HL incident on 2023-07-14 — OK

Operator
Williams Field Services
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$300,000
Incident datetime
2023-07-14 00:00 UTC
Report number
Location
OK
Narrative
On friday evening june 16 about 5pm the station fire-eye tripped the ogallah pump station facility esd, shutting down the pump and blocking in the station. Pipeline control could not get the remote cameras to pull up to verify presence of actual fire, and our technician responded in person within about 20 minutes, to an obvious fire. The fire was localized to one of the two pumps, p-200. The fire department responded and our technician and the fire department stood by about 3/4 mile away from the station. Ogallah ps is on a dead end so there was no concern of public encroachment. The fire size was initially around 3 to 4 feet high and gradually decreasing over time. Decision was made to allow for fire to consume leaking product until size was decreased to reasonable size for entry with a developed safe work management work plan. Entry to the site occurred on saturday evening to ignite the facility flare and open manual blowdowns to accelerate the depressurization. Once the manual blowdown valves were opened, the seal fire soon extinguished by about 7pm. The site was inspected and utility power was restored before the ups batteries expired. No delivery volumes were impacted during fire event due to the pump station being isolated from mainline and fire sufficiently away from the mainline. Ogallah station second pump, p-100 was put back into service as of 6/20/23 18:48 local time. Pump p-200, one that caught fire, is still out of service.
Detailed record list
Report Received Date
2023-07-14 00:00:00
Iyear
2023
Report Number
20230160
Supplemental Number
39102
Report Type
Supplemental Final
Operator Id
Name
Williams Field Services
Operator Street Address
One Williams Center Wrc-3
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74172
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
36
Intentional Release Bbls
4
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Or Pack Calculations)
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Nrc Rpt Num
Additional Nrc Report Numbers
1370443
Ignite Ind
Yes
How Extinguished
Operator/contractor
Consumed By Fire In Barrels
36
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Ogallah Pump Station
Segment Name
Overland Pipeline Pass (Oppl)
Onshore State Abbreviation
Ks
Onshore Postal Code
67656
Onshore City Name
Not Within A Municipality
Onshore County Name
Trego
Designated Location
Milepost
Designated Name
643.8
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pump
Pump Type
Centrifugal
Pump Service Type
Mainline
Installation Year
Unknown
Manufactured Year
Unknown
Material Involved
Material Other Than Carbon Steel
Material Details
Antimony / Tungsten Carbide
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
40000
Est Cost Gas Released
1700
Est Cost Prop Damage
300000
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
341700
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
1219
Mop Psig
1440
Mop Cfr Section
Component Design Pressure �195.406(A)(2)
Maop Established Date
2015-03-14 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Pump station was operating at normal conditions and seal failure could not be caused by any action by a controller.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Pump Or Pump-Related Equipment
Eq Failure Type
Pump Or Pump-Related Equipment
Other Pump Ind
Seal/packing Failure
Ief Addl Misalignment Ind
Yes
Additional Erosion Wear Ind
Yes
Preparer Name
L***** H***
Preparer Title
Pipeline Safety Manager
Preparer Email
L**********@w*******.com
Preparer Telephone
9182404259
Prepared Date
2024-01-23 00:00:00
Local Contact Name
T* S********
Local Contact Email
T***********@w*******.com
Local Contact Telephone
6208342162
Authorizer Name
L***** H***
Authorizer Telephone
9182404259
Authorizer Title
Pipeline Safety Manager
Authorizer Email
L**********@w*******.com
Narrative
On friday evening june 16 about 5pm the station fire-eye tripped the ogallah pump station facility esd, shutting down the pump and blocking in the station. Pipeline control could not get the remote cameras to pull up to verify presence of actual fire, and our technician responded in person within about 20 minutes, to an obvious fire. The fire was localized to one of the two pumps, p-200. The fire department responded and our technician and the fire department stood by about 3/4 mile away from the station. Ogallah ps is on a dead end so there was no concern of public encroachment. The fire size was initially around 3 to 4 feet high and gradually decreasing over time. Decision was made to allow for fire to consume leaking product until size was decreased to reasonable size for entry with a developed safe work management work plan. Entry to the site occurred on saturday evening to ignite the facility flare and open manual blowdowns to accelerate the depressurization. Once the manual blowdown valves were opened, the seal fire soon extinguished by about 7pm. The site was inspected and utility power was restored before the ups batteries expired. No delivery volumes were impacted during fire event due to the pump station being isolated from mainline and fire sufficiently away from the mainline. Ogallah station second pump, p-100 was put back into service as of 6/20/23 18:48 local time. Pump p-200, one that caught fire, is still out of service.
