HL incident on 2023-06-09 — TX

Operator
Ccps Transportation, Llc
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$111,800
Incident datetime
2023-06-09 00:00 UTC
Report number
Location
TX
Narrative
On may 12, 2023, at approximately 7:36 am cdt, a pinhole leak developed on line 55 at mp 25.3071 after an integrity dig crew was sandblasting the area of pipe. The edmonton control center was immediately contacted, and the line was shut down at 7:39 am cdt. The excavation area was evacuated, and enbridge personnel and contractors were mobilized to the site for cleanup and repair. Approximately 2 barrels of crude oil was released and contained within the excavation area. The nrc was notified on may 12, 2023, at 8:42 am cdt (nrc# 1367051). A 48-hour update to the nrc was made on may 13, 2023, at 9:16 pm cdt (nrc# 1367191). The dig at mp 25.3 was issued on april 12, 2023, in response to a priority notification of a corrosion defect called by the december 2022 corrosion inline inspection. The pipe at mp 25.3 is located under a casing as it crosses interstate us39. A sleeve was installed on the pipe and the line was restarted on may 13, 2023, at 6:54 pm cdt. Approximately 53.18 tons of soil was removed from the release site and properly disposed of at an approved facility. A cut out was performed to aid in the investigation to determine a root cause. The results of the investigation indicated that the condensing atmosphere within the casing caused water to drip on the top of the carrier pipe, causing metal loss on the carrier pipe. This process was likely exacerbated by increased pipe operating temperature, as well as the formation of crevices between the pipe and the external coating that formed as corrosion progressed.
Detailed record list
Report Received Date
2023-06-09 00:00:00
Iyear
2023
Report Number
20230124
Supplemental Number
38672
Report Type
Supplemental Final
Operator Id
Name
Ccps Transportation, Llc
Operator Street Address
915 N Eldridge Parkway, Suite 1100
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77079
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
-89.03489181
Commodity Released Type
Crude Oil
Unintentional Release Bbls
2
Recovered Bbls
2
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Communication State Fed Ind
No
Nrc Rpt Num
Additional Nrc Report Numbers
1367191
Ignite Ind
No
Upstream Action Taken
Valve Closure
Upstream Valve Type Ind
Remotely Controlled
Downstream Action Taken
Valve Closure
Downstream Valve Type Ind
Remotely Controlled
Notify Qualified Indiv Ind
Yes
Oil Spill Removal Org Ind
Yes
Osro Arrived On Site Dt
5/12/2023 11:30
Num Pub Evacuated
0
Pipe Fac Name
Line 55
Segment Name
Mp 25.3
Onshore State Abbreviation
Il
Onshore Postal Code
61738
Onshore City Name
El Paso
Onshore County Name
Woodford
Designated Location
Milepost
Designated Name
25.3
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Exposed Due To Excavation
Depth Of Cover
54
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Puddle Weld Ind
No
Pipe Diameter
22
Pipe Wall Thickness
0.312
Pipe Smys
46000
Pipe Specification
X46
Pipe Seam Type
Seamless
Pipe Manufacturer
National Tube
Pipe Coating Type
Coal Tar
Coating Applied Ind
No
Installation Year
1953
Manufactured Year
1953
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
150
Est Cost Prop Damage
111800
Est Cost Emergency
20000
Est Cost Environmental
191455
Est Cost Other
0
Prpty
323405
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
389
Mop Psig
939
Mop Cfr Section
Internal Design Pressure �195.406(A)(1)
Maop Established Date
2005-08-11 00:00:00
Maop Reversal Flow Ind
Yes
Surge Analysis Date
2022-04-28 00:00:00
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
Yes
Exceed Restriction Ind
No
Phmsa Restriction Ind
Not Mandated
Length Segment Isolated
209721
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
External Corrosion
Internal External
External Corrosion
Visual Exam Results
Other
Visual Exam Details
Pinhole
Atmosphere Corrosion Ind
Yes
Other Corrosion Ind
Yes
Corrosion Type Details
Inside Casing
Field Exam Basis Ind
Yes
Other Basis Ind
Yes
Corrosion Basis Details
Engineering Analysis And Lab Testing
Underground Location
No
Externally Coated
Yes
Prior Damage
Yes
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Ultrasonic Ind
Yes
Geometry Deformation Ind
Yes
Other Tool Tech Ind
Yes
Axial Recent Year
2022
