HL incident on 2023-06-14 — OK

Operator
Magellan Pipeline Company, Lp
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,000
Incident datetime
2023-06-14 00:00 UTC
Report number
Location
OK
Narrative
At 15:39 on may 15th, 2023 magellan operations personnel were conducting a daily facility inspection at odessa terminal when they noticed a 3" globe valve on a temporary recirculation line leaking through the packing. The operator shut in the recirculation line to stop the release and clean-up activities were initiated. Further investigation determined excessive vibration caused the packing nut to loosen which allowed product to leak through the packing. To prevent a re-occurrence, the valve was removed and blind flanges were installed.
Detailed record list
Report Received Date
2023-06-14 00:00:00
Iyear
2023
Report Number
20230128
Supplemental Number
38172
Report Type
Original Final
Operator Id
Name
Magellan Pipeline Company, Lp
Operator Street Address
100 West 5th Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
0.6
Recovered Bbls
0.28
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Notify Qualified Indiv Ind
Yes
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Odessa Station
Segment Name
Fac Id 701
Onshore State Abbreviation
Tx
Onshore Postal Code
79766
Onshore City Name
Odessa
Onshore County Name
Ector
Designated Location
Milepost
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
2023
Manufactured Year
2022
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
78
Est Cost Prop Damage
1000
Est Cost Emergency
7500
Est Cost Environmental
5000
Est Cost Other
0
Prpty
13578
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
1200
Mop Psig
1440
Mop Cfr Section
Component Design Pressure �195.406(A)(2)
Maop Established Date
2023-01-01 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The assets involved in the incident are monitored by local operations and not the control room center
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Seal (Not Pump Seal) Or Packing
Additional Vibration Ind
Yes
Preparer Name
C******* R******
Preparer Email
C***************@m*********.com
Preparer Telephone
9185747065
Prepared Date
2023-06-14 00:00:00
Authorizer Name
T***** K***
Authorizer Telephone
9185747191
Authorizer Title
Supv. Integrity Mgmt And Regulatory Compliance
Authorizer Email
T**********@m*********.com
Narrative
At 15:39 on may 15th, 2023 magellan operations personnel were conducting a daily facility inspection at odessa terminal when they noticed a 3" globe valve on a temporary recirculation line leaking through the packing. The operator shut in the recirculation line to stop the release and clean-up activities were initiated. Further investigation determined excessive vibration caused the packing nut to loosen which allowed product to leak through the packing. To prevent a re-occurrence, the valve was removed and blind flanges were installed.
Report Received Date 2023-06-14 00:00:00
Iyear 2023
Report Number 20230128
Supplemental Number 38172
Report Type Original Final
Operator Id 22610 PHMSA Enforcement
Name Magellan Pipeline Company, Lp
Operator Street Address 100 West 5th Street
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74103
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 31.818508 Google Maps OpenStreetMap
Location Longitude -102.333491 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 0.6
Recovered Bbls 0.28
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind Yes
Communication State Fed Ind Yes
Party Initiated Communication Operator
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Notify Qualified Indiv Ind Yes
Oil Spill Removal Org Ind No
Num Pub Evacuated 0
Pipe Fac Name Odessa Station
Segment Name Fac Id 701
Onshore State Abbreviation Tx
Onshore Postal Code 79766
Onshore City Name Odessa
Onshore County Name Ector
Designated Location Milepost
Designated Name 0
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year 2023
Manufactured Year 2022
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 78
Est Cost Prop Damage 1000
Est Cost Emergency 7500
Est Cost Environmental 5000
Est Cost Other 0
Prpty 13578
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 1200
Mop Psig 1440
Mop Cfr Section Component Design Pressure �195.406(A)(2) View CFR 49 §192
Maop Established Date 2023-01-01 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The assets involved in the incident are monitored by local operations and not the control room center
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind Seal (Not Pump Seal) Or Packing
Additional Vibration Ind Yes
Preparer Name C******* R******
Preparer Email C***************@m*********.com
Preparer Telephone 9185747065
Prepared Date 2023-06-14 00:00:00
Authorizer Name T***** K***
Authorizer Telephone 9185747191
Authorizer Title Supv. Integrity Mgmt And Regulatory Compliance
Authorizer Email T**********@m*********.com
Narrative At 15:39 on may 15th, 2023 magellan operations personnel were conducting a daily facility inspection at odessa terminal when they noticed a 3" globe valve on a temporary recirculation line leaking through the packing. The operator shut in the recirculation line to stop the release and clean-up activities were initiated. Further investigation determined excessive vibration caused the packing nut to loosen which allowed product to leak through the packing. To prevent a re-occurrence, the valve was removed and blind flanges were installed.

All rights reserved. Copyright © by ClearPHMSA