HL incident on 2023-08-08 — OH

Operator
Marathon Pipe Line Llc
Cause
Incorrect Operation
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2023-08-08 00:00 UTC
Report number
Location
OH
Narrative
Incident occurred as part of a procedure to re-fill a segment of the system that was purged and repaired due to a fire (incident id# 20230179-38361). Field personnel began loosening a flange on a 2" blow down valve per procedure and the valve was not holding. This allowed propane to be introduced to the atmosphere in the form of vapor. The procedure did not specify to close/verify closed the 2" blown down, but it was closed because of an obvious need to do so for isolation, and it was determined that the valve was not fully closed/seated and remained 1/16 of an inch open. The procedure was halted and the valve was fully closed and re-packed before proceeding. Supplemental update. Cause has been adjusted to reflect new information that the procedure for this operation did not specify to close/verify closed the valve prior to removal of the blind. Supplemental update #2, the south halls bayou (mp16) block valve is located less than a foot downstream from the blow-down valve that in which the failure occurred. The mp16 valve was opened after isolating the segment in which the release was occurring from the upstream portion of the pipe. Isolation from the upstream segment was achieved by closure of the mp 15 north halls block valve. Opening the mp 16 block valve downstream allowed the product to flow into an empty section of pipe and reduced the pressure to a level that allowed for the injection of grease into the blowdown valve to stop the leak. This method was required due to the formation of ice in the blowdown valve preventing its operation.
Detailed record list
Report Received Date
2023-08-08 00:00:00
Iyear
2023
Report Number
20230181
Supplemental Number
38690
Report Type
Supplemental Final
Operator Id
Name
Marathon Pipe Line Llc
Operator Street Address
539 South Main Street
Operator City Name
Findlay
Operator State Abbreviation
OH
Operator Postal Code
45840
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Propane
Unintentional Release Bbls
0.2
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Status When Identified
Post-Maintenance/repair
Communication State Fed Ind
No
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Upstream Action Taken
Valve Closure
Upstream Valve Type Ind
Manual
Downstream Action Taken
Operational Control
Downstream Oprtnl Cntrl Detail
Just Downstream Of The Release, The Mp 16 South Halls Bayou Block Valve Was Opened.
Num Pub Evacuated
0
Pipe Fac Name
Galveston Bay To Chocolate Bayou 8" Lpg
Segment Name
Galveston Bay To Chocolate Bayou 8" Lpg
Onshore State Abbreviation
Tx
Onshore Postal Code
77511
Onshore City Name
Not Within A Municipality
Onshore County Name
Brazoria
Designated Location
Milepost
Designated Name
16.2
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
2017
Manufactured Year
2016
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
Valve Was Not Fully Seated. When Flange Was Loosened, Product Was Introduced To The Atmosphere.
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
5
Est Cost Prop Damage
0
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
5
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
862
Mop Psig
2160
Mop Cfr Section
Component Design Pressure �195.406(A)(2)
Maop Established Date
2016-01-01 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Controller actions had no impact on incident.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Operation Type
Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Related Inadequate Proc Ind
Yes
Category Type
Non-Routine Operating Conditions (Abnormal Operations Or Emergencies)
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
Z*** C*********
Preparer Title
Compliance Specialist
Preparer Email
Z***********@m****************.com
Preparer Telephone
4196726607
Prepared Date
2023-10-23 00:00:00
Authorizer Name
M****** G***
Authorizer Telephone
4194214505
Authorizer Title
Regulatory Compliance Manager
Authorizer Email
M*****@m****************.com
Narrative
Incident occurred as part of a procedure to re-fill a segment of the system that was purged and repaired due to a fire (incident id# 20230179-38361). Field personnel began loosening a flange on a 2" blow down valve per procedure and the valve was not holding. This allowed propane to be introduced to the atmosphere in the form of vapor. The procedure did not specify to close/verify closed the 2" blown down, but it was closed because of an obvious need to do so for isolation, and it was determined that the valve was not fully closed/seated and remained 1/16 of an inch open. The procedure was halted and the valve was fully closed and re-packed before proceeding. Supplemental update. Cause has been adjusted to reflect new information that the procedure for this operation did not specify to close/verify closed the valve prior to removal of the blind. Supplemental update #2, the south halls bayou (mp16) block valve is located less than a foot downstream from the blow-down valve that in which the failure occurred. The mp16 valve was opened after isolating the segment in which the release was occurring from the upstream portion of the pipe. Isolation from the upstream segment was achieved by closure of the mp 15 north halls block valve. Opening the mp 16 block valve downstream allowed the product to flow into an empty section of pipe and reduced the pressure to a level that allowed for the injection of grease into the blowdown valve to stop the leak. This method was required due to the formation of ice in the blowdown valve preventing its operation.
