Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2023-05-17 — OK
Operator
Magellan Terminals Holdings, Lp
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$20,000
Incident datetime
2023-05-17 00:00 UTC
Report number
Location
OK
Narrative
At 15:00 on april 17th, 2023 magellan operations personnel conducting daily facility inspections discovered product dripping from a pinhole in a low-flow section of the unit 6 header piping at cushing. The leak source was isolated and clean-up activities were initiated. The pipe was removed and found to have internal corrosion. The pipe was sent for metallurgical analysis; preliminary results indicate the presence of microbiologically induced corrosion at the site of the pinhole. Further analysis is underway to determine the specific strain(s) of bacteria present. To prevent re-occurrence the portion of the unit 6 header which contained the leak origin was removed, and blind flanges were installed in its place.
Detailed record list
Report Received Date
2023-05-17 00:00:00
Iyear
2023
Report Number
20230100
Supplemental Number
38061
Report Type
Original Final
Operator Id
31580
Name
Magellan Terminals Holdings, Lp
Operator Street Address
100 West 5th Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
35.946089
Location Longitude
-96.747961
Commodity Released Type
Crude Oil
Unintentional Release Bbls
5
Recovered Bbls
5
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Communication State Fed Ind
No
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Notify Qualified Indiv Ind
Yes
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Central Cushing
Segment Name
Fac Id 800
Onshore State Abbreviation
Ok
Onshore Postal Code
74023
Onshore City Name
Cushing
Onshore County Name
Payne
Designated Location
Milepost
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Puddle Weld Ind
No
Pipe Diameter
14
Pipe Wall Thickness
0.375
Pipe Smys
24000
Pipe Specification
Unknown
Pipe Seam Type
Seamless
Pipe Manufacturer
Unknown
Pipe Coating Type
Paint
Coating Applied Ind
Yes
Installation Year
Unknown
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
500
Est Cost Prop Damage
20000
Est Cost Emergency
7500
Est Cost Environmental
0
Est Cost Other
0
Prpty
28000
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
30
Mop Psig
275
Mop Cfr Section
Component Design Pressure �195.406(A)(2)
Maop Established Date
2011-01-01 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Not caused or contributed to by the controller.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Microbiological Ind
Yes
Int Metallurgical Basis Ind
Yes
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
No
Corrosion Lining
No
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
Not Applicable - Not Mainline Pipe
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Intrnl Cor Corrosive Cmdty Ind
Yes
Preparer Name
C******* R******
Preparer Title
Strategic Data Engineer
Preparer Email
C***************@m*********.com
Preparer Telephone
9185747065
Prepared Date
2023-05-17 00:00:00
Authorizer Name
T***** K***
Authorizer Telephone
9185747191
Authorizer Title
Supv. Integrity Mgmt And Regulatory Compliance
Authorizer Email
T**********@m*********.com
Narrative
At 15:00 on april 17th, 2023 magellan operations personnel conducting daily facility inspections discovered product dripping from a pinhole in a low-flow section of the unit 6 header piping at cushing. The leak source was isolated and clean-up activities were initiated. The pipe was removed and found to have internal corrosion. The pipe was sent for metallurgical analysis; preliminary results indicate the presence of microbiologically induced corrosion at the site of the pinhole. Further analysis is underway to determine the specific strain(s) of bacteria present. To prevent re-occurrence the portion of the unit 6 header which contained the leak origin was removed, and blind flanges were installed in its place.
