Incident details
Operator, cause, commodity and consequences with raw source fields.
GTG incident on 2023-12-05 — TX
Operator
M6 Midstream Llc
Cause
Notification Issue
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$75,500
Incident datetime
2023-12-05 00:00 UTC
Report number
Location
TX
Narrative
The landowner (mr. Danny spencer) was conducting grading activities across a drainage ditch on his property, when he struck an active m6 midstream llc, natural gas gathering pipeline. The excavation activities resulted in a puncture of the affected gathering pipeline and resulted in natural gas and associated condensate/produced water to be released to the atmosphere and surrounding area. Due to mr. Spencer's grading activities, there was no way to know the depth of the pipe prior to the excavation. There was a pipeline sign near the area that appeared to have been removed from the row, approximately 300 feet from the line strike. The affected pipeline was isolated and blown down and the damaged section has been removed from service.
Detailed record list
Report Received Date
2023-12-05 00:00:00
Iyear
2023
Report Number
20230111
Supplemental Number
39099
Report Type
Supplemental Final
Operator Id
31613
Name
M6 Midstream Llc
Operator Street Address
600 Travis Suite 5500
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Time Zone
Central
Daylight Savings Ind
No
Location Latitude
32.7772208
Location Longitude
-95.0664501
Nrc Rpt Num
1383789
Additional Nrc Report Numbers
1383821, 1383957
Commodity Released Type
Natural Gas
Unintentional Release
108
Intentional Release
89
Accompanying Liquid
10
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Status When Identified
Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind
Yes
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Ignite Ind
No
Upstream Action Taken
Valve Closure
Downstream Action Taken
Valve Closure
Num Pub Evacuated
0
On Off Shore
Onshore
Onshore State Abbreviation
Tx
Onshore Postal Code
75644
Onshore City Name
Gilmer
Onshore County Name
Upshur
Designated Location
Survey Station No.
Designated Name
7+19
Pipe Fac Name
Rosewood System
Segment Name
Rw-08-09
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
4
Other Underground Facilities
No
Crossing
No
Pipe Facility Type
Intrastate
System Part Involved
Onshore Pipeline, Including Valve Sites
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
4.5
Puddle Weld Ind
No
Pipe Wall Thickness
0.13
Pipe Smys
Unknown
Pipe Specification
Unknown
Pipe Seam Type
Longitudinal Erw - Unknown Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
Coal Tar
Coating Applied Ind
Unknown
Installation Year
Unknown
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Mechanical Puncture
Puncture Axial
0.5
Puncture Circum
0.5
Class Location Type
Class 2 Location
Could Be Hca
No
Pir Radius
107
Heat Damage Ind
No
Non Heat Damage Ind
No
Did Occur In Mca Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
235
Est Cost Intentional Release
194
Est Cost Prop Damage
75500
Est Cost Emergency
5000
Est Cost Other
0
Gas Cost In Mcf
2.18
Prpty
80929
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Wildlife Impact Ind
No
Accident Psig
160
Gas Flow In Pipe In Mcf
1100
Mop Psig
1186
Mop Cfr Section
192.619(A)(1)
Maop Established Date
1978-02-16 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Gas Required Odorized Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Length Segment Isolated
17396
Internal Inspection Ind
No
Diameter Change Ind
Yes
Unsuitable Mainline Ind
Yes
Operation Complications Ind
Yes
Low Op Pressure Ind
Yes
Low Flow Ind
Yes
Pipeline Function
Type A Gathering
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Notification From Third Party That Caused The Incident
