Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2023-06-13 — OK
Operator
Oneok Ngl Pipeline, Llc
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$100
Incident datetime
2023-06-13 00:00 UTC
Report number
Location
OK
Narrative
On may 13, 2023 at 10:50am (mdt) oneok pipeline control received a call from a 3rd party operator who reported a potential ice ball at oneok linam ranch meter skid. A oneok operator was dispatched and arrived on site to discover a release on the oneok launcher door. The launcher was isolated and evacuated of product. Upon investigation, the operator found the launcher door o-ring had failed. The o-ring was replaced, product reintroduced to the launcher with the operator remaining on site to ensure normal operations. Oneok reviewed pressure transmitter data and determined the o-ring failure likely started at approximately 5:50 pm on may 12th. Update: oneok submitted the failed o-ring to a third party for analysis. The third party analysis determined the o-ring failed due to a decompression event and did not find any indication of o-ring material degradation. The o-ring material itself, as compared to an exemplar, appeared to have maintained elasticity, had appropriate hardness, appropriate chemical analysis, and a 1.1 percent deviation in the o-ring circumference measurement. The lab was not able to determine the cause of the decompression event. Oneok verified the o-ring was installed per oneok's procedure.
Detailed record list
Report Received Date
2023-06-13 00:00:00
Iyear
2023
Report Number
20230125
Supplemental Number
38960
Report Type
Supplemental Final
Operator Id
32109
Name
Oneok Ngl Pipeline, Llc
Operator Street Address
100 West Fifth Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Time Zone
Mountain
Daylight Savings Ind
Yes
Location Latitude
32.69511
Location Longitude
-103.281434
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
12.8
Intentional Release Bbls
0.1
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
No
Shutdown Explain
The Pig Trap Was Isolated And The Pipeline Was Available To Operate.
Communication State Fed Ind
No
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Linam Ranch - Site 1012
Segment Name
20378 Enron Hobbs Lateral 4 Inch
Onshore State Abbreviation
Nm
Onshore Postal Code
88240
Onshore City Name
Not Within A Municipality
Onshore County Name
Lea County
Designated Location
Survey Station No.
Designated Name
0+00
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Scraper/pig Trap
Installation Year
2023
Manufactured Year
Unknown
Material Involved
Material Other Than Carbon Steel
Material Details
Viton O-Ring
Release Type
Leak
Leak Type
Other
Leak Type Other
O-Ring Failure
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
500
Est Cost Prop Damage
100
Est Cost Emergency
500
Est Cost Environmental
0
Est Cost Other
0
Prpty
1100
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
763
Mop Psig
1440
Mop Cfr Section
Four Hour Test Or Operation �195.406(A)(5)
Maop Established Date
2022-11-22 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Invest Incorrect Action Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
O-Ring
Eq Additional Other Ind
Yes
Eq Additional Other Details
See Narrative
Preparer Name
B**** T*****
Preparer Title
Supervisor - Regulatory Compliance
Preparer Email
B***********@o****.com
Preparer Telephone
6208203047
Prepared Date
2023-12-14 00:00:00
Local Contact Name
M***** C********
Local Contact Email
M***************@o****.com
Local Contact Telephone
2542928911
Authorizer Name
M****** G******
Authorizer Telephone
9185887382
Authorizer Title
Vp Natural Gas Liquids - Pipelines And Terminals
Authorizer Email
M**************@o****.com
Narrative
On may 13, 2023 at 10:50am (mdt) oneok pipeline control received a call from a 3rd party operator who reported a potential ice ball at oneok linam ranch meter skid. A oneok operator was dispatched and arrived on site to discover a release on the oneok launcher door. The launcher was isolated and evacuated of product. Upon investigation, the operator found the launcher door o-ring had failed. The o-ring was replaced, product reintroduced to the launcher with the operator remaining on site to ensure normal operations. Oneok reviewed pressure transmitter data and determined the o-ring failure likely started at approximately 5:50 pm on may 12th. Update: oneok submitted the failed o-ring to a third party for analysis. The third party analysis determined the o-ring failed due to a decompression event and did not find any indication of o-ring material degradation. The o-ring material itself, as compared to an exemplar, appeared to have maintained elasticity, had appropriate hardness, appropriate chemical analysis, and a 1.1 percent deviation in the o-ring circumference measurement. The lab was not able to determine the cause of the decompression event. Oneok verified the o-ring was installed per oneok's procedure.
