Incident details
Operator, cause, commodity and consequences with raw source fields.
GD incident on 2023-11-06 — MO
Operator
Spire Missouri Inc. West
Cause
Incorrect Operation
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities
1 injury
Property damage (nominal)
$261
Incident datetime
2023-11-06 00:00 UTC
Report number
Location
MO, CLINTON COUNTY
Narrative
A company contractor crew was a performing a 12-inch steel main relocation and retiring a section of main between 2 stopple fittings. The stopples were in position to shut off the flow of gas and the pipe had been cut between the stopples and blown down. The contractor employee was preparing to cap downstream of one stopple. Two vent stacks (v1 & v2) were installed downstream of the stopple with a valve and air handler on the vent nearest the stopple fitting (v1). The contractor employee inserted a gripper plug in the 12-inch main up to the v1 vent stack location. Gas was bleeding past the stopple fitting. The valve on v1 vent stack was closed. This resulted in a pressure build-up between the stopple fitting and the gripper plug and caused the gripper plug to be ejected from the open-cut end of the 12-inch steel main. The gripper plug caused a hand injury with the contractor employee and he was admitted to the hospital for treatment. A 48-hour update to the nrc was made on october 5, 2023 at 18:49 - report number 1380998. Supplemental report created: part e.1, estimated pressure at time of incident updated from 56.0 psig to 125psig. Supplemental report created 12/12/2024: part g, updating to most applicable sub-cause of "wrong equipment specified or installed"
Detailed record list
Report Received Date
2023-11-06 00:00:00
Iyear
2023.0
Report Number
20230064.0
Supplemental Number
40343.0
Report Type
Supplemental Final
Operator Id
30769
Name
Spire Missouri Inc. West
Operator Street Address
700 Market Street
Operator City Name
Saint Louis
Operator State Abbreviation
MO
Operator Postal Code
63101.0
Time Zone
Central
Daylight Savings Ind
Yes
Location Street Address
310 Se Old Cannon Ball Rd
Location City Name
Holt
Location County Name
Clinton County
Location State Abbreviation
MO
Location Postal Code
64048.0
Location Latitude
39.45747
Location Longitude
-94.33586
Flow Cont Stopple Fitng Ind
Yes
Nrc Rpt Num
1380998.0
Additional Nrc Report Numbers
1381071.0
Commodity Released Type
Natural Gas
Unintentional Release
56.0
Intentional Release
0.0
Fatality Ind
No
Fatal
0
Injury Ind
Yes
Num Emp Injuries
0
Num Contr Injuries
1
Num Er Injuries
0
Num Worker Injuries
0
Num Gp Injuries
0
Injure
1
Ignite Ind
No
Num Pub Evacuated
0.0
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Federal
No
Location Type
Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Exposed Due To Excavation
Depth Of Cover
63.0
Other Underground Facilities
No
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Main
Installation Year
1962.0
Pipe Diameter
12.0
Pipe Specification
Unknown
Pipe Manufacturer
Unknown
Material Involved
Steel
Steel Seam Type
Other
Steel Seam Type Details
Cold Rolled Seam
Release Type
Leak
Leak Type
Other
Leak Type Other
Gas Bleeding By Stopple
Class Location Type
Class 3 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
261.0
Est Cost Emergency
500.0
Est Cost Other
0.0
Gas Cost In Mcf
10.96
Est Cost Unintentional Release
614.0
Est Cost Intentional Release
0.0
Prpty
1375.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
0.0
Num Persons Hosp Not Ovnght
0.0
Num Injured Treated By Emt
0.0
Num Resident Building Affctd
0.0
Num Business Building Affctd
0.0
Accident Psig
125.0
Normal Psig
125.0
Mop Psig
150.0
Mop Cfr Section
192.619(A)(3)
Maop Established Date
1962-04-09 00:00:00
