Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2023-07-10 — OH
Operator
Marathon Pipe Line Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$60
Incident datetime
2023-07-10 00:00 UTC
Report number
Location
OH
Narrative
On june 12, 2023, at approximately 0900 central time, the station operator was performing the weekly station checks when he noticed crude oil on the pump skid and around the pump base. He immediately contacted supervision and a stop help start was initiated. Upon further investigation it was discovered that a section of stainless-steel tubing for the bearing cooling system had worn a small hole from the inside due to severe turbulence in the flow through the tube due to a ball valve that was not fully open. The section of tubing was replaced in addition to the ball valve. 08/22/2023 supplemental final made change from "jetting" to flow turbulence and added the partially closed ball valve to the narrative as a cause of the turbulent flow.
Detailed record list
Report Received Date
2023-07-10 00:00:00
Iyear
2023
Report Number
20230153
Supplemental Number
38431
Report Type
Supplemental Final
Operator Id
32147
Name
Marathon Pipe Line Llc
Operator Street Address
539 South Main Street
Operator City Name
Findlay
Operator State Abbreviation
OH
Operator Postal Code
45840
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
41.565023
Location Longitude
-109.980225
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.4
Recovered Bbls
0.4
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Status When Identified
Routine Shutdown
Communication State Fed Ind
No
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Notify Qualified Indiv Ind
Yes
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Wamsutter (Slc Core)
Segment Name
Granger Station
Onshore State Abbreviation
Wy
Onshore Postal Code
82935
Onshore City Name
Granger
Onshore County Name
Sweetwater
Designated Location
Milepost
Designated Name
Granger Stati
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tubing
Tubing Material
Stainless Steel
Tubing Type
Rigid
Installation Year
2022
Manufactured Year
2021
Material Involved
Material Other Than Carbon Steel
Material Details
Stainless Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
10
Est Cost Prop Damage
60
Est Cost Emergency
806
Est Cost Environmental
0
Est Cost Other
0
Prpty
876
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
113
Mop Psig
5100
Mop Cfr Section
Internal Design Pressure �195.406(A)(1)
Maop Established Date
2022-02-26 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Controller actions had no impact on incident.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Defective Or Loose Tubing Or Fitting
Eq Failure Type
Defective Or Loose Tubing Or Fitting
Additional Erosion Wear Ind
Yes
Preparer Name
Z*** C*********
Preparer Title
Compliance Specialist
Preparer Email
Z***********@g****.com
Prepared Date
2023-08-22 00:00:00
Authorizer Name
M****** G***
Authorizer Telephone
4193794019
Authorizer Title
Compliance Manager
Authorizer Email
M*****@m****************.com
Narrative
On june 12, 2023, at approximately 0900 central time, the station operator was performing the weekly station checks when he noticed crude oil on the pump skid and around the pump base. He immediately contacted supervision and a stop help start was initiated. Upon further investigation it was discovered that a section of stainless-steel tubing for the bearing cooling system had worn a small hole from the inside due to severe turbulence in the flow through the tube due to a ball valve that was not fully open. The section of tubing was replaced in addition to the ball valve. 08/22/2023 supplemental final made change from "jetting" to flow turbulence and added the partially closed ball valve to the narrative as a cause of the turbulent flow.