Axial Rcnt Propul Method
Free Swimming
Axial Rcnt Attuned Detect
Metal Loss
Axial Rcnt Atnd Dtct Metal
High Resolution
Axial Previous Year
2018
Axial Prev Propul Method
Free Swimming
Axial Prev Attuned Detect
Metal Loss
Axial Prev Atnd Dtct Metal
High Resolution
Ultrasonic Recent Year
2013
Ultrasonic Rcnt Propul Method
Free Swimming
Ultrasonic Rcnt Attuned
Wall Measurement
Utra Rcnt Att Metl Resolution
Other
Utra Rcnt Att Metl Res Dtls
Ump - High Resolution Suitable To Detect Pitting
Geometry Recent Year
2022
Geometry Rcnt Propul Method
Free Swimming
Geometry Rcnt Resolution
High Resolution
Geometrt Rcnt Measur Cups
Inside Ili Cups
Geometry Previous Year
2018
Geometry Prev Propul Method
Free Swimming
Geometry Prev Resolution
High Resolution
Geometrt Prev Measur Cups
Inside Ili Cups
Other Tool
Ultrasonic Crack Ili
Other Recent Year
2019
Other Rcnt Propul Method
Free Swimming
Other Previous Year
2016
Other Prev Propul Method
Free Swimming
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
2005
Hydrtst Most Rcnt Pressure
1213
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
S**** S****
Preparer Title
Advisor Regulatory Compliance
Preparer Email
S**********@e*******.com
Preparer Telephone
7153953620
Prepared Date
2023-10-17 00:00:00
Authorizer Name
L*** S**********
Authorizer Telephone
7153941584
Authorizer Title
Supervisor Regulatory Affairs Compliance
Authorizer Email
L***************@e*******.com
Narrative
On may 12, 2023, at approximately 7:36 am cdt, a pinhole leak developed on line 55 at mp 25.3071 after an integrity dig crew was sandblasting the area of pipe. The edmonton control center was immediately contacted, and the line was shut down at 7:39 am cdt. The excavation area was evacuated, and enbridge personnel and contractors were mobilized to the site for cleanup and repair. Approximately 2 barrels of crude oil was released and contained within the excavation area. The nrc was notified on may 12, 2023, at 8:42 am cdt (nrc# 1367051). A 48-hour update to the nrc was made on may 13, 2023, at 9:16 pm cdt (nrc# 1367191). The dig at mp 25.3 was issued on april 12, 2023, in response to a priority notification of a corrosion defect called by the december 2022 corrosion inline inspection. The pipe at mp 25.3 is located under a casing as it crosses interstate us39. A sleeve was installed on the pipe and the line was restarted on may 13, 2023, at 6:54 pm cdt. Approximately 53.18 tons of soil was removed from the release site and properly disposed of at an approved facility. A cut out was performed to aid in the investigation to determine a root cause. The results of the investigation indicated that the condensing atmosphere within the casing caused water to drip on the top of the carrier pipe, causing metal loss on the carrier pipe. This process was likely exacerbated by increased pipe operating temperature, as well as the formation of crevices between the pipe and the external coating that formed as corrosion progressed.
Report Received Date 2023-06-09 00:00:00
Iyear 2023
Report Number 20230124
Supplemental Number 38672
Report Type Supplemental Final
Operator Id 32080 PHMSA Enforcement
Name Ccps Transportation, Llc
Operator Street Address 915 N Eldridge Parkway, Suite 1100
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77079
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 40.74448695 Google Maps OpenStreetMap
Location Longitude -89.03489181 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 2
Recovered Bbls 2
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind Yes
Communication State Fed Ind No
Nrc Rpt Num 1367051 NRC Report How to search
Additional Nrc Report Numbers 1367191
Ignite Ind No
Upstream Action Taken Valve Closure
Upstream Valve Type Ind Remotely Controlled
Downstream Action Taken Valve Closure
Downstream Valve Type Ind Remotely Controlled
Notify Qualified Indiv Ind Yes
Oil Spill Removal Org Ind Yes
Osro Arrived On Site Dt 5/12/2023 11:30
Num Pub Evacuated 0
Pipe Fac Name Line 55
Segment Name Mp 25.3
Onshore State Abbreviation Il
Onshore Postal Code 61738
Onshore City Name El Paso
Onshore County Name Woodford
Designated Location Milepost
Designated Name 25.3
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Exposed Due To Excavation
Depth Of Cover 54
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Puddle Weld Ind No
Pipe Diameter 22
Pipe Wall Thickness 0.312
