GTG incident on 2023-12-15 — TX

Operator
Wwm Operating, Llc
Cause
Notification Issue
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$246,909
Incident datetime
2023-12-15 00:00 UTC
Report number
Location
TX
Narrative
Permian anchors was drilling new anchors at a location approximately 4,600 feet from the location indicated on the one call ticket placed. Due to this misinformation, wwm operating, llc was not listed on the operators to clear the one call ticket. The excavator hit the pipeline and notified the operator he was working for. The operator called the emergency number on the wwm operating, llc pipeline markers and notified gas control. Wwm operating, llc determined it had punctured the pipeline and was leaking gas. Upstream and downstream mlvs were closed to isolate the damaged section of pipe. Damaged section of pipe was depressurized and repaired before returning to service. Permian anchor was contracted by chevron. A representative of chevron informed wwm control room of line strike on 11/16/2020 at 13:52 central time.
Detailed record list
Report Received Date
2023-12-15 00:00:00
Iyear
2023
Report Number
20230116
Supplemental Number
39100
Report Type
Supplemental Final
Operator Id
Name
Wwm Operating, Llc
Operator Street Address
100 Congress Ave Suite 2200
Operator City Name
Austin
Operator State Abbreviation
TX
Operator Postal Code
78701
Time Zone
Central
Daylight Savings Ind
No
Location Latitude
Location Longitude
Nrc Rpt Num
Additional Nrc Report Numbers
1384630
Commodity Released Type
Natural Gas
Unintentional Release
0
Intentional Release
39006
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Status When Identified
Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind
Yes
Communication State Fed Ind
No
Ignite Ind
No
Upstream Action Taken
Valve Closure
Downstream Action Taken
Valve Closure
Num Pub Evacuated
0
On Off Shore
Onshore
Onshore State Abbreviation
Tx
Onshore Postal Code
79777
Onshore City Name
Not Within A Municipality
Onshore County Name
Ward
Designated Location
Survey Station No.
Designated Name
2170
Pipe Fac Name
Ab 36"
Segment Name
Waha Connector
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
52
Other Underground Facilities
No
Crossing
No
Pipe Facility Type
Intrastate
System Part Involved
Onshore Pipeline, Including Valve Sites
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
36
Puddle Weld Ind
No
Pipe Wall Thickness
0.469
Pipe Smys
70000
Pipe Specification
Api-5l
Pipe Seam Type
Single Saw
Pipe Manufacturer
Welspun
Pipe Coating Type
Epoxy
Coating Applied Ind
No
Installation Year
2018
Manufactured Year
2014
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
Crack Caused By Tpd
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
900
Heat Damage Ind
No
Non Heat Damage Ind
No
Did Occur In Mca Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
0
Est Cost Intentional Release
91664
Est Cost Prop Damage
246909
Est Cost Emergency
0
Est Cost Other
25000
Est Cost Other Details
Audit And Recordkeeping Post Repair.
Gas Cost In Mcf
2.35
Prpty
363573
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Wildlife Impact Ind
No
Accident Psig
960
Gas Flow In Pipe In Mcf
1011578
Mop Psig
1313
Mop Cfr Section
192.619(A)(1)
Maop Established Date
2017-09-30 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Gas Required Odorized Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Length Segment Isolated
88872
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Notification From Third Party That Caused The Incident
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
No
State Law Exempt Ind
No
Notify Cga Dirt
No
Private Row Ind
Yes
Private Subtype
Private Landowner
Joint Trench Ind
No
Cross Bore Ind
No
Depth Of Grade
> 36�
Excavator Type
Contractor
Excavator Equipment
Auger
Work Performed
Unknown/other
One Call Notified Ind
No
Locator Type
Unknown/other
Visible Marks
Unknown/other
Service Interruption
Yes
Service Interruption Hours
68
Root Cause Category
Notification Issue
Root Cause Type
Excavator Provided Incorrect Notification Information
Excvtn Dmg Third Party Ind
Yes
Preparer Name
S***** M****
Preparer Title
Sr. Regulatory Compliance Specialist
Preparer Email
S*****@w******.com
Preparer Telephone
2816395423
Local Contact Name
J**** G*******
Local Contact Email
J****@w******.com
Local Contact Telephone
4325561348
Authorizer Name
T***** A******
Authorizer Title
Director Of Operations
Authorizer Telephone
432-425-9761
Authorizer Email
T*****@w******.com
Narrative
Permian anchors was drilling new anchors at a location approximately 4,600 feet from the location indicated on the one call ticket placed. Due to this misinformation, wwm operating, llc was not listed on the operators to clear the one call ticket. The excavator hit the pipeline and notified the operator he was working for. The operator called the emergency number on the wwm operating, llc pipeline markers and notified gas control. Wwm operating, llc determined it had punctured the pipeline and was leaking gas. Upstream and downstream mlvs were closed to isolate the damaged section of pipe. Damaged section of pipe was depressurized and repaired before returning to service. Permian anchor was contracted by chevron. A representative of chevron informed wwm control room of line strike on 11/16/2020 at 13:52 central time.
