Incident details
Operator, cause, commodity and consequences with raw source fields.
GD incident on 2023-12-15 — TX
Operator
Centerpoint Energy Resources Corporation
Cause
Locating Issue
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities
1 injury
Property damage (nominal)
$0
Incident datetime
2023-12-15 00:00 UTC
Report number
Location
TX, HARRIS
Narrative
On november 17, 2023, at approximately 8:30am, the houston fire department notified centerpoint energy about a gas leak at the 3600 block of woodhead and kipling street in houston texas. Once centerpoint arrived on site it identified a gas line had been struck by mechanized equipment operated by main line industries (mc2). The damage occurred on a 2" polyethylene gas line which was an offset to deconflict the 6" steel, with another utility placement. While the contractor was preparing the sub-base for the proposed roadway, the contractor came in contact with cnp facility with road reclaimer (asphalt grinder). After initial review, it was determined that mc2 had a valid one call ticket (no. 2381471224) for this work, and the locate vendor responded to the locate request in the required time. After further review it was determined that this 2" polyethylene line was not available in cnp mapping system.
Detailed record list
Report Received Date
2023-12-15 00:00:00
Iyear
2023.0
Report Number
20230077.0
Supplemental Number
39070.0
Report Type
Supplemental Final
Operator Id
4499
Name
Centerpoint Energy Resources Corporation
Operator Street Address
1111 Louisiana St
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002.0
Time Zone
Central
Daylight Savings Ind
Yes
Location Street Address
1************@ ********
Location City Name
Houston
Location County Name
Harris
Location State Abbreviation
TX
Location Postal Code
77098.0
Location Latitude
29.7405
Location Longitude
-95.4047
Flow Cont Squeeze Off Ind
Yes
Flow Cont Stopple Fitng Ind
Yes
Nrc Rpt Num
1384557.0
Additional Nrc Report Numbers
1384618.0
Commodity Released Type
Natural Gas
Unintentional Release
1280.452
Intentional Release
0.0
Fatality Ind
No
Fatal
0
Injury Ind
Yes
Num Emp Injuries
0
Num Contr Injuries
0
Num Er Injuries
0
Num Worker Injuries
1
Num Gp Injuries
0
Injure
1
Ignite Ind
Yes
How Extinguished
Local/state/federal Emergency Responder
Gas Consumed By Fire In Mcf
1280
Explode Ind
No
Num Pub Evacuated
4.0
Federal
No
Location Type
Public Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
8.0
Other Underground Facilities
No
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Main
Installation Year
2023.0
Pipe Diameter
2.0
Pipe Specification
Astm D2513
Pipe Manufacturer
Central
Material Involved
Plastic
Plastic Type
Polyethylene (Pe)
Plastic Sdr
11
Material Pe Pipe Code
2406
Release Type
Mechanical Puncture
Puncture Axial
2.0
Puncture Circum
2.0
Class Location Type
Class 3 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
0.0
Est Cost Emergency
12258.0
Est Cost Other
761900.0
Est Cost Other Details
Damage To Equipment And Home
Gas Cost In Mcf
6.452
Est Cost Unintentional Release
8261.0
Est Cost Intentional Release
0.0
Prpty
782419.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
4.0
Num Persons Hosp Not Ovnght
0.0
Num Injured Treated By Emt
0.0
Num Resident Building Affctd
4.0
Num Business Building Affctd
0.0
Accident Psig
44.0
Normal Psig
44.0
Mop Psig
60.0
Mop Cfr Section
192.619(A)(1)
Maop Established Date
2023-07-03 00:00:00
Accident Pressure
Pressure Did Not Exceed Maop
Gas Odorized System Type
Injection Pump
Gas Odorized Lvl Not Msrd Ind
Yes
Scada In Place Ind
No
Accident Identifier
Notification From Emergency Responder
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Release did not exceed the threshold