Report Received Date 2023-07-14 00:00:00
Iyear 2023
Report Number 20230160
Supplemental Number 39102
Report Type Supplemental Final
Operator Id 30826 PHMSA Enforcement
Name Williams Field Services
Operator Street Address One Williams Center Wrc-3
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74172
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 38.938333 Google Maps OpenStreetMap
Location Longitude -99.760555 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls 36
Intentional Release Bbls 4
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Or Pack Calculations)
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind Yes
Communication State Fed Ind Yes
Party Initiated Communication Operator
Nrc Rpt Num 1370328 NRC Report How to search
Additional Nrc Report Numbers 1370443
Ignite Ind Yes
How Extinguished Operator/contractor
Consumed By Fire In Barrels 36
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Ogallah Pump Station
Segment Name Overland Pipeline Pass (Oppl)
Onshore State Abbreviation Ks
Onshore Postal Code 67656
Onshore City Name Not Within A Municipality
Onshore County Name Trego
Designated Location Milepost
Designated Name 643.8
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Pump
Pump Type Centrifugal
Pump Service Type Mainline
Installation Year Unknown
Manufactured Year Unknown
Material Involved Material Other Than Carbon Steel
Material Details Antimony / Tungsten Carbide
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 40000
Est Cost Gas Released 1700
Est Cost Prop Damage 300000
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 341700
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 1219
Mop Psig 1440
Mop Cfr Section Component Design Pressure �195.406(A)(2) View CFR 49 §192
Maop Established Date 2015-03-14 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Pump station was operating at normal conditions and seal failure could not be caused by any action by a controller.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Pump Or Pump-Related Equipment
Eq Failure Type Pump Or Pump-Related Equipment
Other Pump Ind Seal/packing Failure
Ief Addl Misalignment Ind Yes
Additional Erosion Wear Ind Yes
Preparer Name L***** H***
Preparer Title Pipeline Safety Manager
Preparer Email L**********@w*******.com
Preparer Telephone 9182404259
Prepared Date 2024-01-23 00:00:00
Local Contact Name T* S********
Local Contact Email T***********@w*******.com
Local Contact Telephone 6208342162
Authorizer Name L***** H***
Authorizer Telephone 9182404259
Authorizer Title Pipeline Safety Manager
Authorizer Email L**********@w*******.com
Narrative On friday evening june 16 about 5pm the station fire-eye tripped the ogallah pump station facility esd, shutting down the pump and blocking in the station. Pipeline control could not get the remote cameras to pull up to verify presence of actual fire, and our technician responded in person within about 20 minutes, to an obvious fire. The fire was localized to one of the two pumps, p-200. The fire department responded and our technician and the fire department stood by about 3/4 mile away from the station. Ogallah ps is on a dead end so there was no concern of public encroachment. The fire size was initially around 3 to 4 feet high and gradually decreasing over time. Decision was made to allow for fire to consume leaking product until size was decreased to reasonable size for entry with a developed safe work management work plan. Entry to the site occurred on saturday evening to ignite the facility flare and open manual blowdowns to accelerate the depressurization. Once the manual blowdown valves were opened, the seal fire soon extinguished by about 7pm. The site was inspected and utility power was restored before the ups batteries expired. No delivery volumes were impacted during fire event due to the pump station being isolated from mainline and fire sufficiently away from the mainline. Ogallah station second pump, p-100 was put back into service as of 6/20/23 18:48 local time. Pump p-200, one that caught fire, is still out of service.

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