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Contributing factors were not due to a control room issue. Incident was due to a person of the public excavating on m6 midstream llc right-of-way, without notifying a 811 (locate ticket) system.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
No
State Law Exempt Ind
No
Notify Cga Dirt
No
Private Row Ind
Yes
Private Subtype
Private Landowner
Pipeline Easement Row Ind
Yes
Joint Trench Ind
No
Cross Bore Ind
No
Depth Of Grade
< 18�
Excavator Type
Farmer
Excavator Equipment
Bulldozer
Work Performed
Grading
One Call Notified Ind
No
Locator Type
Unknown/other
Visible Marks
Unknown/other
Service Interruption
Yes
Service Interruption Hours
191
Root Cause Category
Notification Issue
Root Cause Type
No Notification Made To The One-Call Center/811
Preparer Name
R*** R*********
Preparer Title
Compliance Coordinator
Preparer Email
R**************@m****************.com
Preparer Telephone
9033234304
Authorizer Name
R*** R*********
Authorizer Title
Compliance Coordinator
Authorizer Telephone
9033234304
Authorizer Email
R**************@m****************.com
Narrative
The landowner (mr. Danny spencer) was conducting grading activities across a drainage ditch on his property, when he struck an active m6 midstream llc, natural gas gathering pipeline. The excavation activities resulted in a puncture of the affected gathering pipeline and resulted in natural gas and associated condensate/produced water to be released to the atmosphere and surrounding area. Due to mr. Spencer's grading activities, there was no way to know the depth of the pipe prior to the excavation. There was a pipeline sign near the area that appeared to have been removed from the row, approximately 300 feet from the line strike. The affected pipeline was isolated and blown down and the damaged section has been removed from service.
Report Received Date | 2023-12-05 00:00:00 |
---|---|
Iyear | 2023 |
Report Number | 20230111 |
Supplemental Number | 39099 |
Report Type | Supplemental Final |
Operator Id | 31613 PHMSA Enforcement |
Name | M6 Midstream Llc |
Operator Street Address | 600 Travis Suite 5500 |
Operator City Name | Houston |
Operator State Abbreviation | TX |
Operator Postal Code | 77002 |
Time Zone | Central |
Daylight Savings Ind | No |
Location Latitude | 32.7772208 Google Maps OpenStreetMap |
Location Longitude | -95.0664501 Google Maps OpenStreetMap |
Nrc Rpt Num | 1383789 NRC Report How to search |
Additional Nrc Report Numbers | 1383821, 1383957 |
Commodity Released Type | Natural Gas |
Unintentional Release | 108 |
Intentional Release | 89 |
Accompanying Liquid | 10 |
Fatality Ind | No |
Fatal | 0 |
Injury Ind | No |
Injure | 0 |
Status When Identified | Normal Operation, Includes Pauses During Maintenance |
Shutdown Due Accident Ind | Yes |
Communication State Fed Ind | Yes |
Party Initiated Communication | Operator |
Ignite Ind | No |
Upstream Action Taken | Valve Closure |
Downstream Action Taken | Valve Closure |
Num Pub Evacuated | 0 |
On Off Shore | Onshore |
Onshore State Abbreviation | Tx |
Onshore Postal Code | 75644 |
Onshore City Name | Gilmer |
Onshore County Name | Upshur |
Designated Location | Survey Station No. |
Designated Name | 7+19 |
Pipe Fac Name | Rosewood System |
Segment Name | Rw-08-09 |
Federal | No |
Location Type | Pipeline Right-Of-Way |
Incident Area Type | Underground |
Incident Area Subtype | Under Soil |
Depth Of Cover | 4 |
Other Underground Facilities | No |
Crossing | No |
Pipe Facility Type | Intrastate |
System Part Involved | Onshore Pipeline, Including Valve Sites |
Item Involved | Pipe |
Pipe Type | Pipe Body |
Pipe Diameter | 4.5 |
Puddle Weld Ind | No |
Pipe Wall Thickness | 0.13 |
Pipe Smys | Unknown |
Pipe Specification | Unknown |
Pipe Seam Type | Longitudinal Erw - Unknown Frequency |
Pipe Manufacturer | Unknown |
Pipe Coating Type | Coal Tar |
Coating Applied Ind | Unknown |
