GD incident on 2023-11-16 — MI

Operator
Dte Gas Company
Cause
Miscellaneous Root Causes
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$53,500
Incident datetime
2023-11-16 00:00 UTC
Report number
Location
MI, WAYNE
Narrative
2nd party contractor impacted an object while boring for new gas main at 12:45 on 10/17/23. This object in-turn impacted a reducing fitting on a 12" 10 psi cast-iron main that was adjacent to the bore path, causing a crack and a leak. The reducing fitting was on an unmapped stub from activity done in year 1950. Gas was shut off at 02:28 on 10/18/23. Repair activities were initially not expected to exceed $10k total cost, nor any other reporting threshold, so michigan public service commission was not initially notified. Operations updated at 07:33 the following morning that a decision had been made to replace 25' of the main rather than perform the initially intended repair, in order to avoid customer outages. This change caused the repair cost to exceed the $10k threshold and the mpsc incident reporting line was notified at 08:19 on 10/18/23. After repair, gas loss was calculated and estimated at 4872mcf, which caused this incident to be PHMSA reportable. Also notified chemical safety board (csb).
Detailed record list
Report Received Date
2023-11-16 00:00:00
Iyear
2023.0
Report Number
20230068.0
Supplemental Number
38814.0
Report Type
Original Final
Operator Id
Name
Dte Gas Company
Operator Street Address
1 Energy Plaza
Operator City Name
Detroit
Operator State Abbreviation
MI
Operator Postal Code
48226.0
Time Zone
Eastern
Daylight Savings Ind
Yes
Location Street Address
565 E Milwaukee Ave
Location City Name
Detroit
Location County Name
Wayne
Location State Abbreviation
MI
Location Postal Code
48202.0
Location Latitude
Location Longitude
Flow Cont Stopple Fitng Ind
Yes
Nrc Rpt Num
Additional Nrc Report Numbers
1382278.0
Commodity Released Type
Natural Gas
Unintentional Release
4872.0
Intentional Release
0.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Num Pub Evacuated
0.0
Communication State Fed Ind
No
Federal
No
Location Type
Public Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
48.0
Other Underground Facilities
No
Crossing
No
Pipe Facility Type
Privately Owned
System Part Involved
Main
Installation Year
1900.0
Pipe Diameter
12.0
Pipe Specification
Unknown
Pipe Manufacturer
Unknown
Material Involved
Cast/wrought Iron
Release Type
Mechanical Puncture
Puncture Axial
4.0
Puncture Circum
12.0
Class Location Type
Class 3 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
53500.0
Est Cost Emergency
67600.0
Est Cost Other
0.0
Gas Cost In Mcf
3.1
Est Cost Unintentional Release
15103.0
Est Cost Intentional Release
0.0
Prpty
136203.0
Commercial Affected
2.0
Industrial Affected
0.0
Residences Affected
0.0
Num Persons Hosp Not Ovnght
0.0
Num Injured Treated By Emt
0.0
Num Resident Building Affctd
0.0
Num Business Building Affctd
2.0
Accident Psig
7.5
Normal Psig
10.0
Mop Psig
10.0
Mop Cfr Section
192.619(A)(3)
Maop Established Date
1899-01-01 00:00:00
Accident Pressure
Pressure Did Not Exceed Maop
Gas Odorized System Type
Injection Pump
Gas Odorized Lvl Not Msrd Ind
Yes
Scada In Place Ind
No
Accident Identifier
Other
Accident Details
Notification From 2nd Party Contractor
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Operator's Contractor (Second Party)
Ex Party Type
Excavation Damage By Operator's Contractor (Second Party)
Notify Cga Dirt
No
Public Row Ind
Yes
Public Subtype
City Street
Excavator Type
Contractor
Excavator Equipment
Directional Drilling
Work Performed
Natural Gas
One Call Notified Ind
Yes
One Call Ticket Num
2023080000000.0
Locator Type
Facility Owner
Visible Marks
Yes
Service Interruption
Yes
Service Interruption Hours
34.0
Root Cause Category
Miscellaneous Root Causes
Root Cause Type
Root Cause Not Listed (Comment Required)
Root Cause Type Other
Unmapped 6" Stub Extending 4' South Off Of 12" Cast Iron Main Installed In 1899
Preparer Name
J***** M*****
Preparer Email
J************@d********.com
Authorizer Name
M***** D******
Authorizer Telephone
5868724760
Authorizer Email
M*************@d********.com
Narrative
2nd party contractor impacted an object while boring for new gas main at 12:45 on 10/17/23. This object in-turn impacted a reducing fitting on a 12" 10 psi cast-iron main that was adjacent to the bore path, causing a crack and a leak. The reducing fitting was on an unmapped stub from activity done in year 1950. Gas was shut off at 02:28 on 10/18/23. Repair activities were initially not expected to exceed $10k total cost, nor any other reporting threshold, so michigan public service commission was not initially notified. Operations updated at 07:33 the following morning that a decision had been made to replace 25' of the main rather than perform the initially intended repair, in order to avoid customer outages. This change caused the repair cost to exceed the $10k threshold and the mpsc incident reporting line was notified at 08:19 on 10/18/23. After repair, gas loss was calculated and estimated at 4872mcf, which caused this incident to be PHMSA reportable. Also notified chemical safety board (csb).
