GTG incident on 2023-11-02 — TX

Operator
Enable Gas Transmission, Llc
Cause
Material Failure Of Pipe Or Weld
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$10,000,000
Incident datetime
2023-11-02 00:00 UTC
Report number
Location
TX
Narrative
On 10/04/2023 at approximately 443pm, bt-1-an, a natural gas transmission pipeline, ruptured and ignited at jessieville junction. -443pm: system control was notified by a caller from the general public at 443pm -445pm: the lead gas controller began notifying ops personnel at 445pm of a possible failure at jessieville junction. -447pm: the lead gas controller received a rate of change alarm indicating a rapid loss of line pressure. -529pm: ops personnel arrived on site and confirmed that a pipeline had failed at jessieville junction. -531pm: ops personnel isolated the downstream valve 16" bt-1-as valve at hwy 88. -544pm: nrc notification was made (nrc# 1380909); 48hr nrc update (nrc# 1381352) -615pm: determination was made that above ground piping for bt-1-an 24", bt-1 16", bt-1-as 16", and bt-1 30" were affected at jessieville junction. -630pm: ops personnel isolated the upstream valves for bt-1 16" and bt-1-an 24" at dry fork mlv ops personnel manned the valves at dry fork and hwy 88 while additional technicians stayed onsite at jessieville junction throughout the night to monitor the flame as it burned out. Three people were evacuated from a home approximately 645' from the failure site on 10/04/2023; they were evacuated at the time of incident and able to return to the home at approximately 730pm that evening. 10/05/2023 -744am: the fire at the failure site was confirmed to be completely extinguished. -800am: ops personnel initiated the operation of air movers -1255pm: failure site was cleared for access and personnel from aid and the sw region were able to begin their investigation 10/07/2023 -the suspected origin failure piece (bt-1-an) was loaded on a truck to be shipped to adv integrity lab in magnolia, tx -contract crew began excavating bt-1-an, bt-1 16", bt-1 30", and bt-1-as 16" to the appropriate location on each segment to cut and cap. The metallurgical testing results for the origin piece of pipe are pending and a supplemental report will be filed. On 10/13/2023, energy transfer received a corrective action order (4-2023-007 cao egt) defining the requirements to return bt-1-an, bt-1 16", bt-1 30", and bt-1-as to service from dry fork mlv to hwy 88 gate valve. The segments remain isolated and out of service at the of this filing. Customer impact -there are 12 total taps and 1 town border out of service due to the isolated segment from dry fork mlv to hwy 88 gate valve being out of service. -8 domestic style taps and 4 rural extension u-shape taps -hot springs #2 town border -the local distribution company in the area has 244 customers affected with the isolated segments from dry fork mlv to hwy 88 gate valve out of service. *supplemental report updates* part c - additional facility information was updated: -3c: smys is 60,000 -3f: pipe manufacturer is a.O. Smith/ US steel -c6: type of release is longitudinal and approx. Size of release is 30.0in x 538in part g - apparent cause was updated: -g5 - "material failure of pipe or weld" was selected as the apparent cause. -determined by metallurgical analysis. -environmental cracking-related "stress corrosion cracking". -post construction pt pressure was added part j - integrity inspections -updated with most recent and previous tool run information. Updated supplemental and final report with date and time that flow was established on bt-1-an. The pipeline was officially restarted on 3-28-2024 at 19:20.
