HL incident on 2023-09-05 — LA

Operator
Imtt-Bayonne
Cause
Other Accident Cause
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2023-09-05 00:00 UTC
Report number
Location
LA
Narrative
8/9/2023- imtt-bayonne was receiving barrels from a vessel into bot 5803. @ approx1825 the hi level alarm(hla) for 5803 signaled a hi alarm. The vessel was shut down, imtt field personnel obtained a gauge on the tank, according to the figures the level was 3,000bbls from safe fill. Once that was determined, the vessel was restarted. Imtt field personnel were on top of the tank monitoring the level until the safe fill was to be reached. Within 10 minutes of the restart, imtt field personnel observed product spilling from a side vent, the vessel was immediately shut down and the tank valves were secured. The level of the product was lowered and transferred to another tank. Imtt immediately initiated an emergency response. It is estimated that 321 bbls released through the overflow vent, approx. 40 bbls were recovered and disposed. After completion of the investigation, imtt determined third party contractor that calculated the safe fill for 5803, used the wrong calculations. Imtt field personnel were not at fault for this incident, therefore they were not administered a DOT post accident drug screen.
Detailed record list
Report Received Date
2023-09-05 00:00:00
Iyear
2023
Report Number
20230206
Supplemental Number
40086
Report Type
Supplemental
Operator Id
Name
Imtt-Bayonne
Operator Street Address
400 Poydras Street Suite 3000
Operator City Name
New Orleans
Operator State Abbreviation
LA
Operator Postal Code
70130
Time Zone
Eastern
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
321
Recovered Bbls
40
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
System Part Involved
Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
No
Shutdown Explain
Impacted Facilities Were Shut Down, Other Operations Continued
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Nrc Rpt Num
Additional Nrc Report Numbers
1375882
Ignite Ind
No
Notify Qualified Indiv Ind
Yes
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Imtt-Bayonne
Segment Name
Bot 5803
Onshore State Abbreviation
Nj
Onshore Postal Code
07002
Onshore City Name
Bayonne
Onshore County Name
Hudson
Designated Location
Survey Station No.
Designated Name
5803
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tank/vessel
Tank Vessel Subtype
Vent
Tank Type
Atmospheric
Safe Fill Level
41.7
Safe Fill Level Exceeded Ind
Yes
Api Std Out Of Service Year
2023
Api Std No In Service Ind
Yes
Installation Year
1922
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Overfill Or Overflow
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
Yes
Remediation Ind
Yes
Groundwater Remed Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
40000
Est Cost Prop Damage
0
Est Cost Emergency
5000
Est Cost Environmental
175000
Est Cost Other
5000
Est Cost Other Details
Contractor Fees To Inspect Internal Floating Roof.
Prpty
225000
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
90
Pressure Restriction Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Other Accident Cause
Cause Details
Miscellaneous
Other Type
Miscellaneous
Misc Details
An Incorrect Strapping Chart For The Breakout Tank (5803) Was In Use By The Imtt Inventory Control Software Program.
Preparer Name
R***** M**********
Preparer Email
R****************@i***.com
Preparer Telephone
2018235334
Prepared Date
2024-10-10 00:00:00
Local Contact Name
R***** M**********
Local Contact Email
R****************@i***.com
Local Contact Telephone
2018235334
Authorizer Name
R*** A*******
Authorizer Telephone
2014372200
Authorizer Title
Director Of Operations
Authorizer Email
R***********@i***.com
Narrative
8**************************************************************************@ approx1825 the hi level alarm(hla) for 5803 signaled a hi alarm. The vessel was shut down, imtt field personnel obtained a gauge on the tank, according to the figures the level was 3,000bbls from safe fill. Once that was determined, the vessel was restarted. Imtt field personnel were on top of the tank monitoring the level until the safe fill was to be reached. Within 10 minutes of the restart, imtt field personnel observed product spilling from a side vent, the vessel was immediately shut down and the tank valves were secured. The level of the product was lowered and transferred to another tank. Imtt immediately initiated an emergency response. It is estimated that 321 bbls released through the overflow vent, approx. 40 bbls were recovered and disposed. After completion of the investigation, imtt determined third party contractor that calculated the safe fill for 5803, used the wrong calculations. ********************************************************************************************************************************.
