HL incident on 2023-07-13 — TX

Operator
Enterprise Products Operating Llc
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$20,015
Incident datetime
2023-07-13 00:00 UTC
Report number
Location
TX
Narrative
On june 14, 2023 at 10:43am, enterprise was notified by a 3rd party of a ice ball on a valve. A pipeline technician was dispatched and arrived on site to confirm the ice ball was on an enterprise pipeline valve at 11:30. Enterprise dispatched a team to contain the leak area and investigate the source of the leak on the valve. At 1:45 pm enterprise determined that based on the leak rate observed, the leak volume would exceed the 5 gallon threshold and the rrc was notified at 2:00 pm, and assigned incident number 2846. At 6:43 pm, enterprise shut down the pipeline in order to remove and replace the leaking valve. The valve was sent in for examination and it was determined the leak was due to a failed o-ring that was cracked.
Detailed record list
Report Received Date
2023-07-13 00:00:00
Iyear
2023
Report Number
20230158
Supplemental Number
38271
Report Type
Original Final
Operator Id
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
14.77
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Upstream Action Taken
Valve Closure
Upstream Valve Type Ind
Manual
Downstream Action Taken
Valve Closure
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Txca 4" And 3"
Segment Name
Txca
Onshore State Abbreviation
Tx
Onshore Postal Code
77590
Onshore City Name
Texas City
Onshore County Name
Galveston
Designated Location
Survey Station No.
Designated Name
36+48
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Valve
Valve Type
Mainline
Valve Mainline Type
Ball
Valve Manufacturer
Grove
Installation Year
Unknown
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
20015
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
500
Est Cost Other Details
Lab Analysis
Prpty
20515
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
390
Mop Psig
720
Mop Cfr Section
Component Design Pressure �195.406(A)(2)
Maop Established Date
2018-03-28 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
1000
Internal Inspection Ind
No
Diameter Change Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
This was a small leak on a valve.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
O-Ring
Eq Additional Other Ind
Yes
Eq Additional Other Details
O-Ring Failed Over Time
Preparer Name
C******* V******
Preparer Title
Engineer Pipeline Compliance
Preparer Email
C********@e****.com
Preparer Telephone
8326575864
Prepared Date
2023-07-13 00:00:00
Authorizer Name
N*** T*****
Authorizer Telephone
7133812493
Authorizer Title
Senior Manager Compliance
Authorizer Email
N*******@e****.com
Narrative
On june 14, 2023 at 10:43am, enterprise was notified by a 3rd party of a ice ball on a valve. A pipeline technician was dispatched and arrived on site to confirm the ice ball was on an enterprise pipeline valve at 11:30. Enterprise dispatched a team to contain the leak area and investigate the source of the leak on the valve. At 1:45 pm enterprise determined that based on the leak rate observed, the leak volume would exceed the 5 gallon threshold and the rrc was notified at 2:00 pm, and assigned incident number 2846. At 6:43 pm, enterprise shut down the pipeline in order to remove and replace the leaking valve. The valve was sent in for examination and it was determined the leak was due to a failed o-ring that was cracked.
Report Received Date 2023-07-13 00:00:00
Iyear 2023
Report Number 20230158
Supplemental Number 38271
Report Type Original Final
Operator Id 31618 PHMSA Enforcement
Name Enterprise Products Operating Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 29.37092 Google Maps OpenStreetMap
Location Longitude -94.91177 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls 14.77
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Public
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind Yes
Communication State Fed Ind Yes
Party Initiated Communication Operator
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Upstream Action Taken Valve Closure
Upstream Valve Type Ind Manual
Downstream Action Taken Valve Closure
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Txca 4" And 3"
Segment Name Txca
Onshore State Abbreviation Tx
Onshore Postal Code 77590
Onshore City Name Texas City
Onshore County Name Galveston
Designated Location Survey Station No.
Designated Name 36+48
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Valve
Valve Type Mainline
Valve Mainline Type Ball
Valve Manufacturer Grove
Installation Year Unknown
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 20015
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 500
Est Cost Other Details Lab Analysis
Prpty 20515
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 390
Mop Psig 720
Mop Cfr Section Component Design Pressure �195.406(A)(2) View CFR 49 §192
Maop Established Date 2018-03-28 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 1000
Internal Inspection Ind No
Diameter Change Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details This was a small leak on a valve.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind O-Ring
Eq Additional Other Ind Yes
Eq Additional Other Details O-Ring Failed Over Time
Preparer Name C******* V******
Preparer Title Engineer Pipeline Compliance
Preparer Email C********@e****.com
Preparer Telephone 8326575864
Prepared Date 2023-07-13 00:00:00
Authorizer Name N*** T*****
Authorizer Telephone 7133812493
Authorizer Title Senior Manager Compliance
Authorizer Email N*******@e****.com
Narrative On june 14, 2023 at 10:43am, enterprise was notified by a 3rd party of a ice ball on a valve. A pipeline technician was dispatched and arrived on site to confirm the ice ball was on an enterprise pipeline valve at 11:30. Enterprise dispatched a team to contain the leak area and investigate the source of the leak on the valve. At 1:45 pm enterprise determined that based on the leak rate observed, the leak volume would exceed the 5 gallon threshold and the rrc was notified at 2:00 pm, and assigned incident number 2846. At 6:43 pm, enterprise shut down the pipeline in order to remove and replace the leaking valve. The valve was sent in for examination and it was determined the leak was due to a failed o-ring that was cracked.

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