Detailed record list
Report Received Date
2023-11-02 00:00:00
Iyear
2023
Report Number
20230099
Supplemental Number
39400
Report Type
Supplemental Final
Operator Id
Name
Enable Gas Transmission, Llc
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Nrc Rpt Num
Additional Nrc Report Numbers
1381352
Commodity Released Type
Natural Gas
Unintentional Release
99860
Intentional Release
0
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Status When Identified
Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind
Yes
Communication State Fed Ind
Yes
Party Initiated Communication
Local/state/federal Emergency Responder
Ignite Ind
Yes
How Extinguished
Allowed To Burn Out
Gas Consumed By Fire In Mcf
99860
Explode Ind
No
Upstream Action Taken
Valve Closure
Downstream Action Taken
Valve Closure
Num Pub Evacuated
2
On Off Shore
Onshore
Onshore State Abbreviation
Ar
Onshore Postal Code
71949
Onshore City Name
Not Within A Municipality
Onshore County Name
Garland
Designated Location
Not Applicable
Pipe Fac Name
Bt-1-An At Jessieville Junction
Segment Name
Bt-1-An
Federal
No
Location Type
Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
48
Other Underground Facilities
No
Crossing
No
Pipe Facility Type
Interstate
System Part Involved
Onshore Pipeline, Including Valve Sites
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
24
Puddle Weld Ind
No
Pipe Wall Thickness
0.281
Pipe Smys
60000
Pipe Specification
Api-5l
Pipe Seam Type
Dsaw
Pipe Manufacturer
A.o. Smith/us Steel
Pipe Coating Type
Coal Tar
Coating Applied Ind
No
Installation Year
1967
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Rupture
Rupture Orient
Longitudinal
Rupture Length
538
Rupture Width
30
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
524
Heat Damage Ind
Yes
Non Heat Damage Ind
No
Did Occur In Mca Ind
No
Est Cost Oper Paid
60345
Est Cost Unintentional Release
300379
Est Cost Intentional Release
0
Est Cost Prop Damage
10000000
Est Cost Emergency
75000
Est Cost Other
0
Gas Cost In Mcf
3.008
Prpty
10435724
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
10
Num Business Building Affctd
4
Wildlife Impact Ind
No
Accident Psig
980
Gas Flow In Pipe In Mcf
220000
Mop Psig
1000
Mop Cfr Section
192.619(A)(1)
Maop Established Date
1967-10-04 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Gas Required Odorized Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Length Segment Isolated
153120
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Accident Identifier
Notification From Public
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Environmental Cracking-Related
Pwjf Failure Type
Environmental Cracking-Related
Metallurgical Ind
Yes
Stress Subtype
Stress Corrosion Cracking
Post Constr Pressure Test Val
1415
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Geometry Deformation Ind
Yes
Axial Recent Year
2023
Axial Rcnt Propul Method
Free Swimming
Axial Rcnt Attuned Detect
Metal Loss
Axial Rcnt Atnd Dtct Metal
High Resolution
Axial Previous Year
2013
Axial Prev Propul Method
Free Swimming
Axial Prev Attuned Detect
Metal Loss
Axial Prev Atnd Dtct Metal
High Resolution
Geometry Recent Year
2023
Geometry Rcnt Propul Method
Free Swimming
Geometry Rcnt Resolution
High Resolution
Geometrt Rcnt Measur Cups
No Cups
Geometry Previous Year
2013
Geometry Prev Propul Method
Free Swimming
Geometry Prev Resolution
Standard Resolution
Geometrt Prev Measur Cups
Inside Ili Cups
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Extrnl Cor Galvanic Ind
Yes
Preparer Name
D***** A******
Preparer Title
Sr. Dot Specialist
Preparer Email
D*************@e*************.com
Preparer Telephone
501-351-8513
Local Contact Name
D***** A******
Local Contact Email
D*************@e*************.com
Local Contact Telephone
501-351-8513
Authorizer Name
S**** S*****
Authorizer Title
Director Regulatory Compliance
Authorizer Telephone
405-557-5271
Authorizer Email
S***********@e*************.com
Narrative
On 10/04/2023 at approximately 443pm, bt-1-an, a natural gas transmission pipeline, ruptured and ignited at jessieville junction. -443pm: system control was notified by a caller from the general public at 443pm -445pm: the lead gas controller began notifying ops personnel at 445pm of a possible failure at jessieville junction. -447pm: the lead gas controller received a rate of change alarm indicating a rapid loss of line pressure. -529pm: ops personnel arrived on site and confirmed that a pipeline had failed at jessieville junction. -531pm: ops personnel isolated the downstream valve 16" bt-1-as valve at hwy 88. -544pm: nrc notification was made (nrc# 1380909); 48hr nrc update (nrc# 1381352) -615pm: determination was made that above ground piping for bt-1-an 24", bt-1 16", bt-1-as 16", and bt-1 30" were affected at jessieville junction. -630pm: ops personnel isolated the upstream valves for bt-1 16" and bt-1-an 24" at dry fork mlv ops personnel manned the valves at dry fork and hwy 88 while additional technicians stayed onsite at jessieville junction throughout the night to monitor the flame as it burned out. Three people were evacuated from a home approximately 645' from the failure site on 10/04/2023; they were evacuated at the time of incident and able to return to the home at approximately 730pm that evening. 