Report Received Date | 2023-05-17 00:00:00 |
---|---|
Iyear | 2023 |
Report Number | 20230100 |
Supplemental Number | 38061 |
Report Type | Original Final |
Operator Id | 31580 PHMSA Enforcement |
Name | Magellan Terminals Holdings, Lp |
Operator Street Address | 100 West 5th Street |
Operator City Name | Tulsa |
Operator State Abbreviation | OK |
Operator Postal Code | 74103 |
Time Zone | Central |
Daylight Savings Ind | Yes |
Location Latitude | 35.946089 Google Maps OpenStreetMap |
Location Longitude | -96.747961 Google Maps OpenStreetMap |
Commodity Released Type | Crude Oil |
Unintentional Release Bbls | 5 |
Recovered Bbls | 5 |
Fatality Ind | No |
Fatal | 0 |
Injury Ind | No |
Injure | 0 |
Accident Identifier | Local Operating Personnel, Including Contractors |
Operator Type | Operator Employee |
System Part Involved | Onshore Pump/meter Station Equipment And Piping |
On Off Shore | Onshore |
Status When Identified | Normal Operation, Includes Pauses Between Batches And During Maintenance |
Shutdown Due Accident Ind | Yes |
Communication State Fed Ind | No |
Nrc Rpt Num | Nrc Notification Not Required NRC Report How to search |
Ignite Ind | No |
Notify Qualified Indiv Ind | Yes |
Oil Spill Removal Org Ind | No |
Num Pub Evacuated | 0 |
Pipe Fac Name | Central Cushing |
Segment Name | Fac Id 800 |
Onshore State Abbreviation | Ok |
Onshore Postal Code | 74023 |
Onshore City Name | Cushing |
Onshore County Name | Payne |
Designated Location | Milepost |
Designated Name | 0 |
Federal | No |
Location Type | Totally Contained On Operator-Controlled Property |
Incident Area Type | Aboveground |
Incident Area Subtype | Typical Aboveground Facility Piping Or Appurtenance |
Crossing | No |
Pipe Facility Type | Interstate |
Item Involved | Pipe |
Pipe Type | Pipe Body |
Puddle Weld Ind | No |
Pipe Diameter | 14 |
Pipe Wall Thickness | 0.375 |
Pipe Smys | 24000 |
Pipe Specification | Unknown |
Pipe Seam Type | Seamless |
Pipe Manufacturer | Unknown |
Pipe Coating Type | Paint |
Coating Applied Ind | Yes |
Installation Year | Unknown |
Manufactured Year | Unknown |
Material Involved | Carbon Steel |
Release Type | Leak |
Leak Type | Pinhole |
Wildlife Impact Ind | No |
Soil Contamination | No |
Long Term Assessment | No |
Remediation Ind | No |
Water Contam Ind | No |
Could Be Hca | No |
Commodity Reached Hca | No |
Est Cost Oper Paid | 0 |
Est Cost Gas Released | 500 |
Est Cost Prop Damage | 20000 |
Est Cost Emergency | 7500 |
Est Cost Environmental | 0 |
Est Cost Other | 0 |
Prpty | 28000 |
Num Persons Hosp Not Ovnght | 0 |
Num Injured Treated By Emt | 0 |
Num Resident Building Affctd | 0 |
Num Business Building Affctd | 0 |
Accident Psig | 30 |
Mop Psig | 275 |
Mop Cfr Section | Component Design Pressure �195.406(A)(2) View CFR 49 §192 |
Maop Established Date | 2011-01-01 00:00:00 |
Maop Reversal Flow Ind | No |
Accident Pressure | Pressure Did Not Exceed Mop |
Pressure Restriction Ind | No |
Pipeline Function | > 20% Smys Regulated Transmission |
Scada In Place Ind | Yes |
Scada Operating Ind | Yes |
Scada Functional Ind | Yes |
Scada Detection Ind | No |
Scada Conf Ind | No |
Cpm In Place Ind | Yes |
Cpm Operating Ind | Yes |
Cpm Functional Ind | Yes |
Cpm Detection Ind | No |
Cpm Conf Ind | No |
Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
Investigation Status Details | Not caused or contributed to by the controller. |
Employee Drug Test Ind | No |
Contractor Drug Test Ind | No |
Cause | Corrosion Failure |
Cause Details | Internal Corrosion |
Internal External | Internal Corrosion |
Int Visual Exam Results | Localized Pitting |
Int Microbiological Ind | Yes |
Int Metallurgical Basis Ind | Yes |
Int Low Point Pipe Loc Ind | Yes |
Corrosion Inhibitors | No |
Corrosion Lining | No |
Cleaning Dewatering | Not Applicable - Not Mainline Pipe |
Corrosion Coupons | Not Applicable - Not Mainline Pipe |
Collected Data Ind | No |
Has Hydrtst Conduc Before Ind | No |
Direct Asmnt Conducted | No |
Non Destructive Exam Ind | No |
Intrnl Cor Corrosive Cmdty Ind | Yes |
Preparer Name | C******* R****** |
Preparer Title | Strategic Data Engineer |
Preparer Email | C***************@m*********.com |
Preparer Telephone | 9185747065 |
Prepared Date | 2023-05-17 00:00:00 |
Authorizer Name | T***** K*** |
Authorizer Telephone | 9185747191 |
Authorizer Title | Supv. Integrity Mgmt And Regulatory Compliance |
Authorizer Email | T**********@m*********.com |
Narrative | At 15:00 on april 17th, 2023 magellan operations personnel conducting daily facility inspections discovered product dripping from a pinhole in a low-flow section of the unit 6 header piping at cushing. The leak source was isolated and clean-up activities were initiated. The pipe was removed and found to have internal corrosion. The pipe was sent for metallurgical analysis; preliminary results indicate the presence of microbiologically induced corrosion at the site of the pinhole. Further analysis is underway to determine the specific strain(s) of bacteria present. To prevent re-occurrence the portion of the unit 6 header which contained the leak origin was removed, and blind flanges were installed in its place. |
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