HL incident on 2023-08-25 — TX

Operator
Nustar Pipeline Operating Partnership L.p.
Cause
Material Failure Of Pipe Or Weld
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$108,800
Incident datetime
2023-08-25 00:00 UTC
Report number
Location
TX
Narrative
At 11:13 edc personnel notified nustar of a possible ammonia leak bubbling up under their retention pond. The pipeline was already shut down due to a planned hydrotest from peace valley, ar to salem, mo. Local personnel arrived on-site at 11:48 and confirmed a leak, isolated the pipeline by closing manual valves and verified that an mov (23-4) was closed. In that area there is around 741 feet between manual valves with an estimated 2500 pounds that was released during the event. No vapor cloud present as it was being released into the retention pond. The retention pond is used by edc to hold their process wastewater. Metallurgical analysis concluded, "the failure was the result of selective seam weld corrosion (sswc). Multiple weld defects, including lack of fusion (lof), were observed at the inner diameter (id).
Detailed record list
Report Received Date
2023-08-25 00:00:00
Iyear
2023
Report Number
20230194
Supplemental Number
38964
Report Type
Supplemental Final
Operator Id
Name
Nustar Pipeline Operating Partnership L.p.
Operator Street Address
8111 Westchester Drive
Operator City Name
Dallas
Operator State Abbreviation
TX
Operator Postal Code
75225
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Anhydrous Ammonia
Unintentional Release Bbls
11.57
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Status When Identified
Routine Shutdown
Communication State Fed Ind
No
Nrc Rpt Num
Additional Nrc Report Numbers
1374596
Ignite Ind
No
Upstream Action Taken
Valve Closure
Upstream Valve Type Ind
Manual
Downstream Action Taken
Valve Closure
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Ammonia Mainline
Segment Name
El Dorado Chemical Lateral - 4-Inch
Onshore State Abbreviation
Ar
Onshore Postal Code
71730
Onshore City Name
El Dorado
Onshore County Name
Union
Designated Location
Survey Station No.
Designated Name
685+51
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Other
Incident Area Details
Under Soil And Under A Retention Pond
Depth Of Cover
20
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Seam
Pipe Diameter
4.5
Pipe Wall Thickness
0.188
Pipe Smys
35000
Pipe Specification
Api 5l-B
Pipe Seam Type
Erw - High Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
Fusion Bonded Epoxy(Fbe)
Coating Applied Ind
No
Installation Year
1969
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
Crack Like Feature-Tbd
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
Yes
Surface Contam Ind
Yes
Amount Released
11.57
Rel Water Name
El Dorado Chemical Retention Pond
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
338
Est Cost Prop Damage
108800
Est Cost Emergency
0
Est Cost Environmental
33000
Est Cost Other
0
Prpty
142138
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
673
Mop Psig
1340
Mop Cfr Section
Component Design Pressure �195.406(A)(2)
Maop Established Date
1969-07-31 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
741
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Very small pin hole leak undiscoverable by control center.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Field Exam Ind
Yes
Metallurgical Ind
Yes
Failure Type
Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Other Factor
Yes
Other Factor Details
Angled Orientation Of The Seam Weld Bond Line Influenced The Weld Grain Flow
Additional Lack Fusion Ind
Yes
Pwf Additional Other Ind
Yes
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Geometry Deformation Ind
Yes
Axial Recent Year
2018
Axial Rcnt Propul Method
Free Swimming
Axial Rcnt Attuned Detect
Metal Loss
Axial Rcnt Atnd Dtct Metal
Standard Resolution
Axial Previous Year
2013
Axial Prev Propul Method
Free Swimming
Axial Prev Attuned Detect
Metal Loss
Axial Prev Atnd Dtct Metal
Standard Resolution
Geometry Recent Year
2018
Geometry Rcnt Propul Method
Free Swimming
Geometry Rcnt Resolution
Standard Resolution
Geometrt Rcnt Measur Cups
No Cups
Geometry Previous Year
2013
Geometry Prev Propul Method
Free Swimming
Geometry Prev Resolution
Standard Resolution
Geometrt Prev Measur Cups
No Cups
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Extrnl Cor Selective Seam Ind
Yes
Preparer Name
D***** T******
Preparer Title
Director - Hse
Preparer Email
D**********@n***********.com
Preparer Telephone
3167217056
Prepared Date
2023-12-14 00:00:00
Local Contact Name
A**** G***
Local Contact Email
A*********@n***********.com
Local Contact Telephone
5732808181
Authorizer Name
D***** T******
Authorizer Telephone
3167217056
Authorizer Title
Director - Hse
Authorizer Email
D**********@n***********.com
Narrative
At 11:13 edc personnel notified nustar of a possible ammonia leak bubbling up under their retention pond. The pipeline was already shut down due to a planned hydrotest from peace valley, ar to salem, mo. Local personnel arrived on-site at 11:48 and confirmed a leak, isolated the pipeline by closing manual valves and verified that an mov (23-4) was closed. In that area there is around 741 feet between manual valves with an estimated 2500 pounds that was released during the event. No vapor cloud present as it was being released into the retention pond. The retention pond is used by edc to hold their process wastewater. Metallurgical analysis concluded, "the failure was the result of selective seam weld corrosion (sswc). Multiple weld defects, including lack of fusion (lof), were observed at the inner diameter (id).