Accident Pressure
Pressure Did Not Exceed Maop
Gas Odorized System Type
Injection Pump
Gas Odorized Lvl Not Msrd Ind
Yes
Scada In Place Ind
No
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
Yes
Num Contractors Tested
1
Num Contractors Failed
0
Cause
Incorrect Operation
Cause Details
Wrong Equipment Specified Or Installed
Operation Type
Wrong Equipment Specified Or Installed
Related Failure Follow Ind
Yes
Category Type
Construction
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
E*** M******
Preparer Title
Manager Distribution Integrity
Preparer Email
E***********@s**********.com
Preparer Telephone
314-349-2932
Local Contact Name
E*** M******
Local Contact Email
E***********@s**********.com
Local Contact Telephone
314-349-2932
Authorizer Name
C**** H********
Authorizer Title
Vp Operations Services And Sms
Authorizer Telephone
314-349-2972
Authorizer Email
C**************@s**********.com
Narrative
A company contractor crew was a performing a 12-inch steel main relocation and retiring a section of main between 2 stopple fittings. The stopples were in position to shut off the flow of gas and the pipe had been cut between the stopples and blown down. The contractor employee was preparing to cap downstream of one stopple. Two vent stacks (v1 & v2) were installed downstream of the stopple with a valve and air handler on the vent nearest the stopple fitting (v1). The contractor employee inserted a gripper plug in the 12-inch main up to the v1 vent stack location. Gas was bleeding past the stopple fitting. The valve on v1 vent stack was closed. This resulted in a pressure build-up between the stopple fitting and the gripper plug and caused the gripper plug to be ejected from the open-cut end of the 12-inch steel main. The gripper plug caused a hand injury with the contractor employee and he was admitted to the hospital for treatment. A 48-hour update to the nrc was made on october 5, 2023 at 18:49 - report number 1380998. Supplemental report created: part e.1, estimated pressure at time of incident updated from 56.0 psig to 125psig. Supplemental report created 12/12/2024: part g, updating to most applicable sub-cause of "wrong equipment specified or installed"
Report Received Date | 2023-11-06 00:00:00 |
---|---|
Iyear | 2023.0 |
Report Number | 20230064.0 |
Supplemental Number | 40343.0 |
Report Type | Supplemental Final |
Operator Id | 30769 PHMSA Enforcement |
Name | Spire Missouri Inc. West |
Operator Street Address | 700 Market Street |
Operator City Name | Saint Louis |
Operator State Abbreviation | MO |
Operator Postal Code | 63101.0 |
Time Zone | Central |
Daylight Savings Ind | Yes |
Location Street Address | 310 Se Old Cannon Ball Rd |
Location City Name | Holt |
Location County Name | Clinton County |
Location State Abbreviation | MO |
Location Postal Code | 64048.0 |
Location Latitude | 39.45747 Google Maps OpenStreetMap |
Location Longitude | -94.33586 Google Maps OpenStreetMap |
Flow Cont Stopple Fitng Ind | Yes |
Nrc Rpt Num | 1380998.0 NRC Report How to search |
Additional Nrc Report Numbers | 1381071.0 |
Commodity Released Type | Natural Gas |
Unintentional Release | 56.0 |
Intentional Release | 0.0 |
Fatality Ind | No |
Fatal | 0 |
Injury Ind | Yes |
Num Emp Injuries | 0 |
Num Contr Injuries | 1 |
Num Er Injuries | 0 |
Num Worker Injuries | 0 |
Num Gp Injuries | 0 |
Injure | 1 |
Ignite Ind | No |
Num Pub Evacuated | 0.0 |
Communication State Fed Ind | Yes |
Party Initiated Communication | Operator |
Federal | No |
Location Type | Operator-Controlled Property |
Incident Area Type | Underground |
Incident Area Subtype | Exposed Due To Excavation |
Depth Of Cover | 63.0 |
Other Underground Facilities | No |