Report Received Date 2023-12-15 00:00:00
Iyear 2023
Report Number 20230116
Supplemental Number 39100
Report Type Supplemental Final
Operator Id 39572 PHMSA Enforcement
Name Wwm Operating, Llc
Operator Street Address 100 Congress Ave Suite 2200
Operator City Name Austin
Operator State Abbreviation TX
Operator Postal Code 78701
Time Zone Central
Daylight Savings Ind No
Location Latitude 31.47144 Google Maps OpenStreetMap
Location Longitude -103.18876 Google Maps OpenStreetMap
Nrc Rpt Num 1384497 NRC Report How to search
Additional Nrc Report Numbers 1384630
Commodity Released Type Natural Gas
Unintentional Release 0
Intentional Release 39006
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Status When Identified Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind Yes
Communication State Fed Ind No
Ignite Ind No
Upstream Action Taken Valve Closure
Downstream Action Taken Valve Closure
Num Pub Evacuated 0
On Off Shore Onshore
Onshore State Abbreviation Tx
Onshore Postal Code 79777
Onshore City Name Not Within A Municipality
Onshore County Name Ward
Designated Location Survey Station No.
Designated Name 2170
Pipe Fac Name Ab 36"
Segment Name Waha Connector
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 52
Other Underground Facilities No
Crossing No
Pipe Facility Type Intrastate
System Part Involved Onshore Pipeline, Including Valve Sites
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 36
Puddle Weld Ind No
Pipe Wall Thickness 0.469
Pipe Smys 70000
Pipe Specification Api-5l
Pipe Seam Type Single Saw
Pipe Manufacturer Welspun
Pipe Coating Type Epoxy
Coating Applied Ind No
Installation Year 2018
Manufactured Year 2014
Material Involved Carbon Steel
Release Type Leak
Leak Type Other
Leak Type Other Crack Caused By Tpd
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 900
Heat Damage Ind No
Non Heat Damage Ind No
Did Occur In Mca Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 0
Est Cost Intentional Release 91664
Est Cost Prop Damage 246909
Est Cost Emergency 0
Est Cost Other 25000
Est Cost Other Details Audit And Recordkeeping Post Repair.
Gas Cost In Mcf 2.35
Prpty 363573
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Wildlife Impact Ind No
Accident Psig 960
Gas Flow In Pipe In Mcf 1011578
Mop Psig 1313
Mop Cfr Section 192.619(A)(1) View CFR 49 §192
Maop Established Date 2017-09-30 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Gas Required Odorized Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Length Segment Isolated 88872
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Accident Identifier Notification From Third Party That Caused The Incident
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind No
State Law Exempt Ind No
Notify Cga Dirt No
Private Row Ind Yes
Private Subtype Private Landowner
Joint Trench Ind No
Cross Bore Ind No
Depth Of Grade > 36�
Excavator Type Contractor
Excavator Equipment Auger
Work Performed Unknown/other
One Call Notified Ind No
Locator Type Unknown/other
Visible Marks Unknown/other
Service Interruption Yes
Service Interruption Hours 68
Root Cause Category Notification Issue
Root Cause Type Excavator Provided Incorrect Notification Information
Excvtn Dmg Third Party Ind Yes
Preparer Name S***** M****
Preparer Title Sr. Regulatory Compliance Specialist
Preparer Email S*****@w******.com
Preparer Telephone 2816395423
Local Contact Name J**** G*******
Local Contact Email J****@w******.com
Local Contact Telephone 4325561348
Authorizer Name T***** A******
Authorizer Title Director Of Operations
Authorizer Telephone 432-425-9761
Authorizer Email T*****@w******.com
Narrative Permian anchors was drilling new anchors at a location approximately 4,600 feet from the location indicated on the one call ticket placed. Due to this misinformation, wwm operating, llc was not listed on the operators to clear the one call ticket. The excavator hit the pipeline and notified the operator he was working for. The operator called the emergency number on the wwm operating, llc pipeline markers and notified gas control. Wwm operating, llc determined it had punctured the pipeline and was leaking gas. Upstream and downstream mlvs were closed to isolate the damaged section of pipe. Damaged section of pipe was depressurized and repaired before returning to service. Permian anchor was contracted by chevron. A representative of chevron informed wwm control room of line strike on 11/16/2020 at 13:52 central time.

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