Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2023-07-20 — WY
Operator
Bridger Pipeline Llc
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$36,754
Incident datetime
2023-07-20 00:00 UTC
Report number
Location
WY
Narrative
On june 21, 2023 at approximately 09:28 a.M. Mdt, a bridger employee was performing a station check at the iberlin station, which was not operating at the time due to a loss of communications between it and the control center, when he discovered a pump seal had failed and released approximately 25 barrels of diesel inside of the pump building. The employee promptly called the area supervisor to report the release. The area supervisor subsequently contacted operations management to inform them of the release. A local vac truck company was then contacted and a vac truck was dispatched to the location to assist with the recovery of the released product. Once the vac truck arrived all released product was recovered and disposed of in accordance with wyoming deq requirements. After all of the released product was recovered, bpl employees examined the pump seal and determined it had failed due to high temperature. Taking this into consideration, it was decided to replace both the seal and pump. After the pump and seal were replaced, employees corrected the communications issue and the station was placed back into service. Further review of the incident revealed that a configuration in the plc logic allowed the pump to try and restart multiple times under low suction pressure which created a dry run/cavitation situation causing high temperatures and subsequent failure of the seal. The plc logic has subsequently been modified to mitigate the possibility of a dry run/cavitation situation. No wildlife, surface water, ground water or soils were impacted or contaminated as all released product was contained inside of the pump building. As mentioned above, all of the released product was recovered and was properly disposed of in accordance with wyoming deq requirements. Since the release did meet wyoming state deq reporting requirements, they were contacted and advised of the release. The release, however, did not meet national response center telephonic reporting requirements; therefore, no call was made to the nrc.
Detailed record list
Report Received Date
2023-07-20 00:00:00
Iyear
2023
Report Number
20230164
Supplemental Number
38504
Report Type
Supplemental Final
Operator Id
31878
Name
Bridger Pipeline Llc
Operator Street Address
455 N. Poplar St.
Operator City Name
Casper
Operator State Abbreviation
WY
Operator Postal Code
82602
Time Zone
Mountain
Daylight Savings Ind
Yes
Location Latitude
44.00288
Location Longitude
-105.97574
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
25
Recovered Bbls
25
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Status When Identified
Idle
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Notify Qualified Indiv Ind
Yes
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Iberlin Pump Station
Segment Name
Iberlin To Davis
Onshore State Abbreviation
Wy
Onshore Postal Code
82718
Onshore City Name
Not Within A Municipality
Onshore County Name
Campbell
Designated Location
Survey Station No.
Designated Name
0+00
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Inside A Building
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pump
Pump Type
Centrifugal
Pump Service Type
Mainline
Installation Year
2017
Manufactured Year
2017
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
3500
Est Cost Prop Damage
36754
Est Cost Emergency
2375
Est Cost Environmental
0
Est Cost Other
0
Prpty
42629
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
721
Mop Psig
1200
Mop Cfr Section
Subpart E Pressure Test �195.406(A)(3)
Maop Established Date
1997-09-09 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
No
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
No
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Pump Or Pump-Related Equipment
Eq Failure Type
Pump Or Pump-Related Equipment
Other Pump Ind
Seal/packing Failure
Additional Thermal Ind
Yes
Preparer Name
D*** T******
Preparer Title
Compliance Coordinator
Preparer Email
D***********@t******.com
Preparer Telephone
307-266-0320
Prepared Date
2023-09-05 00:00:00
Authorizer Name
K** D*********
Authorizer Telephone
307-266-0275
Authorizer Title
Director - Government And Control Center
Authorizer Email
K*************@t******.com
Narrative
On june 21, 2023 at approximately 09:28 a.M. Mdt, a bridger employee was performing a station check at the iberlin station, which was not operating at the time due to a loss of communications between it and the control center, when he discovered a pump seal had failed and released approximately 25 barrels of diesel inside of the pump building. The employee promptly called the area supervisor to report the release. The area supervisor subsequently contacted operations management to inform them of the release. A local vac truck company was then contacted and a vac truck was dispatched to the location to assist with the recovery of the released product. Once the vac truck arrived all released product was recovered and disposed of in accordance with wyoming deq requirements. After all of the released product was recovered, bpl employees examined the pump seal and determined it had failed due to high temperature. Taking this into consideration, it was decided to replace both the seal and pump. After the pump and seal were replaced, employees corrected the communications issue and the station was placed back into service. Further review of the incident revealed that a configuration in the plc logic allowed the pump to try and restart multiple times under low suction pressure which created a dry run/cavitation situation causing high temperatures and subsequent failure of the seal. The plc logic has subsequently been modified to mitigate the possibility of a dry run/cavitation situation. No wildlife, surface water, ground water or soils were impacted or contaminated as all released product was contained inside of the pump building. As mentioned above, all of the released product was recovered and was properly disposed of in accordance with wyoming deq requirements. Since the release did meet wyoming state deq reporting requirements, they were contacted and advised of the release. The release, however, did not meet national response center telephonic reporting requirements; therefore, no call was made to the nrc.