Report Received Date 2023-08-25 00:00:00
Iyear 2023
Report Number 20230194
Supplemental Number 38964
Report Type Supplemental Final
Operator Id 10012 PHMSA Enforcement
Name Nustar Pipeline Operating Partnership L.p.
Operator Street Address 8111 Westchester Drive
Operator City Name Dallas
Operator State Abbreviation TX
Operator Postal Code 75225
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 33.263307 Google Maps OpenStreetMap
Location Longitude -92.689986 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Anhydrous Ammonia
Unintentional Release Bbls 11.57
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Status When Identified Routine Shutdown
Communication State Fed Ind No
Nrc Rpt Num 1374395 NRC Report How to search
Additional Nrc Report Numbers 1374596
Ignite Ind No
Upstream Action Taken Valve Closure
Upstream Valve Type Ind Manual
Downstream Action Taken Valve Closure
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Ammonia Mainline
Segment Name El Dorado Chemical Lateral - 4-Inch
Onshore State Abbreviation Ar
Onshore Postal Code 71730
Onshore City Name El Dorado
Onshore County Name Union
Designated Location Survey Station No.
Designated Name 685+51
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Other
Incident Area Details Under Soil And Under A Retention Pond
Depth Of Cover 20
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Seam
Pipe Diameter 4.5
Pipe Wall Thickness 0.188
Pipe Smys 35000
Pipe Specification Api 5l-B
Pipe Seam Type Erw - High Frequency
Pipe Manufacturer Unknown
Pipe Coating Type Fusion Bonded Epoxy(Fbe)
Coating Applied Ind No
Installation Year 1969
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Other
Leak Type Other Crack Like Feature-Tbd
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind Yes
Surface Contam Ind Yes
Amount Released 11.57
Rel Water Name El Dorado Chemical Retention Pond
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 338
Est Cost Prop Damage 108800
Est Cost Emergency 0
Est Cost Environmental 33000
Est Cost Other 0
Prpty 142138
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 673
Mop Psig 1340
Mop Cfr Section Component Design Pressure �195.406(A)(2) View CFR 49 §192
Maop Established Date 1969-07-31 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 741
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Very small pin hole leak undiscoverable by control center.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Material Failure Of Pipe Or Weld
Cause Details Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Field Exam Ind Yes
Metallurgical Ind Yes
Failure Type Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Other Factor Yes
Other Factor Details Angled Orientation Of The Seam Weld Bond Line Influenced The Weld Grain Flow
Additional Lack Fusion Ind Yes
Pwf Additional Other Ind Yes
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Geometry Deformation Ind Yes
Axial Recent Year 2018
Axial Rcnt Propul Method Free Swimming
Axial Rcnt Attuned Detect Metal Loss
Axial Rcnt Atnd Dtct Metal Standard Resolution
Axial Previous Year 2013
Axial Prev Propul Method Free Swimming
Axial Prev Attuned Detect Metal Loss
Axial Prev Atnd Dtct Metal Standard Resolution
Geometry Recent Year 2018
Geometry Rcnt Propul Method Free Swimming
Geometry Rcnt Resolution Standard Resolution
Geometrt Rcnt Measur Cups No Cups
Geometry Previous Year 2013
Geometry Prev Propul Method Free Swimming
Geometry Prev Resolution Standard Resolution
Geometrt Prev Measur Cups No Cups
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Extrnl Cor Selective Seam Ind Yes
Preparer Name D***** T******
Preparer Title Director - Hse
Preparer Email D**********@n***********.com
Preparer Telephone 3167217056
Prepared Date 2023-12-14 00:00:00
Local Contact Name A**** G***
Local Contact Email A*********@n***********.com
Local Contact Telephone 5732808181
Authorizer Name D***** T******
Authorizer Telephone 3167217056
Authorizer Title Director - Hse
Authorizer Email D**********@n***********.com
Narrative At 11:13 edc personnel notified nustar of a possible ammonia leak bubbling up under their retention pond. The pipeline was already shut down due to a planned hydrotest from peace valley, ar to salem, mo. Local personnel arrived on-site at 11:48 and confirmed a leak, isolated the pipeline by closing manual valves and verified that an mov (23-4) was closed. In that area there is around 741 feet between manual valves with an estimated 2500 pounds that was released during the event. No vapor cloud present as it was being released into the retention pond. The retention pond is used by edc to hold their process wastewater. Metallurgical analysis concluded, "the failure was the result of selective seam weld corrosion (sswc). Multiple weld defects, including lack of fusion (lof), were observed at the inner diameter (id).

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