10/05/2023 -744am: the fire at the failure site was confirmed to be completely extinguished. -800am: ops personnel initiated the operation of air movers -1255pm: failure site was cleared for access and personnel from aid and the sw region were able to begin their investigation 10/07/2023 -the suspected origin failure piece (bt-1-an) was loaded on a truck to be shipped to adv integrity lab in magnolia, tx -contract crew began excavating bt-1-an, bt-1 16", bt-1 30", and bt-1-as 16" to the appropriate location on each segment to cut and cap. The metallurgical testing results for the origin piece of pipe are pending and a supplemental report will be filed. On 10/13/2023, energy transfer received a corrective action order (4-2023-007 cao egt) defining the requirements to return bt-1-an, bt-1 16", bt-1 30", and bt-1-as to service from dry fork mlv to hwy 88 gate valve. The segments remain isolated and out of service at the of this filing. Customer impact -there are 12 total taps and 1 town border out of service due to the isolated segment from dry fork mlv to hwy 88 gate valve being out of service. -8 domestic style taps and 4 rural extension u-shape taps -hot springs #2 town border -the local distribution company in the area has 244 customers affected with the isolated segments from dry fork mlv to hwy 88 gate valve out of service. *supplemental report updates* part c - additional facility information was updated: -3c: smys is 60,000 -3f: pipe manufacturer is a.O. Smith/ US steel -c6: type of release is longitudinal and approx. Size of release is 30.0in x 538in part g - apparent cause was updated: -g5 - "material failure of pipe or weld" was selected as the apparent cause. -determined by metallurgical analysis. -environmental cracking-related "stress corrosion cracking". -post construction pt pressure was added part j - integrity inspections -updated with most recent and previous tool run information. Updated supplemental and final report with date and time that flow was established on bt-1-an. The pipeline was officially restarted on 3-28-2024 at 19:20.
Report Received Date 2023-11-02 00:00:00
Iyear 2023
Report Number 20230099
Supplemental Number 39400
Report Type Supplemental Final
Operator Id 602 PHMSA Enforcement
Name Enable Gas Transmission, Llc
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 34.68262454 Google Maps OpenStreetMap
Location Longitude -93.1115072 Google Maps OpenStreetMap
Nrc Rpt Num 1380909 NRC Report How to search
Additional Nrc Report Numbers 1381352
Commodity Released Type Natural Gas
Unintentional Release 99860
Intentional Release 0
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Status When Identified Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind Yes
Communication State Fed Ind Yes
Party Initiated Communication Local/state/federal Emergency Responder
Ignite Ind Yes
How Extinguished Allowed To Burn Out
Gas Consumed By Fire In Mcf 99860
Explode Ind No
Upstream Action Taken Valve Closure
Downstream Action Taken Valve Closure
Num Pub Evacuated 2
On Off Shore Onshore
Onshore State Abbreviation Ar
Onshore Postal Code 71949
Onshore City Name Not Within A Municipality
Onshore County Name Garland
Designated Location Not Applicable
Pipe Fac Name Bt-1-An At Jessieville Junction
Segment Name Bt-1-An
Federal No
Location Type Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 48
Other Underground Facilities No
Crossing No
Pipe Facility Type Interstate
System Part Involved Onshore Pipeline, Including Valve Sites
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 24
Puddle Weld Ind No
Pipe Wall Thickness 0.281
Pipe Smys 60000
Pipe Specification Api-5l
Pipe Seam Type Dsaw
Pipe Manufacturer A.o. Smith/us Steel
Pipe Coating Type Coal Tar
Coating Applied Ind No
Installation Year 1967
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Rupture
Rupture Orient Longitudinal
Rupture Length 538
Rupture Width 30
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 524
Heat Damage Ind Yes
Non Heat Damage Ind No
Did Occur In Mca Ind No
Est Cost Oper Paid 60345
Est Cost Unintentional Release 300379
Est Cost Intentional Release 0
Est Cost Prop Damage 10000000
Est Cost Emergency 75000
Est Cost Other 0
Gas Cost In Mcf 3.008
Prpty 10435724
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 10
Num Business Building Affctd 4
Wildlife Impact Ind No
Accident Psig 980
Gas Flow In Pipe In Mcf 220000
Mop Psig 1000
Mop Cfr Section 192.619(A)(1) View CFR 49 §192
Maop Established Date 1967-10-04 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Gas Required Odorized Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Length Segment Isolated 153120
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Accident Identifier Notification From Public
