GD incident on 2023-12-06 — GA

Operator
Atlanta Gas Light Co
Cause
Excavation Issue
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$3,480
Incident datetime
2023-12-06 00:00 UTC
Report number
Location
GA, FULTON
Narrative
On november 8, 2023, at approximately 15:53 hours, a third-party party excavator (washington communication) struck and damaged an atlanta gas light company (aglc) 6-inch steel gas main while directionally boring to install electric conduit lines at the intersection of northside drive and old powers ferry road, sandy springs, ga. Upon arrival, aglc personnel secured the area and monitored the surrounding area for gas migration. Based on a field assessment of conditions surrounding the location of the incident and to not shut down a large metro area should an existing valve north of the damage been used in conjunction with the other two valves operated, a decision was made to squeeze the pipe at a safe distance north of the damage. Upon excavating to expose the existing pipe, it was discovered that the pipe was approximately 66 inches deep and under approximately 36-inches of asphalt, gas was shut-off to the damaged area on november 8, 2023, at 23:54 hours by operating two (2) valves and performing one (1) squeeze off operation. A locate request was made on november 2, 2023, by washington communication (excavator) to locate "w northside dr, old powers ferry rd, locate the entire intersection for 50ft in all directionsboth sides of the rd and within the r/o/w on both sides of the st, this is a 3 leg int, it does notinclude locating along riverview rd nw". Aglc facilities were marked by usic locating company to satisfy this request on november 6, 2023, at 11:26 hours. On november 8, 2023, at 13:00 hours, usic remarked aglc's facilities as requested by the excavator due to facility markings no longer being visible. Investigation of the site revealed that the locate marks were accurate at the point of damage. Had the excavator potholed, it would have determined the location of the gas main. Once the damaged section of main was exposed and all the variables were obtained to perform the gas loss calculation, it was identified that the amount of gas released exceeded the threshold for reporting and the national response center (nrc) was notified at that time on november 9, 2023, at 18:49 hours where an initial nrc report number 1383916 was created. An additional nrc report number 1384000 was created for the same event after a supplemental call was placed with the nrc to update the initial telephonic notice.
Detailed record list
Report Received Date
2023-12-06 00:00:00
Iyear
2023.0
Report Number
20230073.0
Supplemental Number
39481.0
Report Type
Supplemental Final
Operator Id
Name
Atlanta Gas Light Co
Operator Street Address
10 Peachtree Place Ne
Operator City Name
Atlanta
Operator State Abbreviation
GA
Operator Postal Code
30309.0
Time Zone
Eastern
Daylight Savings Ind
No
Location Street Address
Northside Drive Nw At Old Powers Ferry Road
Location City Name
Sandy Springs
Location County Name
Fulton
Location State Abbreviation
GA
Location Postal Code
30339.0
Location Latitude
Location Longitude
Flow Cont Key Crit Ind
Yes
Flow Cont Squeeze Off Ind
Yes
Nrc Rpt Num
Additional Nrc Report Numbers
1384000.0
Commodity Released Type
Natural Gas
Unintentional Release
17423.0
Intentional Release
0.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Num Pub Evacuated
0.0
Federal
No
Location Type
Public Property
Incident Area Type
Underground
Incident Area Subtype
Under Pavement
Depth Of Cover
66.0
Other Underground Facilities
No
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Main
Installation Year
1968.0
Pipe Diameter
6.0
Pipe Specification
Api 5l
Pipe Manufacturer
Unknown
Material Involved
Steel
Steel Seam Type
Longitudinal Erw - Unknown Frequency
Wt Steel
0.188
Release Type
Mechanical Puncture
Puncture Axial
2.0
Puncture Circum
2.5
Class Location Type
Class 3 Location
Est Cost Oper Paid
2734.0
