Incident details
Operator, cause, commodity and consequences with raw source fields.
GTG incident on 2023-12-15 — TX
Operator
Wwm Operating, Llc
Cause
Notification Issue
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$246,909
Incident datetime
2023-12-15 00:00 UTC
Report number
Location
TX
Narrative
Permian anchors was drilling new anchors at a location approximately 4,600 feet from the location indicated on the one call ticket placed. Due to this misinformation, wwm operating, llc was not listed on the operators to clear the one call ticket. The excavator hit the pipeline and notified the operator he was working for. The operator called the emergency number on the wwm operating, llc pipeline markers and notified gas control. Wwm operating, llc determined it had punctured the pipeline and was leaking gas. Upstream and downstream mlvs were closed to isolate the damaged section of pipe. Damaged section of pipe was depressurized and repaired before returning to service. Permian anchor was contracted by chevron. A representative of chevron informed wwm control room of line strike on 11/16/2020 at 13:52 central time.
Detailed record list
Report Received Date
2023-12-15 00:00:00
Iyear
2023
Report Number
20230116
Supplemental Number
39100
Report Type
Supplemental Final
Operator Id
39572
Name
Wwm Operating, Llc
Operator Street Address
100 Congress Ave Suite 2200
Operator City Name
Austin
Operator State Abbreviation
TX
Operator Postal Code
78701
Time Zone
Central
Daylight Savings Ind
No
Location Latitude
31.47144
Location Longitude
-103.18876
Nrc Rpt Num
1384497
Additional Nrc Report Numbers
1384630
Commodity Released Type
Natural Gas
Unintentional Release
0
Intentional Release
39006
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Status When Identified
Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind
Yes
Communication State Fed Ind
No
Ignite Ind
No
Upstream Action Taken
Valve Closure
Downstream Action Taken
Valve Closure
Num Pub Evacuated
0
On Off Shore
Onshore
Onshore State Abbreviation
Tx
Onshore Postal Code
79777
Onshore City Name
Not Within A Municipality
Onshore County Name
Ward
Designated Location
Survey Station No.
Designated Name
2170
Pipe Fac Name
Ab 36"
Segment Name
Waha Connector
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
52
Other Underground Facilities
No
Crossing
No
Pipe Facility Type
Intrastate
System Part Involved
Onshore Pipeline, Including Valve Sites
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
36
Puddle Weld Ind
No
Pipe Wall Thickness
0.469
Pipe Smys
70000
Pipe Specification
Api-5l
Pipe Seam Type
Single Saw
Pipe Manufacturer
Welspun
Pipe Coating Type
Epoxy
Coating Applied Ind
No
Installation Year
2018
Manufactured Year
2014
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
Crack Caused By Tpd
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
900
Heat Damage Ind
No
Non Heat Damage Ind
No
Did Occur In Mca Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
0
Est Cost Intentional Release
91664
Est Cost Prop Damage
246909
Est Cost Emergency
0
Est Cost Other
25000
Est Cost Other Details
Audit And Recordkeeping Post Repair.
