HL incident on 2023-06-21 — TX

Operator
Energy Transfer Company
Cause
Material Failure Of Pipe Or Weld
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$26,000
Incident datetime
2023-06-21 00:00 UTC
Report number
Location
TX
Narrative
On 4/20/2023 at approximately 18:25, operations received a call from a landowner concerning a petroleum odor. Line was shutdown and isolated. After investigation of the area and excavation of the pipeline, confirmation of the release was determined at 23:15. Approximately 4 barrels of crude oil was released. Clean-up crews removed free product and contaminated soil. Nrc was notified in the event that total costs would exceed $50k which they did not. The line was excavated and pinhole leak was found on a weld. A mechanical plidco clamp was installed. The line was monitored under pressure before being released to normal operations. Plans are underway to purge the line section at the clamp site, cut out the pipe section, replace with welded steel pipe, and have the section with the failure further analyzed by third party lab. The plan is to cut out the pipe and sent it to the lab by the end of first quarter 2024. Supplemental: metallurgical analysis determined the cause of the failure was a surface breaking, circumferentially oriented flaw at the girth weld which consisted of two (2) regions. The first region was an inside diameter surface breaking hydrogen assisted cold crack which initiated in the heat affected zone of the u/s pipe joint which displayed a high carbon equivalent. The second region was a semi-elliptical shaped crack that grew through wall while in service.
Detailed record list
Report Received Date
2023-06-21 00:00:00
Iyear
2023
Report Number
20230134
Supplemental Number
40961
Report Type
Supplemental Final
Operator Id
Name
Energy Transfer Company
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Time Zone
Eastern
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
4
Recovered Bbls
4
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Nrc Rpt Num
Additional Nrc Report Numbers
1365352
Ignite Ind
No
Upstream Action Taken
Valve Closure
Upstream Valve Type Ind
Manual
Downstream Action Taken
Valve Closure
Downstream Valve Type Ind
Manual
Notify Qualified Indiv Ind
Yes
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Marysville To Toledo
Segment Name
13002 Cmar-Ctol-16inch
Onshore State Abbreviation
Mi
Onshore Postal Code
48096
Onshore City Name
Ray Township
Onshore County Name
Macomb
Designated Location
Survey Station No.
Designated Name
126955
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
42
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Weld, Including Heat-Affected Zone
Pipe Diameter
16
Pipe Wall Thickness
0.281
Pipe Smys
52000
Pipe Specification
Api 5lx X-52
Pipe Seam Type
Erw - High Frequency
Pipe Manufacturer
Republic Steel
Pipe Coating Type
Coal Tar
Coating Applied Ind
Yes
Weld Subtype
Pipe Girth Weld
Different Girth Weld Ind
No
Installation Year
1967
Manufactured Year
1967
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Crack
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
17246
Est Cost Gas Released
309
Est Cost Prop Damage
26000
Est Cost Emergency
8867
Est Cost Environmental
17698
Est Cost Other
0
Prpty
70120
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
1247
Mop Psig
1300
Mop Cfr Section
Subpart E Pressure Test �195.406(A)(3)
Maop Established Date
1987-04-21 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
52077
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Environmental Cracking-Related
Field Exam Ind
Yes
Metallurgical Ind
Yes
Failure Type
Environmental Cracking-Related
Stress Subtype
Hydrogen Stress Cracking
Additional Crack Ind
Yes
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Cir Trn Wave Mgn Flx Lkg Ind
Yes
Ultrasonic Ind
Yes
Geometry Deformation Ind
Yes
Axial Recent Year
2022
Axial Rcnt Propul Method
Free Swimming
Axial Rcnt Attuned Detect
Metal Loss
Axial Rcnt Atnd Dtct Metal