Pipe Smys 46000
Pipe Specification X46
Pipe Seam Type Seamless
Pipe Manufacturer National Tube
Pipe Coating Type Coal Tar
Coating Applied Ind No
Installation Year 1953
Manufactured Year 1953
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 150
Est Cost Prop Damage 111800
Est Cost Emergency 20000
Est Cost Environmental 191455
Est Cost Other 0
Prpty 323405
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 389
Mop Psig 939
Mop Cfr Section Internal Design Pressure �195.406(A)(1) View CFR 49 §192
Maop Established Date 2005-08-11 00:00:00
Maop Reversal Flow Ind Yes
Surge Analysis Date 2022-04-28 00:00:00
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind Yes
Exceed Restriction Ind No
Phmsa Restriction Ind Not Mandated
Length Segment Isolated 209721
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details External Corrosion
Internal External External Corrosion
Visual Exam Results Other
Visual Exam Details Pinhole
Atmosphere Corrosion Ind Yes
Other Corrosion Ind Yes
Corrosion Type Details Inside Casing
Field Exam Basis Ind Yes
Other Basis Ind Yes
Corrosion Basis Details Engineering Analysis And Lab Testing
Underground Location No
Externally Coated Yes
Prior Damage Yes
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Ultrasonic Ind Yes
Geometry Deformation Ind Yes
Other Tool Tech Ind Yes
Axial Recent Year 2022
Axial Rcnt Propul Method Free Swimming
Axial Rcnt Attuned Detect Metal Loss
Axial Rcnt Atnd Dtct Metal High Resolution
Axial Previous Year 2018
Axial Prev Propul Method Free Swimming
Axial Prev Attuned Detect Metal Loss
Axial Prev Atnd Dtct Metal High Resolution
Ultrasonic Recent Year 2013
Ultrasonic Rcnt Propul Method Free Swimming
Ultrasonic Rcnt Attuned Wall Measurement
Utra Rcnt Att Metl Resolution Other
Utra Rcnt Att Metl Res Dtls Ump - High Resolution Suitable To Detect Pitting
Geometry Recent Year 2022
Geometry Rcnt Propul Method Free Swimming
Geometry Rcnt Resolution High Resolution
Geometrt Rcnt Measur Cups Inside Ili Cups
Geometry Previous Year 2018
Geometry Prev Propul Method Free Swimming
Geometry Prev Resolution High Resolution
Geometrt Prev Measur Cups Inside Ili Cups
Other Tool Ultrasonic Crack Ili
Other Recent Year 2019
Other Rcnt Propul Method Free Swimming
Other Previous Year 2016
Other Prev Propul Method Free Swimming
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 2005
Hydrtst Most Rcnt Pressure 1213
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name S**** S****
Preparer Title Advisor Regulatory Compliance
Preparer Email S**********@e*******.com
Preparer Telephone 7153953620
Prepared Date 2023-10-17 00:00:00
Authorizer Name L*** S**********
Authorizer Telephone 7153941584
Authorizer Title Supervisor Regulatory Affairs Compliance
Authorizer Email L***************@e*******.com
Narrative On may 12, 2023, at approximately 7:36 am cdt, a pinhole leak developed on line 55 at mp 25.3071 after an integrity dig crew was sandblasting the area of pipe. The edmonton control center was immediately contacted, and the line was shut down at 7:39 am cdt. The excavation area was evacuated, and enbridge personnel and contractors were mobilized to the site for cleanup and repair. Approximately 2 barrels of crude oil was released and contained within the excavation area. The nrc was notified on may 12, 2023, at 8:42 am cdt (nrc# 1367051). A 48-hour update to the nrc was made on may 13, 2023, at 9:16 pm cdt (nrc# 1367191). The dig at mp 25.3 was issued on april 12, 2023, in response to a priority notification of a corrosion defect called by the december 2022 corrosion inline inspection. The pipe at mp 25.3 is located under a casing as it crosses interstate us39. A sleeve was installed on the pipe and the line was restarted on may 13, 2023, at 6:54 pm cdt. Approximately 53.18 tons of soil was removed from the release site and properly disposed of at an approved facility. A cut out was performed to aid in the investigation to determine a root cause. The results of the investigation indicated that the condensing atmosphere within the casing caused water to drip on the top of the carrier pipe, causing metal loss on the carrier pipe. This process was likely exacerbated by increased pipe operating temperature, as well as the formation of crevices between the pipe and the external coating that formed as corrosion progressed.

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