Est Cost Prop Damage
3480.0
Est Cost Emergency
75278.0
Est Cost Other
0.0
Gas Cost In Mcf
1.83
Est Cost Unintentional Release
31884.0
Est Cost Intentional Release
0.0
Prpty
113376.0
Commercial Affected
8.0
Industrial Affected
0.0
Residences Affected
0.0
Num Persons Hosp Not Ovnght
0.0
Num Injured Treated By Emt
0.0
Num Resident Building Affctd
0.0
Num Business Building Affctd
0.0
Accident Psig
230.0
Normal Psig
230.0
Mop Psig
300.0
Mop Cfr Section
192.619(A)(4)
Maop Established Date
1968-03-13 00:00:00
Accident Pressure
Pressure Did Not Exceed Maop
Gas Odorized System Type
Injection Pump
Gas Odorized Level
15.5
Scada In Place Ind
No
Accident Identifier
Notification From Emergency Responder
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
Yes
One Call System Ind
Yes
State Law Exempt Ind
No
Notify Cga Dirt
Yes
Public Row Ind
Yes
Public Subtype
City Street
Joint Trench Ind
No
Cross Bore Ind
No
Depth Of Grade
> 36�
Excavator Type
Contractor
Excavator Equipment
Directional Drilling
Work Performed
Electric
One Call Notified Ind
Yes
One Call Ticket Num
231102000000.0
White Lined Ind
Unknown
Locator Type
Contract Locator
Visible Marks
Yes
Service Interruption
Yes
Service Interruption Hours
24.0
Root Cause Category
Excavation Issue
Root Cause Type
Excavator Dug Prior To Verifying Marks By Test-Hole (Pothole)
Preparer Name
R**** M*******
Preparer Title
Principal Compliance Engineer
Preparer Email
R*******@s*********.com
Preparer Telephone
(404) 584-3733
Preparer Fax
(404) 584-4710
Authorizer Name
R*** S*****
Authorizer Title
Director Compliance And Qa
Authorizer Telephone
(404) 584-4910
Authorizer Email
R******@s*********.com
Narrative
On november 8, 2023, at approximately 15:53 hours, a third-party party excavator (washington communication) struck and damaged an atlanta gas light company (aglc) 6-inch steel gas main while directionally boring to install electric conduit lines at the intersection of northside drive and old powers ferry road, sandy springs, ga. Upon arrival, aglc personnel secured the area and monitored the surrounding area for gas migration. Based on a field assessment of conditions surrounding the location of the incident and to not shut down a large metro area should an existing valve north of the damage been used in conjunction with the other two valves operated, a decision was made to squeeze the pipe at a safe distance north of the damage. Upon excavating to expose the existing pipe, it was discovered that the pipe was approximately 66 inches deep and under approximately 36-inches of asphalt, gas was shut-off to the damaged area on november 8, 2023, at 23:54 hours by operating two (2) valves and performing one (1) squeeze off operation. A locate request was made on november 2, 2023, by washington communication (excavator) to locate "w northside dr, old powers ferry rd, locate the entire intersection for 50ft in all directionsboth sides of the rd and within the r/o/w on both sides of the st, this is a 3 leg int, it does notinclude locating along riverview rd nw". Aglc facilities were marked by usic locating company to satisfy this request on november 6, 2023, at 11:26 hours. On november 8, 2023, at 13:00 hours, usic remarked aglc's facilities as requested by the excavator due to facility markings no longer being visible. Investigation of the site revealed that the locate marks were accurate at the point of damage. Had the excavator potholed, it would have determined the location of the gas main. Once the damaged section of main was exposed and all the variables were obtained to perform the gas loss calculation, it was identified that the amount of gas released exceeded the threshold for reporting and the national response center (nrc) was notified at that time on november 9, 2023, at 18:49 hours where an initial nrc report number 1383916 was created. An additional nrc report number 1384000 was created for the same event after a supplemental call was placed with the nrc to update the initial telephonic notice.
