HL incident on 2023-07-06 — GA

Operator
Colonial Pipeline Co
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$5,000
Incident datetime
2023-07-06 00:00 UTC
Report number
Location
GA
Narrative
On thursday, june 8th, 2023, at approximately 20:00 cst, an operator discovered freestanding diesel in the shipper valve check-valve vault. There were three check valves in this vault (one gasoline line and two distillate lines). All three lines were inactive and were isolated at the time of discovery. All appropriate notifications were made. Personnel were mobilized and arrived at approximately 22:25 cst and began spill recovery and dewatering activities so the source could be investigate/identified. On june 9th, 2023, at 15:30 cst, a 16-inch valve flange on a nearby purge line, outside of the vault was found to be the source of the release. As a result of the release 138 gallons of diesel was released and recovered. All released product was contained on cpc property. Repairs were completed and the line returned to normal operational status on june 10th, 2023, at 15:38 cst. On june 9, 2023, at approximately 14:10 cst, it was discovered response actions may meet or exceed $50,000, thus, a nrc notification was made (see report no. 1369619). The nrc 48-hour update information provided corrections to the following information: date of release discovery to june 8th; the $50,000 nrc notification threshold not being met; and to the reduced release volume (see report no. 1369760). September 9, 2023, a supplemental final report was submitted to PHMSA with the following revisions: subpart a(14) - onshore terminal or tank farm equipment and piping.� subpart c(3) - flange assembly, including gaskets.
Detailed record list
Report Received Date
2023-07-06 00:00:00
Iyear
2023
Report Number
20230145
Supplemental Number
38514
Report Type
Supplemental Final
Operator Id
Name
Colonial Pipeline Co
Operator Street Address
1000 Lake St.
Operator City Name
Alpharetta
Operator State Abbreviation
GA
Operator Postal Code
30009
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
-91.28374885
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
3
Recovered Bbls
3
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Status When Identified
Routine Shutdown
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Nrc Rpt Num
Additional Nrc Report Numbers
1369760
Ignite Ind
No
Notify Qualified Indiv Ind
Yes
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Baton Rouge Junction
Segment Name
88799
Onshore State Abbreviation
La
Onshore Postal Code
70748
Onshore City Name
Jackson
Onshore County Name
East Feliciana
Designated Location
Survey Station No.
Designated Name
222
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
24
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Flange Assembly
Installation Year
1978
Manufactured Year
1978
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
325
Est Cost Prop Damage
5000
Est Cost Emergency
0
Est Cost Environmental
33000
Est Cost Other
0
Prpty
38325
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
50
Mop Psig
275
Mop Cfr Section
Component Design Pressure �195.406(A)(2)
Maop Established Date
1972-08-31 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Equipment failure
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Gasket
Eq Additional Other Ind
Yes
Eq Additional Other Details
Indeterminate
Preparer Name
R***** D*****
Preparer Title
Compliance Coordinator
Preparer Email
R******@c******.com
Preparer Telephone
4097904288
Prepared Date
2023-09-07 00:00:00
Authorizer Name
Q****** F******
Authorizer Telephone
678-762-2270
Authorizer Title
Compliance Director
Authorizer Email
Q*******@c******.com
Narrative
On thursday, june 8th, 2023, at approximately 20:00 cst, an operator discovered freestanding diesel in the shipper valve check-valve vault. There were three check valves in this vault (one gasoline line and two distillate lines). All three lines were inactive and were isolated at the time of discovery. All appropriate notifications were made. Personnel were mobilized and arrived at approximately 22:25 cst and began spill recovery and dewatering activities so the source could be investigate/identified. On june 9th, 2023, at 15:30 cst, a 16-inch valve flange on a nearby purge line, outside of the vault was found to be the source of the release. As a result of the release 138 gallons of diesel was released and recovered. All released product was contained on cpc property. Repairs were completed and the line returned to normal operational status on june 10th, 2023, at 15:38 cst. On june 9, 2023, at approximately 14:10 cst, it was discovered response actions may meet or exceed $50,000, thus, a nrc notification was made (see report no. 1369619). The nrc 48-hour update information provided corrections to the following information: date of release discovery to june 8th; the $50,000 nrc notification threshold not being met; and to the reduced release volume (see report no. 1369760). September 9, 2023, a supplemental final report was submitted to PHMSA with the following revisions: subpart a(14) - onshore terminal or tank farm equipment and piping.� subpart c(3) - flange assembly, including gaskets.