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
Yes
One Call System Ind
Yes
State Law Exempt Ind
No
Notify Cga Dirt
No
Public Row Ind
Yes
Public Subtype
City Street
Joint Trench Ind
No
Cross Bore Ind
No
Depth Of Grade
< 18�
Excavator Type
Contractor
Excavator Equipment
Grader/scraper
Work Performed
Road Work
One Call Notified Ind
Yes
One Call Ticket Num
2381471224.0
One Call Center Name
Texas 811
White Lined Ind
Unknown
Locator Type
Contract Locator
Visible Marks
Yes
Service Interruption
Yes
Service Interruption Hours
16.0
Root Cause Category
Locating Issue
Root Cause Type
Facility Not Marked Due To Incorrect Facility Records/maps
Preparer Name
L***** J D********
Preparer Title
Sr Compliance Coordinator
Preparer Email
L***************@c****************.com
Preparer Telephone
713-967-7325
Preparer Fax
713-967-7307
Local Contact Name
S** C***
Local Contact Email
S*******@c****************.com
Local Contact Telephone
713-967-8026
Authorizer Name
J**** G***
Authorizer Title
Regional Operations Director
Authorizer Telephone
713-967-7101
Authorizer Email
J*********@c****************.com
Narrative
On november 17, 2023, at approximately 8:30am, the houston fire department notified centerpoint energy about a gas leak at the 3600 block of woodhead and kipling street in houston texas. Once centerpoint arrived on site it identified a gas line had been struck by mechanized equipment operated by main line industries (mc2). The damage occurred on a 2" polyethylene gas line which was an offset to deconflict the 6" steel, with another utility placement. While the contractor was preparing the sub-base for the proposed roadway, the contractor came in contact with cnp facility with road reclaimer (asphalt grinder). After initial review, it was determined that mc2 had a valid one call ticket (no. 2381471224) for this work, and the locate vendor responded to the locate request in the required time. After further review it was determined that this 2" polyethylene line was not available in cnp mapping system.
Report Received Date | 2023-12-15 00:00:00 |
---|---|
Iyear | 2023.0 |
Report Number | 20230077.0 |
Supplemental Number | 39070.0 |
Report Type | Supplemental Final |
Operator Id | 4499 PHMSA Enforcement |
Name | Centerpoint Energy Resources Corporation |
Operator Street Address | 1111 Louisiana St |
Operator City Name | Houston |
Operator State Abbreviation | TX |
Operator Postal Code | 77002.0 |
Time Zone | Central |
Daylight Savings Ind | Yes |
Location Street Address | 1************@ ******** |
Location City Name | Houston |
Location County Name | Harris |
Location State Abbreviation | TX |
Location Postal Code | 77098.0 |
Location Latitude | 29.7405 Google Maps OpenStreetMap |
Location Longitude | -95.4047 Google Maps OpenStreetMap |
Flow Cont Squeeze Off Ind | Yes |
Flow Cont Stopple Fitng Ind | Yes |
Nrc Rpt Num | 1384557.0 NRC Report How to search |
Additional Nrc Report Numbers | 1384618.0 |
Commodity Released Type | Natural Gas |
Unintentional Release | 1280.452 |
Intentional Release | 0.0 |
Fatality Ind | No |
Fatal | 0 |
Injury Ind | Yes |
Num Emp Injuries | 0 |
Num Contr Injuries | 0 |
Num Er Injuries | 0 |
Num Worker Injuries | 1 |
Num Gp Injuries | 0 |
Injure | 1 |
Ignite Ind | Yes |
How Extinguished | Local/state/federal Emergency Responder |
Gas Consumed By Fire In Mcf | 1280 |
Explode Ind | No |
Num Pub Evacuated | 4.0 |
Federal | No |
Location Type | Public Property |
Incident Area Type | Underground |
Incident Area Subtype | Under Soil |
Depth Of Cover | 8.0 |
Other Underground Facilities | No |
Crossing | No |
Pipe Facility Type | Investor Owned |
System Part Involved | Main |
Installation Year | 2023.0 |
Pipe Diameter | 2.0 |
