HL incident on 2023-08-04 — TX

Operator
Mid - Valley Pipeline Co
Cause
Material Failure Of Pipe Or Weld
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$155,000
Incident datetime
2023-08-04 00:00 UTC
Report number
Location
TX
Narrative
On 7/5/23 at approximately 16:18 et the control center received a line imbalance alarm and began shutting the pipeline down. Investigation into the alarm began while the line was setup for a static pressure test to confirm integrity. Aerial patrol was initiated, and the static test was completed with no indication of a release. The line imbalance was believed to be due to a measurement issue. The line was cleared for restart at approximately 21:04. At approximately 22:00 aerial patrol identified a stain on row north of cygnet. Line was shutdown again at approximately 22:04. Approximately 2 barrels of crude oil released to the soil. Oil spill response contractors were mobilized to cleanup released product. A plidco clamp was installed on 7/6/23 and the line was restarted on 7/7/23. After ili assessment the failed section will be cut out and replaced. The failed section will be analyzed for cause and a supplemental report will be filed. Supplemental: the failed section of pipe was cut out and replaced in january 2024. The failed section was sent for metallurgical analysis. The cause of the failure was determined by metallurgical analysis to be a leak located at a colony of axially oriented, interlinked near neutral ph stress corrosion cracks that were located at an area of externa corrosion and a dent. An ultrasonic crack tool ili assessment was conducted in december 2023. Tool data will be reviewed for similar issues once received and remedial measures taken accordingly.
Detailed record list
Report Received Date
2023-08-04 00:00:00
Iyear
2023
Report Number
20230178
Supplemental Number
39337
Report Type
Supplemental Final
Operator Id
Name
Mid - Valley Pipeline Co
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Time Zone
Eastern
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
2
Recovered Bbls
2
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Or Pack Calculations)
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Nrc Rpt Num
Additional Nrc Report Numbers
1372326
Ignite Ind
No
Upstream Action Taken
Valve Closure
Upstream Valve Type Ind
Remotely Controlled
Downstream Action Taken
Valve Closure
Downstream Valve Type Ind
Manual
Notify Qualified Indiv Ind
Yes
Oil Spill Removal Org Ind
Yes
Osro Arrived On Site Dt
7/5/2023 23:30
Num Pub Evacuated
0
Pipe Fac Name
Mid Valley Pipeline
Segment Name
28003.02 Cygnet To Samaria 22-Inch
Onshore State Abbreviation
Oh
Onshore Postal Code
43413
Onshore City Name
Cygnet
Onshore County Name
Wood
Designated Location
Milepost
Designated Name
51
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
42
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Puddle Weld Ind
No
Pipe Diameter
22
Pipe Wall Thickness
0.344
Pipe Smys
35000
Pipe Specification
Grade B
Pipe Seam Type
Seamless
Pipe Manufacturer
Unknown
Pipe Coating Type
Asphalt
Coating Applied Ind
Unknown
Installation Year
1949
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Crack
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
25000
Est Cost Gas Released
150
Est Cost Prop Damage
155000
Est Cost Emergency
200000
Est Cost Environmental
29000
Est Cost Other
2055
Est Cost Other Details
Aerial Patrol To Locate Release
Prpty
411205
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
200
Mop Psig
788
Mop Cfr Section
Internal Design Pressure �195.406(A)(1)
Maop Established Date
1969-04-23 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
5450
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
Yes
Cpm Conf Ind
Yes
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Environmental Cracking-Related
Metallurgical Ind
Yes
Failure Type
Environmental Cracking-Related
Stress Subtype
Stress Corrosion Cracking
Additional Dent Ind
Yes
Pwf Additional Other Ind
Yes
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Ultrasonic Ind
Yes
Geometry Deformation Ind
Yes
Axial Recent Year
2018
Axial Rcnt Propul Method
Free Swimming
Axial Rcnt Attuned Detect
Metal Loss
Axial Rcnt Atnd Dtct Metal
High Resolution
Axial Previous Year
2014
Axial Prev Propul Method
Free Swimming
Axial Prev Attuned Detect
Metal Loss
Axial Prev Atnd Dtct Metal
High Resolution
Ultrasonic Recent Year
2016
Ultrasonic Rcnt Propul Method
Free Swimming
Ultrasonic Rcnt Attuned
Crack
Geometry Recent Year
2018
Geometry Rcnt Propul Method
Free Swimming
Geometry Rcnt Resolution
High Resolution
Geometrt Rcnt Measur Cups
No Cups
Geometry Previous Year
2014
Geometry Prev Propul Method
Free Swimming
Geometry Prev Resolution
High Resolution
Geometrt Prev Measur Cups
No Cups
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
1969
Hydrtst Most Rcnt Pressure
994
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Extrnl Cor Galvanic Ind
Yes
Preparer Name
T*** N*******
Preparer Title
Director - Dot Compliance
Preparer Email
T************@e*************.com
Preparer Telephone
713-989-7126
Prepared Date
2024-03-18 00:00:00
Authorizer Name
T*** N*******
Authorizer Telephone
713-989-7126
Authorizer Title
Director - Dot Compliance
Authorizer Email
T************@e*************.com
Narrative
On 7/5/23 at approximately 16:18 et the control center received a line imbalance alarm and began shutting the pipeline down. Investigation into the alarm began while the line was setup for a static pressure test to confirm integrity. Aerial patrol was initiated, and the static test was completed with no indication of a release. The line imbalance was believed to be due to a measurement issue. The line was cleared for restart at approximately 21:04. At approximately 22:00 aerial patrol identified a stain on row north of cygnet. Line was shutdown again at approximately 22:04. Approximately 2 barrels of crude oil released to the soil. Oil spill response contractors were mobilized to cleanup released product. A plidco clamp was installed on 7/6/23 and the line was restarted on 7/7/23. After ili assessment the failed section will be cut out and replaced. The failed section will be analyzed for cause and a supplemental report will be filed. Supplemental: the failed section of pipe was cut out and replaced in january 2024. The failed section was sent for metallurgical analysis. The cause of the failure was determined by metallurgical analysis to be a leak located at a colony of axially oriented, interlinked near neutral ph stress corrosion cracks that were located at an area of externa corrosion and a dent. An ultrasonic crack tool ili assessment was conducted in december 2023. Tool data will be reviewed for similar issues once received and remedial measures taken accordingly.