Report Received Date 2023-11-16 00:00:00
Iyear 2023.0
Report Number 20230068.0
Supplemental Number 38814.0
Report Type Original Final
Operator Id 12408 PHMSA Enforcement
Name Dte Gas Company
Operator Street Address 1 Energy Plaza
Operator City Name Detroit
Operator State Abbreviation MI
Operator Postal Code 48226.0
Time Zone Eastern
Daylight Savings Ind Yes
Location Street Address 565 E Milwaukee Ave
Location City Name Detroit
Location County Name Wayne
Location State Abbreviation MI
Location Postal Code 48202.0
Location Latitude 42.371872 Google Maps OpenStreetMap
Location Longitude -83.065578 Google Maps OpenStreetMap
Flow Cont Stopple Fitng Ind Yes
Nrc Rpt Num 1382137.0 NRC Report How to search
Additional Nrc Report Numbers 1382278.0
Commodity Released Type Natural Gas
Unintentional Release 4872.0
Intentional Release 0.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind No
Num Pub Evacuated 0.0
Communication State Fed Ind No
Federal No
Location Type Public Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 48.0
Other Underground Facilities No
Crossing No
Pipe Facility Type Privately Owned
System Part Involved Main
Installation Year 1900.0
Pipe Diameter 12.0
Pipe Specification Unknown
Pipe Manufacturer Unknown
Material Involved Cast/wrought Iron
Release Type Mechanical Puncture
Puncture Axial 4.0
Puncture Circum 12.0
Class Location Type Class 3 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 53500.0
Est Cost Emergency 67600.0
Est Cost Other 0.0
Gas Cost In Mcf 3.1
Est Cost Unintentional Release 15103.0
Est Cost Intentional Release 0.0
Prpty 136203.0
Commercial Affected 2.0
Industrial Affected 0.0
Residences Affected 0.0
Num Persons Hosp Not Ovnght 0.0
Num Injured Treated By Emt 0.0
Num Resident Building Affctd 0.0
Num Business Building Affctd 2.0
Accident Psig 7.5
Normal Psig 10.0
Mop Psig 10.0
Mop Cfr Section 192.619(A)(3) View CFR 49 §192
Maop Established Date 1899-01-01 00:00:00
Accident Pressure Pressure Did Not Exceed Maop
Gas Odorized System Type Injection Pump
Gas Odorized Lvl Not Msrd Ind Yes
Scada In Place Ind No
Accident Identifier Other
Accident Details Notification From 2nd Party Contractor
Investigation Status No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Operator's Contractor (Second Party)
Ex Party Type Excavation Damage By Operator's Contractor (Second Party)
Notify Cga Dirt No
Public Row Ind Yes
Public Subtype City Street
Excavator Type Contractor
Excavator Equipment Directional Drilling
Work Performed Natural Gas
One Call Notified Ind Yes
One Call Ticket Num 2023080000000.0
Locator Type Facility Owner
Visible Marks Yes
Service Interruption Yes
Service Interruption Hours 34.0
Root Cause Category Miscellaneous Root Causes
Root Cause Type Root Cause Not Listed (Comment Required)
Root Cause Type Other Unmapped 6" Stub Extending 4' South Off Of 12" Cast Iron Main Installed In 1899
Preparer Name J***** M*****
Preparer Email J************@d********.com
Authorizer Name M***** D******
Authorizer Telephone 5868724760
Authorizer Email M*************@d********.com
Narrative 2nd party contractor impacted an object while boring for new gas main at 12:45 on 10/17/23. This object in-turn impacted a reducing fitting on a 12" 10 psi cast-iron main that was adjacent to the bore path, causing a crack and a leak. The reducing fitting was on an unmapped stub from activity done in year 1950. Gas was shut off at 02:28 on 10/18/23. Repair activities were initially not expected to exceed $10k total cost, nor any other reporting threshold, so michigan public service commission was not initially notified. Operations updated at 07:33 the following morning that a decision had been made to replace 25' of the main rather than perform the initially intended repair, in order to avoid customer outages. This change caused the repair cost to exceed the $10k threshold and the mpsc incident reporting line was notified at 08:19 on 10/18/23. After repair, gas loss was calculated and estimated at 4872mcf, which caused this incident to be PHMSA reportable. Also notified chemical safety board (csb).

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