Strainer. It Was Located Opposite The Inlet Of The Strainer.. |
Corrosion Inhibitors | No |
Corrosion Lining | No |
Cleaning Dewatering | Not Applicable - Not Mainline Pipe |
Corrosion Coupons | Yes |
Preparer Name | S*** C******* |
Preparer Title | Specialist-Technical Compliance Code St Ii |
Preparer Email | S************@k***********.com |
Preparer Telephone | 7134204277 |
Prepared Date | 2023-12-08 00:00:00 |
Local Contact Name | S*** S****** |
Local Contact Email | S***********@k***********.com |
Local Contact Telephone | 7134203219 |
Authorizer Name | D******* S******* |
Authorizer Telephone | 7134206496 |
Authorizer Title | Manager Codes And Standards |
Authorizer Email | D****************@k***********.com |
Narrative | On august 20, 2023, a control room vapor alarm sounded at 0804 for the kmcc karnes pump station. The local operator was contacted and dispatched to the site and witnessed product leaking from a pin hole on the side of a strainer pot. The operator closed the valve and leak stopped. 21.4 bbls. Leaked into containment and 2 gallons sprayed outside containment. A vacuum truck was called to begin clean-up efforts, which were completed that evening. On august 28, 2023, it was determined the cost would exceed $50,000. The nrc was contacted and report 1377471 was taken. The following day, august 29, 2023, a 48-hour update was given to the nrc and report 1377624 was taken. On november 8, 2023, the investigation to determine the cause of the release was completed. The source of the release was a pinhole/corrosion pit that had completely penetrated the wall of strainer pot #502 caused by corrosion. The corrosion was caused by 1) the presence of corrosion-causing mechanisms (water, chlorides, oxygen, microbiologically influenced corrosion, iron sulfide); 2) the presence of dead-leg piping; and 3) the lack of direct chemical treatment upstream of this piping section. Changes have been made to this narrative. The wrong date was inadvertently entered for the nrc notification. The wrong time was also entered incorrectly in part a, question 21a. Both have been corrected. |
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