Report Received Date | 2023-07-10 00:00:00 |
---|---|
Iyear | 2023 |
Report Number | 20230153 |
Supplemental Number | 38431 |
Report Type | Supplemental Final |
Operator Id | 32147 PHMSA Enforcement |
Name | Marathon Pipe Line Llc |
Operator Street Address | 539 South Main Street |
Operator City Name | Findlay |
Operator State Abbreviation | OH |
Operator Postal Code | 45840 |
Time Zone | Central |
Daylight Savings Ind | Yes |
Location Latitude | 41.565023 Google Maps OpenStreetMap |
Location Longitude | -109.980225 Google Maps OpenStreetMap |
Commodity Released Type | Crude Oil |
Unintentional Release Bbls | 0.4 |
Recovered Bbls | 0.4 |
Fatality Ind | No |
Fatal | 0 |
Injury Ind | No |
Injure | 0 |
Accident Identifier | Local Operating Personnel, Including Contractors |
Operator Type | Operator Employee |
System Part Involved | Onshore Pump/meter Station Equipment And Piping |
On Off Shore | Onshore |
Status When Identified | Routine Shutdown |
Communication State Fed Ind | No |
Nrc Rpt Num | Nrc Notification Not Required NRC Report How to search |
Ignite Ind | No |
Notify Qualified Indiv Ind | Yes |
Oil Spill Removal Org Ind | No |
Num Pub Evacuated | 0 |
Pipe Fac Name | Wamsutter (Slc Core) |
Segment Name | Granger Station |
Onshore State Abbreviation | Wy |
Onshore Postal Code | 82935 |
Onshore City Name | Granger |
Onshore County Name | Sweetwater |
Designated Location | Milepost |
Designated Name | Granger Stati |
Federal | No |
Location Type | Totally Contained On Operator-Controlled Property |
Incident Area Type | Aboveground |
Incident Area Subtype | Typical Aboveground Facility Piping Or Appurtenance |
Crossing | No |
Pipe Facility Type | Interstate |
Item Involved | Tubing |
Tubing Material | Stainless Steel |
Tubing Type | Rigid |
Installation Year | 2022 |
Manufactured Year | 2021 |
Material Involved | Material Other Than Carbon Steel |
Material Details | Stainless Steel |
Release Type | Leak |
Leak Type | Pinhole |
Wildlife Impact Ind | No |
Soil Contamination | Yes |
Long Term Assessment | No |
Remediation Ind | No |
Water Contam Ind | No |
Could Be Hca | Yes |
Commodity Reached Hca | No |
Est Cost Oper Paid | 0 |
Est Cost Gas Released | 10 |
Est Cost Prop Damage | 60 |
Est Cost Emergency | 806 |
Est Cost Environmental | 0 |
Est Cost Other | 0 |
Prpty | 876 |
Num Persons Hosp Not Ovnght | 0 |
Num Injured Treated By Emt | 0 |
Num Resident Building Affctd | 0 |
Num Business Building Affctd | 0 |
Accident Psig | 113 |
Mop Psig | 5100 |
Mop Cfr Section | Internal Design Pressure �195.406(A)(1) View CFR 49 §192 |
Maop Established Date | 2022-02-26 00:00:00 |
Maop Reversal Flow Ind | No |
Accident Pressure | Pressure Did Not Exceed Mop |
Pressure Restriction Ind | No |
Pipeline Function | > 20% Smys Regulated Transmission |
Scada In Place Ind | Yes |
Scada Operating Ind | Yes |
Scada Functional Ind | Yes |
Scada Detection Ind | No |
Scada Conf Ind | No |
Cpm In Place Ind | Yes |
Cpm Operating Ind | Yes |
Cpm Functional Ind | Yes |
Cpm Detection Ind | No |
Cpm Conf Ind | No |
Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
Investigation Status Details | Controller actions had no impact on incident. |
Employee Drug Test Ind | No |
Contractor Drug Test Ind | No |
Cause | Equipment Failure |
Cause Details | Defective Or Loose Tubing Or Fitting |
Eq Failure Type | Defective Or Loose Tubing Or Fitting |
Additional Erosion Wear Ind | Yes |
Preparer Name | Z*** C********* |
Preparer Title | Compliance Specialist |
Preparer Email | Z***********@g****.com |
Prepared Date | 2023-08-22 00:00:00 |
Authorizer Name | M****** G*** |
Authorizer Telephone | 4193794019 |
Authorizer Title | Compliance Manager |
Authorizer Email | M*****@m****************.com |
Narrative | On june 12, 2023, at approximately 0900 central time, the station operator was performing the weekly station checks when he noticed crude oil on the pump skid and around the pump base. He immediately contacted supervision and a stop help start was initiated. Upon further investigation it was discovered that a section of stainless-steel tubing for the bearing cooling system had worn a small hole from the inside due to severe turbulence in the flow through the tube due to a ball valve that was not fully open. The section of tubing was replaced in addition to the ball valve. 08/22/2023 supplemental final made change from "jetting" to flow turbulence and added the partially closed ball valve to the narrative as a cause of the turbulent flow. |
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