Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2023-08-29 — TX
Operator
Phillips 66 Pipeline Llc
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$50,000
Incident datetime
2023-08-29 00:00 UTC
Report number
Location
TX
Narrative
During routine operator rounds, a company employee noticed product around an air to soil transition on a relief line. The employee immediately began notifying supervisory and regulatory personnel, while also initiating emergency response activities. The relief line was isolated and routed to a different tank, as the line was not active at the time of the release. The product release migrated off site to a nearby drainage ditch via culvert and was contained by operator personnel by use of an earthen dam in the ditch. All product and affected soil were remediated/removed via vacuum truck and/or roll off box. The release was due to a hole on the underground portion of the piping downstream of the air to soil transition. After laboratory analysis, report received 11/15/2023, it was determined that the release was due to internal corrosion from sludge and water drop out in the product. The remainder of the line was inspected, and no further issues were found.
Detailed record list
Report Received Date
2023-08-29 00:00:00
Iyear
2023
Report Number
20230197
Supplemental Number
38798
Report Type
Supplemental Final
Operator Id
31684
Name
Phillips 66 Pipeline Llc
Operator Street Address
2331 Citywest Blvd
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77042
Time Zone
Central
Daylight Savings Ind
No
Location Latitude
29.988186
Location Longitude
-93.987212
Commodity Released Type
Crude Oil
Unintentional Release Bbls
13
Recovered Bbls
13
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
No
Shutdown Explain
Relief Was Isolated And Routed To Another Tank In The Tank Farm.
Communication State Fed Ind
No
Nrc Rpt Num
1374819
Additional Nrc Report Numbers
1374999
Ignite Ind
No
Notify Qualified Indiv Ind
Yes
Oil Spill Removal Org Ind
Yes
Osro Arrived On Site Dt
7/31/2023 20:00
Num Pub Evacuated
0
Pipe Fac Name
P66 Beaumont Terminal
Segment Name
Seaway Relief Line
Onshore State Abbreviation
Tx
Onshore Postal Code
77627
Onshore City Name
Nederland
Onshore County Name
Jefferson
Designated Location
Milepost
Designated Name
Seaway Relief
Federal
No
Location Type
Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type
Transition Area
Incident Area Subtype
Soil/air Interface
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Relief Line And Relief Equipment
Installation Year
2014
Manufactured Year
2014
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
1040
Est Cost Prop Damage
50000
Est Cost Emergency
95000
Est Cost Environmental
75000
Est Cost Other
0
Prpty
221040
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
13
Mop Psig
285
Mop Cfr Section
Subpart E Pressure Test �195.406(A)(3)
Maop Established Date
2014-05-21 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Other Corrosion Ind
Yes
Int Corrosion Type Details
Unknown At This Time. Waiting For Lab Analysis.
Int Field Exam Basis Ind
Yes
Int Metallurgical Basis Ind
Yes
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
No
Corrosion Lining
No
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
Not Applicable - Not Mainline Pipe
Preparer Name
M****** B*********
Preparer Email
M*******************@p**.com
Preparer Telephone
7134122371
Prepared Date
2023-11-15 00:00:00
Local Contact Name
M****** B*********
Local Contact Email
M*******************@p**.com
Local Contact Telephone
7134122371
Authorizer Name
T*** F****
Authorizer Telephone
8327651632
Authorizer Title
Director Of Dot Compliance
Authorizer Email
T***********@p**.com
Narrative
During routine operator rounds, a company employee noticed product around an air to soil transition on a relief line. The employee immediately began notifying supervisory and regulatory personnel, while also initiating emergency response activities. The relief line was isolated and routed to a different tank, as the line was not active at the time of the release. The product release migrated off site to a nearby drainage ditch via culvert and was contained by operator personnel by use of an earthen dam in the ditch. All product and affected soil were remediated/removed via vacuum truck and/or roll off box. The release was due to a hole on the underground portion of the piping downstream of the air to soil transition. After laboratory analysis, report received 11/15/2023, it was determined that the release was due to internal corrosion from sludge and water drop out in the product. The remainder of the line was inspected, and no further issues were found.