Gas Cost In Mcf
2.35
Prpty
363573
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Wildlife Impact Ind
No
Accident Psig
960
Gas Flow In Pipe In Mcf
1011578
Mop Psig
1313
Mop Cfr Section
192.619(A)(1)
Maop Established Date
2017-09-30 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Gas Required Odorized Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Length Segment Isolated
88872
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Notification From Third Party That Caused The Incident
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
No
State Law Exempt Ind
No
Notify Cga Dirt
No
Private Row Ind
Yes
Private Subtype
Private Landowner
Joint Trench Ind
No
Cross Bore Ind
No
Depth Of Grade
> 36�
Excavator Type
Contractor
Excavator Equipment
Auger
Work Performed
Unknown/other
One Call Notified Ind
No
Locator Type
Unknown/other
Visible Marks
Unknown/other
Service Interruption
Yes
Service Interruption Hours
68
Root Cause Category
Notification Issue
Root Cause Type
Excavator Provided Incorrect Notification Information
Excvtn Dmg Third Party Ind
Yes
Preparer Name
S***** M****
Preparer Title
Sr. Regulatory Compliance Specialist
Preparer Email
S*****@w******.com
Preparer Telephone
2816395423
Local Contact Name
J**** G*******
Local Contact Email
J****@w******.com
Local Contact Telephone
4325561348
Authorizer Name
T***** A******
Authorizer Title
Director Of Operations
Authorizer Telephone
432-425-9761
Authorizer Email
T*****@w******.com
Narrative
Permian anchors was drilling new anchors at a location approximately 4,600 feet from the location indicated on the one call ticket placed. Due to this misinformation, wwm operating, llc was not listed on the operators to clear the one call ticket. The excavator hit the pipeline and notified the operator he was working for. The operator called the emergency number on the wwm operating, llc pipeline markers and notified gas control. Wwm operating, llc determined it had punctured the pipeline and was leaking gas. Upstream and downstream mlvs were closed to isolate the damaged section of pipe. Damaged section of pipe was depressurized and repaired before returning to service. Permian anchor was contracted by chevron. A representative of chevron informed wwm control room of line strike on 11/16/2020 at 13:52 central time.
Report Received Date | 2023-12-15 00:00:00 |
---|---|
Iyear | 2023 |
Report Number | 20230116 |
Supplemental Number | 39100 |
Report Type | Supplemental Final |
Operator Id | 39572 PHMSA Enforcement |
Name | Wwm Operating, Llc |
Operator Street Address | 100 Congress Ave Suite 2200 |
Operator City Name | Austin |
Operator State Abbreviation | TX |
Operator Postal Code | 78701 |
Time Zone | Central |
Daylight Savings Ind | No |
Location Latitude | 31.47144 Google Maps OpenStreetMap |
Location Longitude | -103.18876 Google Maps OpenStreetMap |
Nrc Rpt Num | 1384497 NRC Report How to search |
Additional Nrc Report Numbers | 1384630 |
Commodity Released Type | Natural Gas |
Unintentional Release | 0 |
Intentional Release | 39006 |
Accompanying Liquid | 0 |
Fatality Ind | No |
Fatal | 0 |
Injury Ind | No |
Injure | 0 |
Status When Identified | Normal Operation, Includes Pauses During Maintenance |
Shutdown Due Accident Ind | Yes |
Communication State Fed Ind | No |
Ignite Ind | No |
Upstream Action Taken | Valve Closure |
Downstream Action Taken | Valve Closure |
Num Pub Evacuated | 0 |
On Off Shore | Onshore |
Onshore State Abbreviation | Tx |
Onshore Postal Code | 79777 |
Onshore City Name | Not Within A Municipality |
Onshore County Name | Ward |
Designated Location | Survey Station No. |
Designated Name | 2170 |
Pipe Fac Name | Ab 36" |
Segment Name | Waha Connector |
Federal | No |
Location Type | Pipeline Right-Of-Way |
Incident Area Type | Underground |
Incident Area Subtype | Under Soil |
Depth Of Cover | 52 |
Other Underground Facilities | No |
Crossing | No |
Pipe Facility Type | Intrastate |
System Part Involved | Onshore Pipeline, Including Valve Sites |
Item Involved | Pipe |
Pipe Type | Pipe Body |