Report Received Date 2023-07-06 00:00:00
Iyear 2023
Report Number 20230145
Supplemental Number 38514
Report Type Supplemental Final
Operator Id 2552 PHMSA Enforcement
Name Colonial Pipeline Co
Operator Street Address 1000 Lake St.
Operator City Name Alpharetta
Operator State Abbreviation GA
Operator Postal Code 30009
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 30.71091977 Google Maps OpenStreetMap
Location Longitude -91.28374885 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 3
Recovered Bbls 3
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Status When Identified Routine Shutdown
Communication State Fed Ind Yes
Party Initiated Communication Operator
Nrc Rpt Num 1369619 NRC Report How to search
Additional Nrc Report Numbers 1369760
Ignite Ind No
Notify Qualified Indiv Ind Yes
Oil Spill Removal Org Ind No
Num Pub Evacuated 0
Pipe Fac Name Baton Rouge Junction
Segment Name 88799
Onshore State Abbreviation La
Onshore Postal Code 70748
Onshore City Name Jackson
Onshore County Name East Feliciana
Designated Location Survey Station No.
Designated Name 222
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 24
Crossing No
Pipe Facility Type Interstate
Item Involved Flange Assembly
Installation Year 1978
Manufactured Year 1978
Material Involved Carbon Steel
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 325
Est Cost Prop Damage 5000
Est Cost Emergency 0
Est Cost Environmental 33000
Est Cost Other 0
Prpty 38325
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 50
Mop Psig 275
Mop Cfr Section Component Design Pressure �195.406(A)(2) View CFR 49 §192
Maop Established Date 1972-08-31 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Equipment failure
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind Gasket
Eq Additional Other Ind Yes
Eq Additional Other Details Indeterminate
Preparer Name R***** D*****
Preparer Title Compliance Coordinator
Preparer Email R******@c******.com
Preparer Telephone 4097904288
Prepared Date 2023-09-07 00:00:00
Authorizer Name Q****** F******
Authorizer Telephone 678-762-2270
Authorizer Title Compliance Director
Authorizer Email Q*******@c******.com
Narrative On thursday, june 8th, 2023, at approximately 20:00 cst, an operator discovered freestanding diesel in the shipper valve check-valve vault. There were three check valves in this vault (one gasoline line and two distillate lines). All three lines were inactive and were isolated at the time of discovery. All appropriate notifications were made. Personnel were mobilized and arrived at approximately 22:25 cst and began spill recovery and dewatering activities so the source could be investigate/identified. On june 9th, 2023, at 15:30 cst, a 16-inch valve flange on a nearby purge line, outside of the vault was found to be the source of the release. As a result of the release 138 gallons of diesel was released and recovered. All released product was contained on cpc property. Repairs were completed and the line returned to normal operational status on june 10th, 2023, at 15:38 cst. On june 9, 2023, at approximately 14:10 cst, it was discovered response actions may meet or exceed $50,000, thus, a nrc notification was made (see report no. 1369619). The nrc 48-hour update information provided corrections to the following information: date of release discovery to june 8th; the $50,000 nrc notification threshold not being met; and to the reduced release volume (see report no. 1369760). September 9, 2023, a supplemental final report was submitted to PHMSA with the following revisions: subpart a(14) - onshore terminal or tank farm equipment and piping.� subpart c(3) - flange assembly, including gaskets.

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