GTG incident on 2023-12-05 — TX

Operator
M6 Midstream Llc
Cause
Notification Issue
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$75,500
Incident datetime
2023-12-05 00:00 UTC
Report number
Location
TX
Narrative
The landowner (mr. Danny spencer) was conducting grading activities across a drainage ditch on his property, when he struck an active m6 midstream llc, natural gas gathering pipeline. The excavation activities resulted in a puncture of the affected gathering pipeline and resulted in natural gas and associated condensate/produced water to be released to the atmosphere and surrounding area. Due to mr. Spencer's grading activities, there was no way to know the depth of the pipe prior to the excavation. There was a pipeline sign near the area that appeared to have been removed from the row, approximately 300 feet from the line strike. The affected pipeline was isolated and blown down and the damaged section has been removed from service.
Detailed record list
Report Received Date
2023-12-05 00:00:00
Iyear
2023
Report Number
20230111
Supplemental Number
39099
Report Type
Supplemental Final
Operator Id
Name
M6 Midstream Llc
Operator Street Address
600 Travis Suite 5500
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Time Zone
Central
Daylight Savings Ind
No
Location Latitude
Location Longitude
Nrc Rpt Num
Additional Nrc Report Numbers
1383821, 1383957
Commodity Released Type
Natural Gas
Unintentional Release
108
Intentional Release
89
Accompanying Liquid
10
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Status When Identified
Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind
Yes
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Ignite Ind
No
Upstream Action Taken
Valve Closure
Downstream Action Taken
Valve Closure
Num Pub Evacuated
0
On Off Shore
Onshore
Onshore State Abbreviation
Tx
Onshore Postal Code
75644
Onshore City Name
Gilmer
Onshore County Name
Upshur
Designated Location
Survey Station No.
Designated Name
7+19
Pipe Fac Name
Rosewood System
Segment Name
Rw-08-09
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
4
Other Underground Facilities
No
Crossing
No
Pipe Facility Type
Intrastate
System Part Involved
Onshore Pipeline, Including Valve Sites
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
4.5
Puddle Weld Ind
No
Pipe Wall Thickness
0.13
Pipe Smys
Unknown
Pipe Specification
Unknown
Pipe Seam Type
Longitudinal Erw - Unknown Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
Coal Tar
Coating Applied Ind
Unknown
Installation Year
Unknown
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Mechanical Puncture
Puncture Axial
0.5
Puncture Circum
0.5
Class Location Type
Class 2 Location
Could Be Hca
No
Pir Radius
107
Heat Damage Ind
No
Non Heat Damage Ind
No
Did Occur In Mca Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
235
Est Cost Intentional Release
194
Est Cost Prop Damage
75500
Est Cost Emergency
5000
Est Cost Other
0
Gas Cost In Mcf
2.18
Prpty
80929
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Wildlife Impact Ind
No
Accident Psig
160
Gas Flow In Pipe In Mcf
1100
Mop Psig
1186
Mop Cfr Section
192.619(A)(1)
Maop Established Date
1978-02-16 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Gas Required Odorized Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Length Segment Isolated
17396
Internal Inspection Ind
No
Diameter Change Ind
Yes
Unsuitable Mainline Ind
Yes
Operation Complications Ind
Yes
Low Op Pressure Ind
Yes
Low Flow Ind
Yes
Pipeline Function
Type A Gathering
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Notification From Third Party That Caused The Incident
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Contributing factors were not due to a control room issue. Incident was due to a person of the public excavating on m6 midstream llc right-of-way, without notifying a 811 (locate ticket) system.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
No
State Law Exempt Ind
No
Notify Cga Dirt
No
Private Row Ind
Yes
Private Subtype
Private Landowner
Pipeline Easement Row Ind
Yes
Joint Trench Ind
No
Cross Bore Ind
No
Depth Of Grade
< 18�
Excavator Type
Farmer
Excavator Equipment
Bulldozer
Work Performed
Grading
One Call Notified Ind
No
Locator Type
Unknown/other
Visible Marks
Unknown/other
Service Interruption
Yes
Service Interruption Hours
191
Root Cause Category
Notification Issue
Root Cause Type
No Notification Made To The One-Call Center/811
Preparer Name
R*** R*********
Preparer Title
Compliance Coordinator
Preparer Email
R**************@m****************.com
Preparer Telephone
9033234304
Authorizer Name
R*** R*********
Authorizer Title
Compliance Coordinator
Authorizer Telephone
9033234304
Authorizer Email
R**************@m****************.com
Narrative
The landowner (mr. Danny spencer) was conducting grading activities across a drainage ditch on his property, when he struck an active m6 midstream llc, natural gas gathering pipeline. The excavation activities resulted in a puncture of the affected gathering pipeline and resulted in natural gas and associated condensate/produced water to be released to the atmosphere and surrounding area. Due to mr. Spencer's grading activities, there was no way to know the depth of the pipe prior to the excavation. There was a pipeline sign near the area that appeared to have been removed from the row, approximately 300 feet from the line strike. The affected pipeline was isolated and blown down and the damaged section has been removed from service.
