HL incident on 2023-09-07 — TX

Operator
Kinder Morgan Crude And Condensate Llc
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$53,500
Incident datetime
2023-09-07 00:00 UTC
Report number
Location
TX
Narrative
On august 20, 2023, a control room vapor alarm sounded at 0804 for the kmcc karnes pump station. The local operator was contacted and dispatched to the site and witnessed product leaking from a pin hole on the side of a strainer pot. The operator closed the valve and leak stopped. 21.4 bbls. Leaked into containment and 2 gallons sprayed outside containment. A vacuum truck was called to begin clean-up efforts, which were completed that evening. On august 28, 2023, it was determined the cost would exceed $50,000. The nrc was contacted and report 1377471 was taken. The following day, august 29, 2023, a 48-hour update was given to the nrc and report 1377624 was taken. On november 8, 2023, the investigation to determine the cause of the release was completed. The source of the release was a pinhole/corrosion pit that had completely penetrated the wall of strainer pot #502 caused by corrosion. The corrosion was caused by 1) the presence of corrosion-causing mechanisms (water, chlorides, oxygen, microbiologically influenced corrosion, iron sulfide); 2) the presence of dead-leg piping; and 3) the lack of direct chemical treatment upstream of this piping section. Changes have been made to this narrative. The wrong date was inadvertently entered for the nrc notification. The wrong time was also entered incorrectly in part a, question 21a. Both have been corrected.
Detailed record list
Report Received Date
2023-09-07 00:00:00
Iyear
2023
Report Number
20230209
Supplemental Number
38929
Report Type
Supplemental Final
Operator Id
Name
Kinder Morgan Crude And Condensate Llc
Operator Street Address
1001 Louisiana St., Suite 1000
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
21.4
Recovered Bbls
21.4
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Or Pack Calculations)
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Status When Identified
Routine Shutdown
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Nrc Rpt Num
Additional Nrc Report Numbers
1377624
Ignite Ind
No
Notify Qualified Indiv Ind
Yes
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Karnes Pump Station
Segment Name
Opods-527
Onshore State Abbreviation
Tx
Onshore Postal Code
78151
Onshore City Name
Runge
Onshore County Name
Karnes
Designated Location
Survey Station No.
Designated Name
0+00
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Filter/strainer/separator
Installation Year
2014
Manufactured Year
2014
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
4
Est Cost Prop Damage
53500
Est Cost Emergency
2000
Est Cost Environmental
0
Est Cost Other
0
Prpty
55504
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
14
Mop Psig
285
Mop Cfr Section
Component Design Pressure �195.406(A)(2)
Maop Established Date
2014-08-27 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
There was a pinhole in the strainer pot that was not associated with the controller.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Corrosive Commodity Ind
Yes
Int Metallurgical Basis Ind
Yes
Int Dead Leg Loc Ind
Yes
Int Other Loc Ind
Yes
Corrosion Location Details
The Leak Location Was In The Body Of The Carbon-Steel Strainer. It Was Located Opposite The Inlet Of The Strainer..
Corrosion Inhibitors
No
Corrosion Lining
No
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
Yes
Preparer Name
S*** C*******
Preparer Title
Specialist-Technical Compliance Code St Ii
Preparer Email
S************@k***********.com
Preparer Telephone
7134204277
Prepared Date
2023-12-08 00:00:00
Local Contact Name
S*** S******
Local Contact Email
S***********@k***********.com
Local Contact Telephone
7134203219
Authorizer Name
D******* S*******
Authorizer Telephone
7134206496
Authorizer Title
Manager Codes And Standards
Authorizer Email
D****************@k***********.com
Narrative
On august 20, 2023, a control room vapor alarm sounded at 0804 for the kmcc karnes pump station. The local operator was contacted and dispatched to the site and witnessed product leaking from a pin hole on the side of a strainer pot. The operator closed the valve and leak stopped. 21.4 bbls. Leaked into containment and 2 gallons sprayed outside containment. A vacuum truck was called to begin clean-up efforts, which were completed that evening. On august 28, 2023, it was determined the cost would exceed $50,000. The nrc was contacted and report 1377471 was taken. The following day, august 29, 2023, a 48-hour update was given to the nrc and report 1377624 was taken. On november 8, 2023, the investigation to determine the cause of the release was completed. The source of the release was a pinhole/corrosion pit that had completely penetrated the wall of strainer pot #502 caused by corrosion. The corrosion was caused by 1) the presence of corrosion-causing mechanisms (water, chlorides, oxygen, microbiologically influenced corrosion, iron sulfide); 2) the presence of dead-leg piping; and 3) the lack of direct chemical treatment upstream of this piping section. Changes have been made to this narrative. The wrong date was inadvertently entered for the nrc notification. The wrong time was also entered incorrectly in part a, question 21a. Both have been corrected.