Report Received Date 2023-08-04 00:00:00
Iyear 2023
Report Number 20230178
Supplemental Number 39337
Report Type Supplemental Final
Operator Id 12470 PHMSA Enforcement
Name Mid - Valley Pipeline Co
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Time Zone Eastern
Daylight Savings Ind Yes
Location Latitude 41.29919 Google Maps OpenStreetMap
Location Longitude -83.61619 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 2
Recovered Bbls 2
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Or Pack Calculations)
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind Yes
Communication State Fed Ind Yes
Party Initiated Communication Operator
Nrc Rpt Num 1372213 NRC Report How to search
Additional Nrc Report Numbers 1372326
Ignite Ind No
Upstream Action Taken Valve Closure
Upstream Valve Type Ind Remotely Controlled
Downstream Action Taken Valve Closure
Downstream Valve Type Ind Manual
Notify Qualified Indiv Ind Yes
Oil Spill Removal Org Ind Yes
Osro Arrived On Site Dt 7/5/2023 23:30
Num Pub Evacuated 0
Pipe Fac Name Mid Valley Pipeline
Segment Name 28003.02 Cygnet To Samaria 22-Inch
Onshore State Abbreviation Oh
Onshore Postal Code 43413
Onshore City Name Cygnet
Onshore County Name Wood
Designated Location Milepost
Designated Name 51
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 42
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Puddle Weld Ind No
Pipe Diameter 22
Pipe Wall Thickness 0.344
Pipe Smys 35000
Pipe Specification Grade B
Pipe Seam Type Seamless
Pipe Manufacturer Unknown
Pipe Coating Type Asphalt
Coating Applied Ind Unknown
Installation Year 1949
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Crack
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 25000
Est Cost Gas Released 150
Est Cost Prop Damage 155000
Est Cost Emergency 200000
Est Cost Environmental 29000
Est Cost Other 2055
Est Cost Other Details Aerial Patrol To Locate Release
Prpty 411205
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 200
Mop Psig 788
Mop Cfr Section Internal Design Pressure �195.406(A)(1) View CFR 49 §192
Maop Established Date 1969-04-23 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 5450
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind Yes
Cpm Conf Ind Yes
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Material Failure Of Pipe Or Weld
Cause Details Environmental Cracking-Related
Metallurgical Ind Yes
Failure Type Environmental Cracking-Related
Stress Subtype Stress Corrosion Cracking
Additional Dent Ind Yes
Pwf Additional Other Ind Yes
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Ultrasonic Ind Yes
Geometry Deformation Ind Yes
Axial Recent Year 2018
Axial Rcnt Propul Method Free Swimming
Axial Rcnt Attuned Detect Metal Loss
Axial Rcnt Atnd Dtct Metal High Resolution
Axial Previous Year 2014
Axial Prev Propul Method Free Swimming
Axial Prev Attuned Detect Metal Loss
Axial Prev Atnd Dtct Metal High Resolution
Ultrasonic Recent Year 2016
Ultrasonic Rcnt Propul Method Free Swimming
Ultrasonic Rcnt Attuned Crack
Geometry Recent Year 2018
Geometry Rcnt Propul Method Free Swimming
Geometry Rcnt Resolution High Resolution
Geometrt Rcnt Measur Cups No Cups
Geometry Previous Year 2014
Geometry Prev Propul Method Free Swimming
Geometry Prev Resolution High Resolution
Geometrt Prev Measur Cups No Cups
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 1969
Hydrtst Most Rcnt Pressure 994
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Extrnl Cor Galvanic Ind Yes
Preparer Name T*** N*******
Preparer Title Director - Dot Compliance
Preparer Email T************@e*************.com
Preparer Telephone 713-989-7126
Prepared Date 2024-03-18 00:00:00
Authorizer Name T*** N*******
Authorizer Telephone 713-989-7126
Authorizer Title Director - Dot Compliance
Authorizer Email T************@e*************.com
Narrative On 7/5/23 at approximately 16:18 et the control center received a line imbalance alarm and began shutting the pipeline down. Investigation into the alarm began while the line was setup for a static pressure test to confirm integrity. Aerial patrol was initiated, and the static test was completed with no indication of a release. The line imbalance was believed to be due to a measurement issue. The line was cleared for restart at approximately 21:04. At approximately 22:00 aerial patrol identified a stain on row north of cygnet. Line was shutdown again at approximately 22:04. Approximately 2 barrels of crude oil released to the soil. Oil spill response contractors were mobilized to cleanup released product. A plidco clamp was installed on 7/6/23 and the line was restarted on 7/7/23. After ili assessment the failed section will be cut out and replaced. The failed section will be analyzed for cause and a supplemental report will be filed. Supplemental: the failed section of pipe was cut out and replaced in january 2024. The failed section was sent for metallurgical analysis. The cause of the failure was determined by metallurgical analysis to be a leak located at a colony of axially oriented, interlinked near neutral ph stress corrosion cracks that were located at an area of externa corrosion and a dent. An ultrasonic crack tool ili assessment was conducted in december 2023. Tool data will be reviewed for similar issues once received and remedial measures taken accordingly.

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