High Resolution
Axial Previous Year
2017
Axial Prev Propul Method
Free Swimming
Axial Prev Attuned Detect
Metal Loss
Axial Prev Atnd Dtct Metal
High Resolution
Circ Wave Recent Year
2022
Circ Wv Rcnt Propul Method
Free Swimming
Circ Wv Rcnt Resolution
High Resolution
Circ Wv Previous Year
2020
Circ Wv Prev Propul Method
Free Swimming
Circ Wv Prev Resolution
High Resolution
Ultrasonic Recent Year
2014
Ultrasonic Rcnt Propul Method
Free Swimming
Ultrasonic Rcnt Attuned
Crack
Ultr Previous Year
2014
Ultra Prev Propul Method
Free Swimming
Ultra Prev Attuned
Crack
Geometry Recent Year
2022
Geometry Rcnt Propul Method
Free Swimming
Geometry Rcnt Resolution
High Resolution
Geometrt Rcnt Measur Cups
No Cups
Geometry Previous Year
2017
Geometry Prev Propul Method
Free Swimming
Geometry Prev Resolution
High Resolution
Geometrt Prev Measur Cups
No Cups
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
1987
Hydrtst Most Rcnt Pressure
1644
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Pwf Construction Ind
Yes
Preparer Name
T*** N*******
Preparer Title
Director - Dot Compliance
Preparer Email
T************@e*************.com
Preparer Telephone
713-989-7126
Prepared Date
2025-05-28 00:00:00
Authorizer Name
T*** N*******
Authorizer Telephone
713-989-7126
Authorizer Title
Director - Dot Compliance
Authorizer Email
T************@e*************.com
Narrative
On 4/20/2023 at approximately 18:25, operations received a call from a landowner concerning a petroleum odor. Line was shutdown and isolated. After investigation of the area and excavation of the pipeline, confirmation of the release was determined at 23:15. Approximately 4 barrels of crude oil was released. Clean-up crews removed free product and contaminated soil. Nrc was notified in the event that total costs would exceed $50k which they did not. The line was excavated and pinhole leak was found on a weld. A mechanical plidco clamp was installed. The line was monitored under pressure before being released to normal operations. Plans are underway to purge the line section at the clamp site, cut out the pipe section, replace with welded steel pipe, and have the section with the failure further analyzed by third party lab. The plan is to cut out the pipe and sent it to the lab by the end of first quarter 2024. Supplemental: metallurgical analysis determined the cause of the failure was a surface breaking, circumferentially oriented flaw at the girth weld which consisted of two (2) regions. The first region was an inside diameter surface breaking hydrogen assisted cold crack which initiated in the heat affected zone of the u/s pipe joint which displayed a high carbon equivalent. The second region was a semi-elliptical shaped crack that grew through wall while in service.
Report Received Date 2023-06-21 00:00:00
Iyear 2023
Report Number 20230134
Supplemental Number 40961
Report Type Supplemental Final
Operator Id 32099 PHMSA Enforcement
Name Energy Transfer Company
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Time Zone Eastern
Daylight Savings Ind Yes
Location Latitude 42.719019 Google Maps OpenStreetMap
Location Longitude -82.861316 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 4
Recovered Bbls 4
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Public
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind Yes
Communication State Fed Ind Yes
Party Initiated Communication Operator
Nrc Rpt Num 1365300 NRC Report How to search
Additional Nrc Report Numbers 1365352
Ignite Ind No
Upstream Action Taken Valve Closure
Upstream Valve Type Ind Manual
Downstream Action Taken Valve Closure
Downstream Valve Type Ind Manual
Notify Qualified Indiv Ind Yes
Oil Spill Removal Org Ind No
Num Pub Evacuated 0
Pipe Fac Name Marysville To Toledo
Segment Name 13002 Cmar-Ctol-16inch
Onshore State Abbreviation Mi
Onshore Postal Code 48096
Onshore City Name Ray Township
Onshore County Name Macomb
Designated Location Survey Station No.