Report Received Date 2023-09-07 00:00:00
Iyear 2023
Report Number 20230209
Supplemental Number 38929
Report Type Supplemental Final
Operator Id 32678 PHMSA Enforcement
Name Kinder Morgan Crude And Condensate Llc
Operator Street Address 1001 Louisiana St., Suite 1000
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 29.030131 Google Maps OpenStreetMap
Location Longitude -97.789485 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 21.4
Recovered Bbls 21.4
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Or Pack Calculations)
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Status When Identified Routine Shutdown
Communication State Fed Ind Yes
Party Initiated Communication Operator
Nrc Rpt Num 1377471 NRC Report How to search
Additional Nrc Report Numbers 1377624
Ignite Ind No
Notify Qualified Indiv Ind Yes
Oil Spill Removal Org Ind No
Num Pub Evacuated 0
Pipe Fac Name Karnes Pump Station
Segment Name Opods-527
Onshore State Abbreviation Tx
Onshore Postal Code 78151
Onshore City Name Runge
Onshore County Name Karnes
Designated Location Survey Station No.
Designated Name 0+00
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Filter/strainer/separator
Installation Year 2014
Manufactured Year 2014
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 4
Est Cost Prop Damage 53500
Est Cost Emergency 2000
Est Cost Environmental 0
Est Cost Other 0
Prpty 55504
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 14
Mop Psig 285
Mop Cfr Section Component Design Pressure �195.406(A)(2) View CFR 49 §192
Maop Established Date 2014-08-27 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details There was a pinhole in the strainer pot that was not associated with the controller.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Localized Pitting
Int Corrosive Commodity Ind Yes
Int Metallurgical Basis Ind Yes
Int Dead Leg Loc Ind Yes
Int Other Loc Ind Yes
Corrosion Location Details The Leak Location Was In The Body Of The Carbon-Steel Strainer. It Was Located Opposite The Inlet Of The Strainer..
Corrosion Inhibitors No
Corrosion Lining No
Cleaning Dewatering Not Applicable - Not Mainline Pipe
Corrosion Coupons Yes
Preparer Name S*** C*******
Preparer Title Specialist-Technical Compliance Code St Ii
Preparer Email S************@k***********.com
Preparer Telephone 7134204277
Prepared Date 2023-12-08 00:00:00
Local Contact Name S*** S******
Local Contact Email S***********@k***********.com
Local Contact Telephone 7134203219
Authorizer Name D******* S*******
Authorizer Telephone 7134206496
Authorizer Title Manager Codes And Standards
Authorizer Email D****************@k***********.com
Narrative On august 20, 2023, a control room vapor alarm sounded at 0804 for the kmcc karnes pump station. The local operator was contacted and dispatched to the site and witnessed product leaking from a pin hole on the side of a strainer pot. The operator closed the valve and leak stopped. 21.4 bbls. Leaked into containment and 2 gallons sprayed outside containment. A vacuum truck was called to begin clean-up efforts, which were completed that evening. On august 28, 2023, it was determined the cost would exceed $50,000. The nrc was contacted and report 1377471 was taken. The following day, august 29, 2023, a 48-hour update was given to the nrc and report 1377624 was taken. On november 8, 2023, the investigation to determine the cause of the release was completed. The source of the release was a pinhole/corrosion pit that had completely penetrated the wall of strainer pot #502 caused by corrosion. The corrosion was caused by 1) the presence of corrosion-causing mechanisms (water, chlorides, oxygen, microbiologically influenced corrosion, iron sulfide); 2) the presence of dead-leg piping; and 3) the lack of direct chemical treatment upstream of this piping section. Changes have been made to this narrative. The wrong date was inadvertently entered for the nrc notification. The wrong time was also entered incorrectly in part a, question 21a. Both have been corrected.

All rights reserved. Copyright © by ClearPHMSA