Report Received Date 2023-12-05 00:00:00
Iyear 2023
Report Number 20230111
Supplemental Number 39099
Report Type Supplemental Final
Operator Id 31613 PHMSA Enforcement
Name M6 Midstream Llc
Operator Street Address 600 Travis Suite 5500
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Time Zone Central
Daylight Savings Ind No
Location Latitude 32.7772208 Google Maps OpenStreetMap
Location Longitude -95.0664501 Google Maps OpenStreetMap
Nrc Rpt Num 1383789 NRC Report How to search
Additional Nrc Report Numbers 1383821, 1383957
Commodity Released Type Natural Gas
Unintentional Release 108
Intentional Release 89
Accompanying Liquid 10
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Status When Identified Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind Yes
Communication State Fed Ind Yes
Party Initiated Communication Operator
Ignite Ind No
Upstream Action Taken Valve Closure
Downstream Action Taken Valve Closure
Num Pub Evacuated 0
On Off Shore Onshore
Onshore State Abbreviation Tx
Onshore Postal Code 75644
Onshore City Name Gilmer
Onshore County Name Upshur
Designated Location Survey Station No.
Designated Name 7+19
Pipe Fac Name Rosewood System
Segment Name Rw-08-09
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 4
Other Underground Facilities No
Crossing No
Pipe Facility Type Intrastate
System Part Involved Onshore Pipeline, Including Valve Sites
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 4.5
Puddle Weld Ind No
Pipe Wall Thickness 0.13
Pipe Smys Unknown
Pipe Specification Unknown
Pipe Seam Type Longitudinal Erw - Unknown Frequency
Pipe Manufacturer Unknown
Pipe Coating Type Coal Tar
Coating Applied Ind Unknown
Installation Year Unknown
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Mechanical Puncture
Puncture Axial 0.5
Puncture Circum 0.5
Class Location Type Class 2 Location
Could Be Hca No
Pir Radius 107
Heat Damage Ind No
Non Heat Damage Ind No
Did Occur In Mca Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 235
Est Cost Intentional Release 194
Est Cost Prop Damage 75500
Est Cost Emergency 5000
Est Cost Other 0
Gas Cost In Mcf 2.18
Prpty 80929
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Wildlife Impact Ind No
Accident Psig 160
Gas Flow In Pipe In Mcf 1100
Mop Psig 1186
Mop Cfr Section 192.619(A)(1) View CFR 49 §192
Maop Established Date 1978-02-16 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Gas Required Odorized Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Length Segment Isolated 17396
Internal Inspection Ind No
Diameter Change Ind Yes
Unsuitable Mainline Ind Yes
Operation Complications Ind Yes
Low Op Pressure Ind Yes
Low Flow Ind Yes
Pipeline Function Type A Gathering
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Accident Identifier Notification From Third Party That Caused The Incident
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Contributing factors were not due to a control room issue. Incident was due to a person of the public excavating on m6 midstream llc right-of-way, without notifying a 811 (locate ticket) system.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind No
State Law Exempt Ind No
Notify Cga Dirt No
Private Row Ind Yes
Private Subtype Private Landowner
Pipeline Easement Row Ind Yes
Joint Trench Ind No
Cross Bore Ind No
Depth Of Grade < 18�
Excavator Type Farmer
Excavator Equipment Bulldozer
Work Performed Grading
One Call Notified Ind No
Locator Type Unknown/other
Visible Marks Unknown/other
Service Interruption Yes
Service Interruption Hours 191
Root Cause Category Notification Issue
Root Cause Type No Notification Made To The One-Call Center/811
Preparer Name R*** R*********
Preparer Title Compliance Coordinator
Preparer Email R**************@m****************.com
Preparer Telephone 9033234304
Authorizer Name R*** R*********
Authorizer Title Compliance Coordinator
Authorizer Telephone 9033234304
Authorizer Email R**************@m****************.com
Narrative The landowner (mr. Danny spencer) was conducting grading activities across a drainage ditch on his property, when he struck an active m6 midstream llc, natural gas gathering pipeline. The excavation activities resulted in a puncture of the affected gathering pipeline and resulted in natural gas and associated condensate/produced water to be released to the atmosphere and surrounding area. Due to mr. Spencer's grading activities, there was no way to know the depth of the pipe prior to the excavation. There was a pipeline sign near the area that appeared to have been removed from the row, approximately 300 feet from the line strike. The affected pipeline was isolated and blown down and the damaged section has been removed from service.

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