Pipe Diameter | 36 |
Puddle Weld Ind | No |
Pipe Wall Thickness | 0.469 |
Pipe Smys | 70000 |
Pipe Specification | Api-5l |
Pipe Seam Type | Single Saw |
Pipe Manufacturer | Welspun |
Pipe Coating Type | Epoxy |
Coating Applied Ind | No |
Installation Year | 2018 |
Manufactured Year | 2014 |
Material Involved | Carbon Steel |
Release Type | Leak |
Leak Type | Other |
Leak Type Other | Crack Caused By Tpd |
Class Location Type | Class 1 Location |
Could Be Hca | No |
Pir Radius | 900 |
Heat Damage Ind | No |
Non Heat Damage Ind | No |
Did Occur In Mca Ind | No |
Est Cost Oper Paid | 0 |
Est Cost Unintentional Release | 0 |
Est Cost Intentional Release | 91664 |
Est Cost Prop Damage | 246909 |
Est Cost Emergency | 0 |
Est Cost Other | 25000 |
Est Cost Other Details | Audit And Recordkeeping Post Repair. |
Gas Cost In Mcf | 2.35 |
Prpty | 363573 |
Num Persons Hosp Not Ovnght | 0 |
Num Injured Treated By Emt | 0 |
Num Resident Building Affctd | 0 |
Num Business Building Affctd | 0 |
Wildlife Impact Ind | No |
Accident Psig | 960 |
Gas Flow In Pipe In Mcf | 1011578 |
Mop Psig | 1313 |
Mop Cfr Section | 192.619(A)(1) View CFR 49 §192 |
Maop Established Date | 2017-09-30 00:00:00 |
Maop Reversal Flow Ind | No |
Accident Pressure | Pressure Did Not Exceed Maop |
Pressure Restriction Ind | No |
Gas Required Odorized Ind | No |
Upstream Valve Type Ind | Manual |
Downstream Valve Type Ind | Manual |
Length Segment Isolated | 88872 |
Internal Inspection Ind | Yes |
Operation Complications Ind | No |
Pipeline Function | Transmission System |
Scada In Place Ind | Yes |
Scada Operating Ind | Yes |
Scada Functional Ind | Yes |
Scada Detection Ind | No |
Scada Conf Ind | No |
Accident Identifier | Notification From Third Party That Caused The Incident |
Investigation Status | Yes, specify investigation result(s): (select all that apply) |
Invest No Control Room Ind | Yes |
Invest No Controller Ind | Yes |
Employee Drug Test Ind | No |
Contractor Drug Test Ind | No |
Cause | Excavation Damage |
Cause Details | Excavation Damage By Third Party |
Ex Party Type | Excavation Damage By Third Party |
Prior Notification Ind | No |
State Law Exempt Ind | No |
Notify Cga Dirt | No |
Private Row Ind | Yes |
Private Subtype | Private Landowner |
Joint Trench Ind | No |
Cross Bore Ind | No |
Depth Of Grade | > 36� |
Excavator Type | Contractor |
Excavator Equipment | Auger |
Work Performed | Unknown/other |
One Call Notified Ind | No |
Locator Type | Unknown/other |
Visible Marks | Unknown/other |
Service Interruption | Yes |
Service Interruption Hours | 68 |
Root Cause Category | Notification Issue |
Root Cause Type | Excavator Provided Incorrect Notification Information |
Excvtn Dmg Third Party Ind | Yes |
Preparer Name | S***** M**** |
Preparer Title | Sr. Regulatory Compliance Specialist |
Preparer Email | S*****@w******.com |
Preparer Telephone | 2816395423 |
Local Contact Name | J**** G******* |
Local Contact Email | J****@w******.com |
Local Contact Telephone | 4325561348 |
Authorizer Name | T***** A****** |
Authorizer Title | Director Of Operations |
Authorizer Telephone | 432-425-9761 |
Authorizer Email | T*****@w******.com |
Narrative | Permian anchors was drilling new anchors at a location approximately 4,600 feet from the location indicated on the one call ticket placed. Due to this misinformation, wwm operating, llc was not listed on the operators to clear the one call ticket. The excavator hit the pipeline and notified the operator he was working for. The operator called the emergency number on the wwm operating, llc pipeline markers and notified gas control. Wwm operating, llc determined it had punctured the pipeline and was leaking gas. Upstream and downstream mlvs were closed to isolate the damaged section of pipe. Damaged section of pipe was depressurized and repaired before returning to service. Permian anchor was contracted by chevron. A representative of chevron informed wwm control room of line strike on 11/16/2020 at 13:52 central time. |
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