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind Yes
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Material Failure Of Pipe Or Weld
Cause Details Environmental Cracking-Related
Pwjf Failure Type Environmental Cracking-Related
Metallurgical Ind Yes
Stress Subtype Stress Corrosion Cracking
Post Constr Pressure Test Val 1415
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Geometry Deformation Ind Yes
Axial Recent Year 2023
Axial Rcnt Propul Method Free Swimming
Axial Rcnt Attuned Detect Metal Loss
Axial Rcnt Atnd Dtct Metal High Resolution
Axial Previous Year 2013
Axial Prev Propul Method Free Swimming
Axial Prev Attuned Detect Metal Loss
Axial Prev Atnd Dtct Metal High Resolution
Geometry Recent Year 2023
Geometry Rcnt Propul Method Free Swimming
Geometry Rcnt Resolution High Resolution
Geometrt Rcnt Measur Cups No Cups
Geometry Previous Year 2013
Geometry Prev Propul Method Free Swimming
Geometry Prev Resolution Standard Resolution
Geometrt Prev Measur Cups Inside Ili Cups
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Extrnl Cor Galvanic Ind Yes
Preparer Name D***** A******
Preparer Title Sr. Dot Specialist
Preparer Email D*************@e*************.com
Preparer Telephone 501-351-8513
Local Contact Name D***** A******
Local Contact Email D*************@e*************.com
Local Contact Telephone 501-351-8513
Authorizer Name S**** S*****
Authorizer Title Director Regulatory Compliance
Authorizer Telephone 405-557-5271
Authorizer Email S***********@e*************.com
Narrative On 10/04/2023 at approximately 443pm, bt-1-an, a natural gas transmission pipeline, ruptured and ignited at jessieville junction. -443pm: system control was notified by a caller from the general public at 443pm -445pm: the lead gas controller began notifying ops personnel at 445pm of a possible failure at jessieville junction. -447pm: the lead gas controller received a rate of change alarm indicating a rapid loss of line pressure. -529pm: ops personnel arrived on site and confirmed that a pipeline had failed at jessieville junction. -531pm: ops personnel isolated the downstream valve 16" bt-1-as valve at hwy 88. -544pm: nrc notification was made (nrc# 1380909); 48hr nrc update (nrc# 1381352) -615pm: determination was made that above ground piping for bt-1-an 24", bt-1 16", bt-1-as 16", and bt-1 30" were affected at jessieville junction. -630pm: ops personnel isolated the upstream valves for bt-1 16" and bt-1-an 24" at dry fork mlv ops personnel manned the valves at dry fork and hwy 88 while additional technicians stayed onsite at jessieville junction throughout the night to monitor the flame as it burned out. Three people were evacuated from a home approximately 645' from the failure site on 10/04/2023; they were evacuated at the time of incident and able to return to the home at approximately 730pm that evening. 10/05/2023 -744am: the fire at the failure site was confirmed to be completely extinguished. -800am: ops personnel initiated the operation of air movers -1255pm: failure site was cleared for access and personnel from aid and the sw region were able to begin their investigation 10/07/2023 -the suspected origin failure piece (bt-1-an) was loaded on a truck to be shipped to adv integrity lab in magnolia, tx -contract crew began excavating bt-1-an, bt-1 16", bt-1 30", and bt-1-as 16" to the appropriate location on each segment to cut and cap. The metallurgical testing results for the origin piece of pipe are pending and a supplemental report will be filed. On 10/13/2023, energy transfer received a corrective action order (4-2023-007 cao egt) defining the requirements to return bt-1-an, bt-1 16", bt-1 30", and bt-1-as to service from dry fork mlv to hwy 88 gate valve. The segments remain isolated and out of service at the of this filing. Customer impact -there are 12 total taps and 1 town border out of service due to the isolated segment from dry fork mlv to hwy 88 gate valve being out of service. -8 domestic style taps and 4 rural extension u-shape taps -hot springs #2 town border -the local distribution company in the area has 244 customers affected with the isolated segments from dry fork mlv to hwy 88 gate valve out of service. *supplemental report updates* part c - additional facility information was updated: -3c: smys is 60,000 -3f: pipe manufacturer is a.O. Smith/ US steel -c6: type of release is longitudinal and approx. Size of release is 30.0in x 538in part g - apparent cause was updated: -g5 - "material failure of pipe or weld" was selected as the apparent cause. -determined by metallurgical analysis. -environmental cracking-related "stress corrosion cracking". -post construction pt pressure was added part j - integrity inspections -updated with most recent and previous tool run information. Updated supplemental and final report with date and time that flow was established on bt-1-an. The pipeline was officially restarted on 3-28-2024 at 19:20.

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