Report Received Date | 2023-08-29 00:00:00 |
---|---|
Iyear | 2023 |
Report Number | 20230197 |
Supplemental Number | 38798 |
Report Type | Supplemental Final |
Operator Id | 31684 PHMSA Enforcement |
Name | Phillips 66 Pipeline Llc |
Operator Street Address | 2331 Citywest Blvd |
Operator City Name | Houston |
Operator State Abbreviation | TX |
Operator Postal Code | 77042 |
Time Zone | Central |
Daylight Savings Ind | No |
Location Latitude | 29.988186 Google Maps OpenStreetMap |
Location Longitude | -93.987212 Google Maps OpenStreetMap |
Commodity Released Type | Crude Oil |
Unintentional Release Bbls | 13 |
Recovered Bbls | 13 |
Fatality Ind | No |
Fatal | 0 |
Injury Ind | No |
Injure | 0 |
Accident Identifier | Local Operating Personnel, Including Contractors |
Operator Type | Operator Employee |
System Part Involved | Onshore Terminal/tank Farm Equipment And Piping |
On Off Shore | Onshore |
Status When Identified | Normal Operation, Includes Pauses Between Batches And During Maintenance |
Shutdown Due Accident Ind | No |
Shutdown Explain | Relief Was Isolated And Routed To Another Tank In The Tank Farm. |
Communication State Fed Ind | No |
Nrc Rpt Num | 1374819 NRC Report How to search |
Additional Nrc Report Numbers | 1374999 |
Ignite Ind | No |
Notify Qualified Indiv Ind | Yes |
Oil Spill Removal Org Ind | Yes |
Osro Arrived On Site Dt | 7/31/2023 20:00 |
Num Pub Evacuated | 0 |
Pipe Fac Name | P66 Beaumont Terminal |
Segment Name | Seaway Relief Line |
Onshore State Abbreviation | Tx |
Onshore Postal Code | 77627 |
Onshore City Name | Nederland |
Onshore County Name | Jefferson |
Designated Location | Milepost |
Designated Name | Seaway Relief |
Federal | No |
Location Type | Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property |
Incident Area Type | Transition Area |
Incident Area Subtype | Soil/air Interface |
Crossing | No |
Pipe Facility Type | Interstate |
Item Involved | Relief Line And Relief Equipment |
Installation Year | 2014 |
Manufactured Year | 2014 |
Material Involved | Carbon Steel |
Release Type | Leak |
Leak Type | Pinhole |
Wildlife Impact Ind | No |
Soil Contamination | No |
Long Term Assessment | No |
Remediation Ind | No |
Water Contam Ind | No |
Could Be Hca | Yes |
Commodity Reached Hca | Yes |
High Pop Ind | Yes |
High Pop Yes No | Yes |
Usa Drinking Ind | Yes |
Usa Drinking Yes No | Yes |
Est Cost Oper Paid | 0 |
Est Cost Gas Released | 1040 |
Est Cost Prop Damage | 50000 |
Est Cost Emergency | 95000 |
Est Cost Environmental | 75000 |
Est Cost Other | 0 |
Prpty | 221040 |
Num Persons Hosp Not Ovnght | 0 |
Num Injured Treated By Emt | 0 |
Num Resident Building Affctd | 0 |
Num Business Building Affctd | 0 |
Accident Psig | 13 |
Mop Psig | 285 |
Mop Cfr Section | Subpart E Pressure Test �195.406(A)(3) View CFR 49 §192 |
Maop Established Date | 2014-05-21 00:00:00 |
Maop Reversal Flow Ind | No |
Accident Pressure | Pressure Did Not Exceed Mop |
Pressure Restriction Ind | No |
Pipeline Function | < 20% Smys Regulated Transmission |
Scada In Place Ind | No |
Cpm In Place Ind | No |
Investigation Status | No, the facility was not monitored by a controller(s) at the time of the accident |
Employee Drug Test Ind | No |
Contractor Drug Test Ind | No |
Cause | Corrosion Failure |
Cause Details | Internal Corrosion |
Internal External | Internal Corrosion |
Int Visual Exam Results | Localized Pitting |
Int Other Corrosion Ind | Yes |
Int Corrosion Type Details | Unknown At This Time. Waiting For Lab Analysis. |
Int Field Exam Basis Ind | Yes |
Int Metallurgical Basis Ind | Yes |
Int Low Point Pipe Loc Ind | Yes |
Corrosion Inhibitors | No |
Corrosion Lining | No |
Cleaning Dewatering | Not Applicable - Not Mainline Pipe |
Corrosion Coupons | Not Applicable - Not Mainline Pipe |
Preparer Name | M****** B********* |
Preparer Email | M*******************@p**.com |
Preparer Telephone | 7134122371 |
Prepared Date | 2023-11-15 00:00:00 |
Local Contact Name | M****** B********* |
Local Contact Email | M*******************@p**.com |
Local Contact Telephone | 7134122371 |
Authorizer Name | T*** F**** |
Authorizer Telephone | 8327651632 |
Authorizer Title | Director Of Dot Compliance |
Authorizer Email | T***********@p**.com |
Narrative | During routine operator rounds, a company employee noticed product around an air to soil transition on a relief line. The employee immediately began notifying supervisory and regulatory personnel, while also initiating emergency response activities. The relief line was isolated and routed to a different tank, as the line was not active at the time of the release. The product release migrated off site to a nearby drainage ditch via culvert and was contained by operator personnel by use of an earthen dam in the ditch. All product and affected soil were remediated/removed via vacuum truck and/or roll off box. The release was due to a hole on the underground portion of the piping downstream of the air to soil transition. After laboratory analysis, report received 11/15/2023, it was determined that the release was due to internal corrosion from sludge and water drop out in the product. The remainder of the line was inspected, and no further issues were found. |
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