Installation Year | Unknown |
Manufactured Year | Unknown |
Material Involved | Carbon Steel |
Release Type | Mechanical Puncture |
Puncture Axial | 0.5 |
Puncture Circum | 0.5 |
Class Location Type | Class 2 Location |
Could Be Hca | No |
Pir Radius | 107 |
Heat Damage Ind | No |
Non Heat Damage Ind | No |
Did Occur In Mca Ind | No |
Est Cost Oper Paid | 0 |
Est Cost Unintentional Release | 235 |
Est Cost Intentional Release | 194 |
Est Cost Prop Damage | 75500 |
Est Cost Emergency | 5000 |
Est Cost Other | 0 |
Gas Cost In Mcf | 2.18 |
Prpty | 80929 |
Num Persons Hosp Not Ovnght | 0 |
Num Injured Treated By Emt | 0 |
Num Resident Building Affctd | 0 |
Num Business Building Affctd | 0 |
Wildlife Impact Ind | No |
Accident Psig | 160 |
Gas Flow In Pipe In Mcf | 1100 |
Mop Psig | 1186 |
Mop Cfr Section | 192.619(A)(1) View CFR 49 §192 |
Maop Established Date | 1978-02-16 00:00:00 |
Maop Reversal Flow Ind | No |
Accident Pressure | Pressure Did Not Exceed Maop |
Pressure Restriction Ind | No |
Gas Required Odorized Ind | No |
Upstream Valve Type Ind | Manual |
Downstream Valve Type Ind | Manual |
Length Segment Isolated | 17396 |
Internal Inspection Ind | No |
Diameter Change Ind | Yes |
Unsuitable Mainline Ind | Yes |
Operation Complications Ind | Yes |
Low Op Pressure Ind | Yes |
Low Flow Ind | Yes |
Pipeline Function | Type A Gathering |
Scada In Place Ind | Yes |
Scada Operating Ind | Yes |
Scada Functional Ind | Yes |
Scada Detection Ind | No |
Scada Conf Ind | No |
Accident Identifier | Notification From Third Party That Caused The Incident |
Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
Investigation Status Details | Contributing factors were not due to a control room issue. Incident was due to a person of the public excavating on m6 midstream llc right-of-way, without notifying a 811 (locate ticket) system. |
Employee Drug Test Ind | No |
Contractor Drug Test Ind | No |
Cause | Excavation Damage |
Cause Details | Excavation Damage By Third Party |
Ex Party Type | Excavation Damage By Third Party |
Prior Notification Ind | No |
State Law Exempt Ind | No |
Notify Cga Dirt | No |
Private Row Ind | Yes |
Private Subtype | Private Landowner |
Pipeline Easement Row Ind | Yes |
Joint Trench Ind | No |
Cross Bore Ind | No |
Depth Of Grade | < 18� |
Excavator Type | Farmer |
Excavator Equipment | Bulldozer |
Work Performed | Grading |
One Call Notified Ind | No |
Locator Type | Unknown/other |
Visible Marks | Unknown/other |
Service Interruption | Yes |
Service Interruption Hours | 191 |
Root Cause Category | Notification Issue |
Root Cause Type | No Notification Made To The One-Call Center/811 |
Preparer Name | R*** R********* |
Preparer Title | Compliance Coordinator |
Preparer Email | R**************@m****************.com |
Preparer Telephone | 9033234304 |
Authorizer Name | R*** R********* |
Authorizer Title | Compliance Coordinator |
Authorizer Telephone | 9033234304 |
Authorizer Email | R**************@m****************.com |
Narrative | The landowner (mr. Danny spencer) was conducting grading activities across a drainage ditch on his property, when he struck an active m6 midstream llc, natural gas gathering pipeline. The excavation activities resulted in a puncture of the affected gathering pipeline and resulted in natural gas and associated condensate/produced water to be released to the atmosphere and surrounding area. Due to mr. Spencer's grading activities, there was no way to know the depth of the pipe prior to the excavation. There was a pipeline sign near the area that appeared to have been removed from the row, approximately 300 feet from the line strike. The affected pipeline was isolated and blown down and the damaged section has been removed from service. |
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