Report Received Date 2023-09-05 00:00:00
Iyear 2023
Report Number 20230206
Supplemental Number 40086
Report Type Supplemental
Operator Id 39149 PHMSA Enforcement
Name Imtt-Bayonne
Operator Street Address 400 Poydras Street Suite 3000
Operator City Name New Orleans
Operator State Abbreviation LA
Operator Postal Code 70130
Time Zone Eastern
Daylight Savings Ind Yes
Location Latitude 40.658472 Google Maps OpenStreetMap
Location Longitude -74.106889 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 321
Recovered Bbls 40
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
System Part Involved Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind No
Shutdown Explain Impacted Facilities Were Shut Down, Other Operations Continued
Communication State Fed Ind Yes
Party Initiated Communication Operator
Nrc Rpt Num 1375736 NRC Report How to search
Additional Nrc Report Numbers 1375882
Ignite Ind No
Notify Qualified Indiv Ind Yes
Oil Spill Removal Org Ind No
Num Pub Evacuated 0
Pipe Fac Name Imtt-Bayonne
Segment Name Bot 5803
Onshore State Abbreviation Nj
Onshore Postal Code 07002
Onshore City Name Bayonne
Onshore County Name Hudson
Designated Location Survey Station No.
Designated Name 5803
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Tank, Including Attached Appurtenances
Crossing No
Pipe Facility Type Interstate
Item Involved Tank/vessel
Tank Vessel Subtype Vent
Tank Type Atmospheric
Safe Fill Level 41.7
Safe Fill Level Exceeded Ind Yes
Api Std Out Of Service Year 2023
Api Std No In Service Ind Yes
Installation Year 1922
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Overfill Or Overflow
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment Yes
Remediation Ind Yes
Groundwater Remed Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 40000
Est Cost Prop Damage 0
Est Cost Emergency 5000
Est Cost Environmental 175000
Est Cost Other 5000
Est Cost Other Details Contractor Fees To Inspect Internal Floating Roof.
Prpty 225000
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 90
Pressure Restriction Ind No
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Other Accident Cause
Cause Details Miscellaneous
Other Type Miscellaneous
Misc Details An Incorrect Strapping Chart For The Breakout Tank (5803) Was In Use By The Imtt Inventory Control Software Program.
Preparer Name R***** M**********
Preparer Email R****************@i***.com
Preparer Telephone 2018235334
Prepared Date 2024-10-10 00:00:00
Local Contact Name R***** M**********
Local Contact Email R****************@i***.com
Local Contact Telephone 2018235334
Authorizer Name R*** A*******
Authorizer Telephone 2014372200
Authorizer Title Director Of Operations
Authorizer Email R***********@i***.com
Narrative 8**************************************************************************@ approx1825 the hi level alarm(hla) for 5803 signaled a hi alarm. The vessel was shut down, imtt field personnel obtained a gauge on the tank, according to the figures the level was 3,000bbls from safe fill. Once that was determined, the vessel was restarted. Imtt field personnel were on top of the tank monitoring the level until the safe fill was to be reached. Within 10 minutes of the restart, imtt field personnel observed product spilling from a side vent, the vessel was immediately shut down and the tank valves were secured. The level of the product was lowered and transferred to another tank. Imtt immediately initiated an emergency response. It is estimated that 321 bbls released through the overflow vent, approx. 40 bbls were recovered and disposed. After completion of the investigation, imtt determined third party contractor that calculated the safe fill for 5803, used the wrong calculations. ********************************************************************************************************************************.

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