HL incident on 2023-05-17 — OK

Operator
Magellan Terminals Holdings, Lp
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$20,000
Incident datetime
2023-05-17 00:00 UTC
Report number
Location
OK
Narrative
At 15:00 on april 17th, 2023 magellan operations personnel conducting daily facility inspections discovered product dripping from a pinhole in a low-flow section of the unit 6 header piping at cushing. The leak source was isolated and clean-up activities were initiated. The pipe was removed and found to have internal corrosion. The pipe was sent for metallurgical analysis; preliminary results indicate the presence of microbiologically induced corrosion at the site of the pinhole. Further analysis is underway to determine the specific strain(s) of bacteria present. To prevent re-occurrence the portion of the unit 6 header which contained the leak origin was removed, and blind flanges were installed in its place.
Detailed record list
Report Received Date
2023-05-17 00:00:00
Iyear
2023
Report Number
20230100
Supplemental Number
38061
Report Type
Original Final
Operator Id
Name
Magellan Terminals Holdings, Lp
Operator Street Address
100 West 5th Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
5
Recovered Bbls
5
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Communication State Fed Ind
No
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Notify Qualified Indiv Ind
Yes
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Central Cushing
Segment Name
Fac Id 800
Onshore State Abbreviation
Ok
Onshore Postal Code
74023
Onshore City Name
Cushing
Onshore County Name
Payne
Designated Location
Milepost
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Puddle Weld Ind
No
Pipe Diameter
14
Pipe Wall Thickness
0.375
Pipe Smys
24000
Pipe Specification
Unknown
Pipe Seam Type
Seamless
Pipe Manufacturer
Unknown
Pipe Coating Type
Paint
Coating Applied Ind
Yes
Installation Year
Unknown
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
500
Est Cost Prop Damage
20000
Est Cost Emergency
7500
Est Cost Environmental
0
Est Cost Other
0
Prpty
28000
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
30
Mop Psig
275
Mop Cfr Section
Component Design Pressure �195.406(A)(2)
Maop Established Date
2011-01-01 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Not caused or contributed to by the controller.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Microbiological Ind
Yes
Int Metallurgical Basis Ind
Yes
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
No
Corrosion Lining
No
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
Not Applicable - Not Mainline Pipe
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Intrnl Cor Corrosive Cmdty Ind
Yes
Preparer Name
C******* R******
Preparer Title
Strategic Data Engineer
Preparer Email
C***************@m*********.com
Preparer Telephone
9185747065
Prepared Date
2023-05-17 00:00:00
Authorizer Name
T***** K***
Authorizer Telephone
9185747191
Authorizer Title
Supv. Integrity Mgmt And Regulatory Compliance
Authorizer Email
T**********@m*********.com
Narrative
At 15:00 on april 17th, 2023 magellan operations personnel conducting daily facility inspections discovered product dripping from a pinhole in a low-flow section of the unit 6 header piping at cushing. The leak source was isolated and clean-up activities were initiated. The pipe was removed and found to have internal corrosion. The pipe was sent for metallurgical analysis; preliminary results indicate the presence of microbiologically induced corrosion at the site of the pinhole. Further analysis is underway to determine the specific strain(s) of bacteria present. To prevent re-occurrence the portion of the unit 6 header which contained the leak origin was removed, and blind flanges were installed in its place.
Report Received Date 2023-05-17 00:00:00
Iyear 2023
Report Number 20230100
Supplemental Number 38061
Report Type Original Final
Operator Id 31580 PHMSA Enforcement
Name Magellan Terminals Holdings, Lp
Operator Street Address 100 West 5th Street
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74103
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 35.946089 Google Maps OpenStreetMap
Location Longitude -96.747961 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 5
Recovered Bbls 5
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind Yes
Communication State Fed Ind No
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Notify Qualified Indiv Ind Yes
Oil Spill Removal Org Ind No
Num Pub Evacuated 0
Pipe Fac Name Central Cushing
Segment Name Fac Id 800
Onshore State Abbreviation Ok
Onshore Postal Code 74023
Onshore City Name Cushing
Onshore County Name Payne
Designated Location Milepost
Designated Name 0
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Puddle Weld Ind No
Pipe Diameter 14
Pipe Wall Thickness 0.375
Pipe Smys 24000
Pipe Specification Unknown
Pipe Seam Type Seamless
Pipe Manufacturer Unknown
Pipe Coating Type Paint
Coating Applied Ind Yes
Installation Year Unknown
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 500
Est Cost Prop Damage 20000
Est Cost Emergency 7500
Est Cost Environmental 0
Est Cost Other 0
Prpty 28000
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 30
Mop Psig 275
Mop Cfr Section Component Design Pressure �195.406(A)(2) View CFR 49 §192
Maop Established Date 2011-01-01 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Not caused or contributed to by the controller.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Localized Pitting
Int Microbiological Ind Yes
Int Metallurgical Basis Ind Yes
Int Low Point Pipe Loc Ind Yes
Corrosion Inhibitors No
Corrosion Lining No
Cleaning Dewatering Not Applicable - Not Mainline Pipe
Corrosion Coupons Not Applicable - Not Mainline Pipe
Collected Data Ind No
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Intrnl Cor Corrosive Cmdty Ind Yes
Preparer Name C******* R******
Preparer Title Strategic Data Engineer
Preparer Email C***************@m*********.com
Preparer Telephone 9185747065
Prepared Date 2023-05-17 00:00:00
Authorizer Name T***** K***
Authorizer Telephone 9185747191
Authorizer Title Supv. Integrity Mgmt And Regulatory Compliance
Authorizer Email T**********@m*********.com
Narrative At 15:00 on april 17th, 2023 magellan operations personnel conducting daily facility inspections discovered product dripping from a pinhole in a low-flow section of the unit 6 header piping at cushing. The leak source was isolated and clean-up activities were initiated. The pipe was removed and found to have internal corrosion. The pipe was sent for metallurgical analysis; preliminary results indicate the presence of microbiologically induced corrosion at the site of the pinhole. Further analysis is underway to determine the specific strain(s) of bacteria present. To prevent re-occurrence the portion of the unit 6 header which contained the leak origin was removed, and blind flanges were installed in its place.

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