Designated Name 126955
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 42
Crossing No
Pipe Facility Type Interstate
Item Involved Weld, Including Heat-Affected Zone
Pipe Diameter 16
Pipe Wall Thickness 0.281
Pipe Smys 52000
Pipe Specification Api 5lx X-52
Pipe Seam Type Erw - High Frequency
Pipe Manufacturer Republic Steel
Pipe Coating Type Coal Tar
Coating Applied Ind Yes
Weld Subtype Pipe Girth Weld
Different Girth Weld Ind No
Installation Year 1967
Manufactured Year 1967
Material Involved Carbon Steel
Release Type Leak
Leak Type Crack
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 17246
Est Cost Gas Released 309
Est Cost Prop Damage 26000
Est Cost Emergency 8867
Est Cost Environmental 17698
Est Cost Other 0
Prpty 70120
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 1247
Mop Psig 1300
Mop Cfr Section Subpart E Pressure Test �195.406(A)(3) View CFR 49 §192
Maop Established Date 1987-04-21 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 52077
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Material Failure Of Pipe Or Weld
Cause Details Environmental Cracking-Related
Field Exam Ind Yes
Metallurgical Ind Yes
Failure Type Environmental Cracking-Related
Stress Subtype Hydrogen Stress Cracking
Additional Crack Ind Yes
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Cir Trn Wave Mgn Flx Lkg Ind Yes
Ultrasonic Ind Yes
Geometry Deformation Ind Yes
Axial Recent Year 2022
Axial Rcnt Propul Method Free Swimming
Axial Rcnt Attuned Detect Metal Loss
Axial Rcnt Atnd Dtct Metal High Resolution
Axial Previous Year 2017
Axial Prev Propul Method Free Swimming
Axial Prev Attuned Detect Metal Loss
Axial Prev Atnd Dtct Metal High Resolution
Circ Wave Recent Year 2022
Circ Wv Rcnt Propul Method Free Swimming
Circ Wv Rcnt Resolution High Resolution
Circ Wv Previous Year 2020
Circ Wv Prev Propul Method Free Swimming
Circ Wv Prev Resolution High Resolution
Ultrasonic Recent Year 2014
Ultrasonic Rcnt Propul Method Free Swimming
Ultrasonic Rcnt Attuned Crack
Ultr Previous Year 2014
Ultra Prev Propul Method Free Swimming
Ultra Prev Attuned Crack
Geometry Recent Year 2022
Geometry Rcnt Propul Method Free Swimming
Geometry Rcnt Resolution High Resolution
Geometrt Rcnt Measur Cups No Cups
Geometry Previous Year 2017
Geometry Prev Propul Method Free Swimming
Geometry Prev Resolution High Resolution
Geometrt Prev Measur Cups No Cups
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 1987
Hydrtst Most Rcnt Pressure 1644
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Pwf Construction Ind Yes
Preparer Name T*** N*******
Preparer Title Director - Dot Compliance
Preparer Email T************@e*************.com
Preparer Telephone 713-989-7126
Prepared Date 2025-05-28 00:00:00
Authorizer Name T*** N*******
Authorizer Telephone 713-989-7126
Authorizer Title Director - Dot Compliance
Authorizer Email T************@e*************.com
Narrative On 4/20/2023 at approximately 18:25, operations received a call from a landowner concerning a petroleum odor. Line was shutdown and isolated. After investigation of the area and excavation of the pipeline, confirmation of the release was determined at 23:15. Approximately 4 barrels of crude oil was released. Clean-up crews removed free product and contaminated soil. Nrc was notified in the event that total costs would exceed $50k which they did not. The line was excavated and pinhole leak was found on a weld. A mechanical plidco clamp was installed. The line was monitored under pressure before being released to normal operations. Plans are underway to purge the line section at the clamp site, cut out the pipe section, replace with welded steel pipe, and have the section with the failure further analyzed by third party lab. The plan is to cut out the pipe and sent it to the lab by the end of first quarter 2024. Supplemental: metallurgical analysis determined the cause of the failure was a surface breaking, circumferentially oriented flaw at the girth weld which consisted of two (2) regions. The first region was an inside diameter surface breaking hydrogen assisted cold crack which initiated in the heat affected zone of the u/s pipe joint which displayed a high carbon equivalent. The second region was a semi-elliptical shaped crack that grew through wall while in service.

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