Report Received Date 2023-08-08 00:00:00
Iyear 2023
Report Number 20230181
Supplemental Number 38690
Report Type Supplemental Final
Operator Id 32147 PHMSA Enforcement
Name Marathon Pipe Line Llc
Operator Street Address 539 South Main Street
Operator City Name Findlay
Operator State Abbreviation OH
Operator Postal Code 45840
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 29.2671393 Google Maps OpenStreetMap
Location Longitude -95.1265417 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details Propane
Unintentional Release Bbls 0.2
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Status When Identified Post-Maintenance/repair
Communication State Fed Ind No
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Upstream Action Taken Valve Closure
Upstream Valve Type Ind Manual
Downstream Action Taken Operational Control
Downstream Oprtnl Cntrl Detail Just Downstream Of The Release, The Mp 16 South Halls Bayou Block Valve Was Opened.
Num Pub Evacuated 0
Pipe Fac Name Galveston Bay To Chocolate Bayou 8" Lpg
Segment Name Galveston Bay To Chocolate Bayou 8" Lpg
Onshore State Abbreviation Tx
Onshore Postal Code 77511
Onshore City Name Not Within A Municipality
Onshore County Name Brazoria
Designated Location Milepost
Designated Name 16.2
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year 2017
Manufactured Year 2016
Material Involved Carbon Steel
Release Type Other
Release Type Details Valve Was Not Fully Seated. When Flange Was Loosened, Product Was Introduced To The Atmosphere.
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 5
Est Cost Prop Damage 0
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 5
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 862
Mop Psig 2160
Mop Cfr Section Component Design Pressure �195.406(A)(2) View CFR 49 §192
Maop Established Date 2016-01-01 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Controller actions had no impact on incident.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Operation Type Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Related Inadequate Proc Ind Yes
Category Type Non-Routine Operating Conditions (Abnormal Operations Or Emergencies)
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name Z*** C*********
Preparer Title Compliance Specialist
Preparer Email Z***********@m****************.com
Preparer Telephone 4196726607
Prepared Date 2023-10-23 00:00:00
Authorizer Name M****** G***
Authorizer Telephone 4194214505
Authorizer Title Regulatory Compliance Manager
Authorizer Email M*****@m****************.com
Narrative Incident occurred as part of a procedure to re-fill a segment of the system that was purged and repaired due to a fire (incident id# 20230179-38361). Field personnel began loosening a flange on a 2" blow down valve per procedure and the valve was not holding. This allowed propane to be introduced to the atmosphere in the form of vapor. The procedure did not specify to close/verify closed the 2" blown down, but it was closed because of an obvious need to do so for isolation, and it was determined that the valve was not fully closed/seated and remained 1/16 of an inch open. The procedure was halted and the valve was fully closed and re-packed before proceeding. Supplemental update. Cause has been adjusted to reflect new information that the procedure for this operation did not specify to close/verify closed the valve prior to removal of the blind. Supplemental update #2, the south halls bayou (mp16) block valve is located less than a foot downstream from the blow-down valve that in which the failure occurred. The mp16 valve was opened after isolating the segment in which the release was occurring from the upstream portion of the pipe. Isolation from the upstream segment was achieved by closure of the mp 15 north halls block valve. Opening the mp 16 block valve downstream allowed the product to flow into an empty section of pipe and reduced the pressure to a level that allowed for the injection of grease into the blowdown valve to stop the leak. This method was required due to the formation of ice in the blowdown valve preventing its operation.

All rights reserved. Copyright © by ClearPHMSA