Report Received Date | 2023-06-13 00:00:00 |
---|---|
Iyear | 2023 |
Report Number | 20230125 |
Supplemental Number | 38960 |
Report Type | Supplemental Final |
Operator Id | 32109 PHMSA Enforcement |
Name | Oneok Ngl Pipeline, Llc |
Operator Street Address | 100 West Fifth Street |
Operator City Name | Tulsa |
Operator State Abbreviation | OK |
Operator Postal Code | 74103 |
Time Zone | Mountain |
Daylight Savings Ind | Yes |
Location Latitude | 32.69511 Google Maps OpenStreetMap |
Location Longitude | -103.281434 Google Maps OpenStreetMap |
Commodity Released Type | Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions |
Commodity Subtype | Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid) |
Unintentional Release Bbls | 12.8 |
Intentional Release Bbls | 0.1 |
Recovered Bbls | 0 |
Fatality Ind | No |
Fatal | 0 |
Injury Ind | No |
Injure | 0 |
Accident Identifier | Notification From Public |
System Part Involved | Onshore Pump/meter Station Equipment And Piping |
On Off Shore | Onshore |
Status When Identified | Normal Operation, Includes Pauses Between Batches And During Maintenance |
Shutdown Due Accident Ind | No |
Shutdown Explain | The Pig Trap Was Isolated And The Pipeline Was Available To Operate. |
Communication State Fed Ind | No |
Nrc Rpt Num | Nrc Notification Not Required NRC Report How to search |
Ignite Ind | No |
Num Pub Evacuated | 0 |
Pipe Fac Name | Linam Ranch - Site 1012 |
Segment Name | 20378 Enron Hobbs Lateral 4 Inch |
Onshore State Abbreviation | Nm |
Onshore Postal Code | 88240 |
Onshore City Name | Not Within A Municipality |
Onshore County Name | Lea County |
Designated Location | Survey Station No. |
Designated Name | 0+00 |
Federal | No |
Location Type | Totally Contained On Operator-Controlled Property |
Incident Area Type | Aboveground |
Incident Area Subtype | Typical Aboveground Facility Piping Or Appurtenance |
Crossing | No |
Pipe Facility Type | Interstate |
Item Involved | Scraper/pig Trap |
Installation Year | 2023 |
Manufactured Year | Unknown |
Material Involved | Material Other Than Carbon Steel |
Material Details | Viton O-Ring |
Release Type | Leak |
Leak Type | Other |
Leak Type Other | O-Ring Failure |
Wildlife Impact Ind | No |
Soil Contamination | No |
Long Term Assessment | No |
Remediation Ind | No |
Water Contam Ind | No |
Could Be Hca | Yes |
Commodity Reached Hca | Yes |
Usa Drinking Ind | Yes |
Usa Drinking Yes No | Yes |
Est Cost Oper Paid | 0 |
Est Cost Gas Released | 500 |
Est Cost Prop Damage | 100 |
Est Cost Emergency | 500 |
Est Cost Environmental | 0 |
Est Cost Other | 0 |
Prpty | 1100 |
Num Persons Hosp Not Ovnght | 0 |
Num Injured Treated By Emt | 0 |
Num Resident Building Affctd | 0 |
Num Business Building Affctd | 0 |
Accident Psig | 763 |
Mop Psig | 1440 |
Mop Cfr Section | Four Hour Test Or Operation �195.406(A)(5) View CFR 49 §192 |
Maop Established Date | 2022-11-22 00:00:00 |
Maop Reversal Flow Ind | No |
Accident Pressure | Pressure Did Not Exceed Mop |
Pressure Restriction Ind | No |
Pipeline Function | > 20% Smys Regulated Transmission |
Scada In Place Ind | Yes |
Scada Operating Ind | Yes |
Scada Functional Ind | Yes |
Scada Detection Ind | No |
Scada Conf Ind | Yes |
Cpm In Place Ind | Yes |
Cpm Operating Ind | Yes |
Cpm Functional Ind | Yes |
Cpm Detection Ind | No |
Cpm Conf Ind | No |
Investigation Status | Yes, specify investigation result(s): (select all that apply) |
Invest Schedule Ind | Yes |
Invest No Control Room Ind | Yes |
Invest Incorrect Action Ind | Yes |
Employee Drug Test Ind | No |
Contractor Drug Test Ind | No |
Cause | Equipment Failure |
Cause Details | Non-Threaded Connection Failure |
Eq Failure Type | Non-Threaded Connection Failure |
Other Non Threaded Ind | O-Ring |
Eq Additional Other Ind | Yes |
Eq Additional Other Details | See Narrative |
Preparer Name | B**** T***** |
Preparer Title | Supervisor - Regulatory Compliance |
Preparer Email | B***********@o****.com |
Preparer Telephone | 6208203047 |
Prepared Date | 2023-12-14 00:00:00 |
Local Contact Name | M***** C******** |
Local Contact Email | M***************@o****.com |
Local Contact Telephone | 2542928911 |
Authorizer Name | M****** G****** |
Authorizer Telephone | 9185887382 |
Authorizer Title | Vp Natural Gas Liquids - Pipelines And Terminals |
Authorizer Email | M**************@o****.com |
Narrative | On may 13, 2023 at 10:50am (mdt) oneok pipeline control received a call from a 3rd party operator who reported a potential ice ball at oneok linam ranch meter skid. A oneok operator was dispatched and arrived on site to discover a release on the oneok launcher door. The launcher was isolated and evacuated of product. Upon investigation, the operator found the launcher door o-ring had failed. The o-ring was replaced, product reintroduced to the launcher with the operator remaining on site to ensure normal operations. Oneok reviewed pressure transmitter data and determined the o-ring failure likely started at approximately 5:50 pm on may 12th. Update: oneok submitted the failed o-ring to a third party for analysis. The third party analysis determined the o-ring failed due to a decompression event and did not find any indication of o-ring material degradation. The o-ring material itself, as compared to an exemplar, appeared to have maintained elasticity, had appropriate hardness, appropriate chemical analysis, and a 1.1 percent deviation in the o-ring circumference measurement. The lab was not able to determine the cause of the decompression event. Oneok verified the o-ring was installed per oneok's procedure. |
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