Pipe Specification | Astm D2513 |
Pipe Manufacturer | Central |
Material Involved | Plastic |
Plastic Type | Polyethylene (Pe) |
Plastic Sdr | 11 |
Material Pe Pipe Code | 2406 |
Release Type | Mechanical Puncture |
Puncture Axial | 2.0 |
Puncture Circum | 2.0 |
Class Location Type | Class 3 Location |
Est Cost Oper Paid | 0.0 |
Est Cost Prop Damage | 0.0 |
Est Cost Emergency | 12258.0 |
Est Cost Other | 761900.0 |
Est Cost Other Details | Damage To Equipment And Home |
Gas Cost In Mcf | 6.452 |
Est Cost Unintentional Release | 8261.0 |
Est Cost Intentional Release | 0.0 |
Prpty | 782419.0 |
Commercial Affected | 0.0 |
Industrial Affected | 0.0 |
Residences Affected | 4.0 |
Num Persons Hosp Not Ovnght | 0.0 |
Num Injured Treated By Emt | 0.0 |
Num Resident Building Affctd | 4.0 |
Num Business Building Affctd | 0.0 |
Accident Psig | 44.0 |
Normal Psig | 44.0 |
Mop Psig | 60.0 |
Mop Cfr Section | 192.619(A)(1) View CFR 49 §192 |
Maop Established Date | 2023-07-03 00:00:00 |
Accident Pressure | Pressure Did Not Exceed Maop |
Gas Odorized System Type | Injection Pump |
Gas Odorized Lvl Not Msrd Ind | Yes |
Scada In Place Ind | No |
Accident Identifier | Notification From Emergency Responder |
Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
Investigation Status Details | Release did not exceed the threshold |
Employee Drug Test Ind | No |
Contractor Drug Test Ind | No |
Cause | Excavation Damage |
Cause Details | Excavation Damage By Third Party |
Ex Party Type | Excavation Damage By Third Party |
Prior Notification Ind | Yes |
One Call System Ind | Yes |
State Law Exempt Ind | No |
Notify Cga Dirt | No |
Public Row Ind | Yes |
Public Subtype | City Street |
Joint Trench Ind | No |
Cross Bore Ind | No |
Depth Of Grade | < 18� |
Excavator Type | Contractor |
Excavator Equipment | Grader/scraper |
Work Performed | Road Work |
One Call Notified Ind | Yes |
One Call Ticket Num | 2381471224.0 |
One Call Center Name | Texas 811 |
White Lined Ind | Unknown |
Locator Type | Contract Locator |
Visible Marks | Yes |
Service Interruption | Yes |
Service Interruption Hours | 16.0 |
Root Cause Category | Locating Issue |
Root Cause Type | Facility Not Marked Due To Incorrect Facility Records/maps |
Preparer Name | L***** J D******** |
Preparer Title | Sr Compliance Coordinator |
Preparer Email | L***************@c****************.com |
Preparer Telephone | 713-967-7325 |
Preparer Fax | 713-967-7307 |
Local Contact Name | S** C*** |
Local Contact Email | S*******@c****************.com |
Local Contact Telephone | 713-967-8026 |
Authorizer Name | J**** G*** |
Authorizer Title | Regional Operations Director |
Authorizer Telephone | 713-967-7101 |
Authorizer Email | J*********@c****************.com |
Narrative | On november 17, 2023, at approximately 8:30am, the houston fire department notified centerpoint energy about a gas leak at the 3600 block of woodhead and kipling street in houston texas. Once centerpoint arrived on site it identified a gas line had been struck by mechanized equipment operated by main line industries (mc2). The damage occurred on a 2" polyethylene gas line which was an offset to deconflict the 6" steel, with another utility placement. While the contractor was preparing the sub-base for the proposed roadway, the contractor came in contact with cnp facility with road reclaimer (asphalt grinder). After initial review, it was determined that mc2 had a valid one call ticket (no. 2381471224) for this work, and the locate vendor responded to the locate request in the required time. After further review it was determined that this 2" polyethylene line was not available in cnp mapping system. |
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