Crossing | No |
Pipe Facility Type | Investor Owned |
System Part Involved | Main |
Installation Year | 1962.0 |
Pipe Diameter | 12.0 |
Pipe Specification | Unknown |
Pipe Manufacturer | Unknown |
Material Involved | Steel |
Steel Seam Type | Other |
Steel Seam Type Details | Cold Rolled Seam |
Release Type | Leak |
Leak Type | Other |
Leak Type Other | Gas Bleeding By Stopple |
Class Location Type | Class 3 Location |
Est Cost Oper Paid | 0.0 |
Est Cost Prop Damage | 261.0 |
Est Cost Emergency | 500.0 |
Est Cost Other | 0.0 |
Gas Cost In Mcf | 10.96 |
Est Cost Unintentional Release | 614.0 |
Est Cost Intentional Release | 0.0 |
Prpty | 1375.0 |
Commercial Affected | 0.0 |
Industrial Affected | 0.0 |
Residences Affected | 0.0 |
Num Persons Hosp Not Ovnght | 0.0 |
Num Injured Treated By Emt | 0.0 |
Num Resident Building Affctd | 0.0 |
Num Business Building Affctd | 0.0 |
Accident Psig | 125.0 |
Normal Psig | 125.0 |
Mop Psig | 150.0 |
Mop Cfr Section | 192.619(A)(3) View CFR 49 §192 |
Maop Established Date | 1962-04-09 00:00:00 |
Accident Pressure | Pressure Did Not Exceed Maop |
Gas Odorized System Type | Injection Pump |
Gas Odorized Lvl Not Msrd Ind | Yes |
Scada In Place Ind | No |
Accident Identifier | Local Operating Personnel, Including Contractors |
Operator Type | Contractor Working For The Operator |
Investigation Status | No, the facility was not monitored by a controller(s) at the time of the incident |
Employee Drug Test Ind | No |
Contractor Drug Test Ind | Yes |
Num Contractors Tested | 1 |
Num Contractors Failed | 0 |
Cause | Incorrect Operation |
Cause Details | Wrong Equipment Specified Or Installed |
Operation Type | Wrong Equipment Specified Or Installed |
Related Failure Follow Ind | Yes |
Category Type | Construction |
Operator Qualification Ind | Yes |
Qualified Individuals | Yes, They Were Qualified For The Task(S) |
Preparer Name | E*** M****** |
Preparer Title | Manager Distribution Integrity |
Preparer Email | E***********@s**********.com |
Preparer Telephone | 314-349-2932 |
Local Contact Name | E*** M****** |
Local Contact Email | E***********@s**********.com |
Local Contact Telephone | 314-349-2932 |
Authorizer Name | C**** H******** |
Authorizer Title | Vp Operations Services And Sms |
Authorizer Telephone | 314-349-2972 |
Authorizer Email | C**************@s**********.com |
Narrative | A company contractor crew was a performing a 12-inch steel main relocation and retiring a section of main between 2 stopple fittings. The stopples were in position to shut off the flow of gas and the pipe had been cut between the stopples and blown down. The contractor employee was preparing to cap downstream of one stopple. Two vent stacks (v1 & v2) were installed downstream of the stopple with a valve and air handler on the vent nearest the stopple fitting (v1). The contractor employee inserted a gripper plug in the 12-inch main up to the v1 vent stack location. Gas was bleeding past the stopple fitting. The valve on v1 vent stack was closed. This resulted in a pressure build-up between the stopple fitting and the gripper plug and caused the gripper plug to be ejected from the open-cut end of the 12-inch steel main. The gripper plug caused a hand injury with the contractor employee and he was admitted to the hospital for treatment. A 48-hour update to the nrc was made on october 5, 2023 at 18:49 - report number 1380998. Supplemental report created: part e.1, estimated pressure at time of incident updated from 56.0 psig to 125psig. Supplemental report created 12/12/2024: part g, updating to most applicable sub-cause of "wrong equipment specified or installed" |
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