Report Received Date | 2023-07-20 00:00:00 |
---|---|
Iyear | 2023 |
Report Number | 20230164 |
Supplemental Number | 38504 |
Report Type | Supplemental Final |
Operator Id | 31878 PHMSA Enforcement |
Name | Bridger Pipeline Llc |
Operator Street Address | 455 N. Poplar St. |
Operator City Name | Casper |
Operator State Abbreviation | WY |
Operator Postal Code | 82602 |
Time Zone | Mountain |
Daylight Savings Ind | Yes |
Location Latitude | 44.00288 Google Maps OpenStreetMap |
Location Longitude | -105.97574 Google Maps OpenStreetMap |
Commodity Released Type | Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions |
Commodity Subtype | Diesel, Fuel Oil, Kerosene, Jet Fuel |
Unintentional Release Bbls | 25 |
Recovered Bbls | 25 |
Fatality Ind | No |
Fatal | 0 |
Injury Ind | No |
Injure | 0 |
Accident Identifier | Local Operating Personnel, Including Contractors |
Operator Type | Operator Employee |
System Part Involved | Onshore Pump/meter Station Equipment And Piping |
On Off Shore | Onshore |
Status When Identified | Idle |
Communication State Fed Ind | Yes |
Party Initiated Communication | Operator |
Nrc Rpt Num | Nrc Notification Not Required NRC Report How to search |
Ignite Ind | No |
Notify Qualified Indiv Ind | Yes |
Oil Spill Removal Org Ind | No |
Num Pub Evacuated | 0 |
Pipe Fac Name | Iberlin Pump Station |
Segment Name | Iberlin To Davis |
Onshore State Abbreviation | Wy |
Onshore Postal Code | 82718 |
Onshore City Name | Not Within A Municipality |
Onshore County Name | Campbell |
Designated Location | Survey Station No. |
Designated Name | 0+00 |
Federal | No |
Location Type | Totally Contained On Operator-Controlled Property |
Incident Area Type | Aboveground |
Incident Area Subtype | Inside A Building |
Crossing | No |
Pipe Facility Type | Interstate |
Item Involved | Pump |
Pump Type | Centrifugal |
Pump Service Type | Mainline |
Installation Year | 2017 |
Manufactured Year | 2017 |
Material Involved | Carbon Steel |
Release Type | Leak |
Leak Type | Seal Or Packing |
Wildlife Impact Ind | No |
Soil Contamination | No |
Long Term Assessment | No |
Remediation Ind | No |
Water Contam Ind | No |
Could Be Hca | No |
Commodity Reached Hca | No |
Est Cost Oper Paid | 0 |
Est Cost Gas Released | 3500 |
Est Cost Prop Damage | 36754 |
Est Cost Emergency | 2375 |
Est Cost Environmental | 0 |
Est Cost Other | 0 |
Prpty | 42629 |
Num Persons Hosp Not Ovnght | 0 |
Num Injured Treated By Emt | 0 |
Num Resident Building Affctd | 0 |
Num Business Building Affctd | 0 |
Accident Psig | 721 |
Mop Psig | 1200 |
Mop Cfr Section | Subpart E Pressure Test �195.406(A)(3) View CFR 49 §192 |
Maop Established Date | 1997-09-09 00:00:00 |
Maop Reversal Flow Ind | No |
Accident Pressure | Pressure Did Not Exceed Mop |
Pressure Restriction Ind | No |
Pipeline Function | > 20% Smys Regulated Transmission |
Scada In Place Ind | Yes |
Scada Operating Ind | Yes |
Scada Functional Ind | No |
Scada Detection Ind | No |
Scada Conf Ind | No |
Cpm In Place Ind | Yes |
Cpm Operating Ind | Yes |
Cpm Functional Ind | No |
Cpm Detection Ind | No |
Cpm Conf Ind | No |
Investigation Status | Yes, specify investigation result(s): (select all that apply) |
Invest Schedule Ind | Yes |
Invest No Control Room Ind | Yes |
Invest No Controller Ind | Yes |
Employee Drug Test Ind | No |
Contractor Drug Test Ind | No |
Cause | Equipment Failure |
Cause Details | Pump Or Pump-Related Equipment |
Eq Failure Type | Pump Or Pump-Related Equipment |
Other Pump Ind | Seal/packing Failure |
Additional Thermal Ind | Yes |
Preparer Name | D*** T****** |
Preparer Title | Compliance Coordinator |
Preparer Email | D***********@t******.com |
Preparer Telephone | 307-266-0320 |
Prepared Date | 2023-09-05 00:00:00 |
Authorizer Name | K** D********* |
Authorizer Telephone | 307-266-0275 |
Authorizer Title | Director - Government And Control Center |
Authorizer Email | K*************@t******.com |
Narrative | On june 21, 2023 at approximately 09:28 a.M. Mdt, a bridger employee was performing a station check at the iberlin station, which was not operating at the time due to a loss of communications between it and the control center, when he discovered a pump seal had failed and released approximately 25 barrels of diesel inside of the pump building. The employee promptly called the area supervisor to report the release. The area supervisor subsequently contacted operations management to inform them of the release. A local vac truck company was then contacted and a vac truck was dispatched to the location to assist with the recovery of the released product. Once the vac truck arrived all released product was recovered and disposed of in accordance with wyoming deq requirements. After all of the released product was recovered, bpl employees examined the pump seal and determined it had failed due to high temperature. Taking this into consideration, it was decided to replace both the seal and pump. After the pump and seal were replaced, employees corrected the communications issue and the station was placed back into service. Further review of the incident revealed that a configuration in the plc logic allowed the pump to try and restart multiple times under low suction pressure which created a dry run/cavitation situation causing high temperatures and subsequent failure of the seal. The plc logic has subsequently been modified to mitigate the possibility of a dry run/cavitation situation. No wildlife, surface water, ground water or soils were impacted or contaminated as all released product was contained inside of the pump building. As mentioned above, all of the released product was recovered and was properly disposed of in accordance with wyoming deq requirements. Since the release did meet wyoming state deq reporting requirements, they were contacted and advised of the release. The release, however, did not meet national response center telephonic reporting requirements; therefore, no call was made to the nrc. |
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