Report Received Date 2023-12-06 00:00:00
Iyear 2023.0
Report Number 20230073.0
Supplemental Number 39481.0
Report Type Supplemental Final
Operator Id 792 PHMSA Enforcement
Name Atlanta Gas Light Co
Operator Street Address 10 Peachtree Place Ne
Operator City Name Atlanta
Operator State Abbreviation GA
Operator Postal Code 30309.0
Time Zone Eastern
Daylight Savings Ind No
Location Street Address Northside Drive Nw At Old Powers Ferry Road
Location City Name Sandy Springs
Location County Name Fulton
Location State Abbreviation GA
Location Postal Code 30339.0
Location Latitude 33.901791 Google Maps OpenStreetMap
Location Longitude -84.427496 Google Maps OpenStreetMap
Flow Cont Key Crit Ind Yes
Flow Cont Squeeze Off Ind Yes
Nrc Rpt Num 1383916.0 NRC Report How to search
Additional Nrc Report Numbers 1384000.0
Commodity Released Type Natural Gas
Unintentional Release 17423.0
Intentional Release 0.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind No
Num Pub Evacuated 0.0
Federal No
Location Type Public Property
Incident Area Type Underground
Incident Area Subtype Under Pavement
Depth Of Cover 66.0
Other Underground Facilities No
Crossing No
Pipe Facility Type Investor Owned
System Part Involved Main
Installation Year 1968.0
Pipe Diameter 6.0
Pipe Specification Api 5l
Pipe Manufacturer Unknown
Material Involved Steel
Steel Seam Type Longitudinal Erw - Unknown Frequency
Wt Steel 0.188
Release Type Mechanical Puncture
Puncture Axial 2.0
Puncture Circum 2.5
Class Location Type Class 3 Location
Est Cost Oper Paid 2734.0
Est Cost Prop Damage 3480.0
Est Cost Emergency 75278.0
Est Cost Other 0.0
Gas Cost In Mcf 1.83
Est Cost Unintentional Release 31884.0
Est Cost Intentional Release 0.0
Prpty 113376.0
Commercial Affected 8.0
Industrial Affected 0.0
Residences Affected 0.0
Num Persons Hosp Not Ovnght 0.0
Num Injured Treated By Emt 0.0
Num Resident Building Affctd 0.0
Num Business Building Affctd 0.0
Accident Psig 230.0
Normal Psig 230.0
Mop Psig 300.0
Mop Cfr Section 192.619(A)(4) View CFR 49 §192
Maop Established Date 1968-03-13 00:00:00
Accident Pressure Pressure Did Not Exceed Maop
Gas Odorized System Type Injection Pump
Gas Odorized Level 15.5
Scada In Place Ind No
Accident Identifier Notification From Emergency Responder
Investigation Status No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind Yes
One Call System Ind Yes
State Law Exempt Ind No
Notify Cga Dirt Yes
Public Row Ind Yes
Public Subtype City Street
Joint Trench Ind No
Cross Bore Ind No
Depth Of Grade > 36�
Excavator Type Contractor
Excavator Equipment Directional Drilling
Work Performed Electric
One Call Notified Ind Yes
One Call Ticket Num 231102000000.0
White Lined Ind Unknown
Locator Type Contract Locator
Visible Marks Yes
Service Interruption Yes
Service Interruption Hours 24.0
Root Cause Category Excavation Issue
Root Cause Type Excavator Dug Prior To Verifying Marks By Test-Hole (Pothole)
Preparer Name R**** M*******
Preparer Title Principal Compliance Engineer
Preparer Email R*******@s*********.com
Preparer Telephone (404) 584-3733
Preparer Fax (404) 584-4710
Authorizer Name R*** S*****
Authorizer Title Director Compliance And Qa
Authorizer Telephone (404) 584-4910
Authorizer Email R******@s*********.com
Narrative On november 8, 2023, at approximately 15:53 hours, a third-party party excavator (washington communication) struck and damaged an atlanta gas light company (aglc) 6-inch steel gas main while directionally boring to install electric conduit lines at the intersection of northside drive and old powers ferry road, sandy springs, ga. Upon arrival, aglc personnel secured the area and monitored the surrounding area for gas migration. Based on a field assessment of conditions surrounding the location of the incident and to not shut down a large metro area should an existing valve north of the damage been used in conjunction with the other two valves operated, a decision was made to squeeze the pipe at a safe distance north of the damage. Upon excavating to expose the existing pipe, it was discovered that the pipe was approximately 66 inches deep and under approximately 36-inches of asphalt, gas was shut-off to the damaged area on november 8, 2023, at 23:54 hours by operating two (2) valves and performing one (1) squeeze off operation. A locate request was made on november 2, 2023, by washington communication (excavator) to locate "w northside dr, old powers ferry rd, locate the entire intersection for 50ft in all directionsboth sides of the rd and within the r/o/w on both sides of the st, this is a 3 leg int, it does notinclude locating along riverview rd nw". Aglc facilities were marked by usic locating company to satisfy this request on november 6, 2023, at 11:26 hours. On november 8, 2023, at 13:00 hours, usic remarked aglc's facilities as requested by the excavator due to facility markings no longer being visible. Investigation of the site revealed that the locate marks were accurate at the point of damage. Had the excavator potholed, it would have determined the location of the gas main. Once the damaged section of main was exposed and all the variables were obtained to perform the gas loss calculation, it was identified that the amount of gas released exceeded the threshold for reporting and the national response center (nrc) was notified at that time on november 9, 2023, at 18:49 hours where an initial nrc report number 1383916 was created. An additional nrc report number 1384000 was created for the same event after a supplemental call was placed with the nrc to update the initial telephonic notice.

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