GD incident on 2023-10-20 — GA

Operator
Atlanta Gas Light Co
Cause
Excavation Issue
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$87,500
Incident datetime
2023-10-20 00:00 UTC
Report number
Location
GA, FULTON
Narrative
A third-party party excavator (cable east) struck and damaged an atlanta gas light company (aglc) 4-inch plastic gas main while directionally boring to install traffic signal conduit lines near 2049 sylvan road sw, atlanta. Escaping gas from the damage was ignited by an unknown ignition source and a subsequent fire occurred at the street resulting in significant property damage. At least one vehicle as well as a tractor and the directional boring rig were damaged in the fire; there was also heat damage to a large commercial sign and a diesel pump at a nearby chevron gasoline station. Upon arrival, aglc personnel secured the area and monitored the surrounding area for gas. Gas was shut-off to the damaged area at 12:06 pm by operating two (2) valves and performing one (1) squeeze off operation. A locate request was made on september 6, 2023, by cable east (excavator) to "locate the intersection of sr 166 ramps east bound off & on and sylvan rd sw 200' in all direction entire row". Aglc facilities were marked by stake center locating to satisfy this request on september 20, 2023, at 10:19 am. Investigation of the site revealed that the locate marks were not accurate at the point of damage; the nearest locate mark to where the 4-inch plastic main was damaged was approximately seven (7) feet away. Because the excavator did not verify the location of aglc facilities by pot holing and instead blindly crossed the marks on the ground which ran parallel to the actual location of the gas main, the gas main was damaged. Had the excavator potholed, it would have determined the location of the main was not consistent with the marks on the ground at the point of crossing and taken steps to determine the actual location of the gas main. Additional nrc report number 1379789 was created for the same event after a supplemental call was placed with the nrc to update the initial telephonic notice.
Detailed record list
Report Received Date
2023-10-20 00:00:00
Iyear
2023.0
Report Number
20230059.0
Supplemental Number
38679.0
Report Type
Original Final
Operator Id
Name
Atlanta Gas Light Co
Operator Street Address
10 Peachtree Place Ne
Operator City Name
Atlanta
Operator State Abbreviation
GA
Operator Postal Code
30309.0
Time Zone
Eastern
Daylight Savings Ind
Yes
Location Street Address
2049 Sylvan Road Sw
Location City Name
Atlanta
Location County Name
Fulton
Location State Abbreviation
GA
Location Postal Code
30310.0
Location Latitude
Location Longitude
Flow Cont Key Crit Ind
Yes
Flow Cont Main Valve Ind
Yes
Flow Cont Squeeze Off Ind
Yes
Nrc Rpt Num
Additional Nrc Report Numbers
1379789.0
Commodity Released Type
Natural Gas
Unintentional Release
500.0
Intentional Release
0.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
Yes
How Extinguished
Local/state/federal Emergency Responder
Gas Consumed By Fire In Mcf
500
Explode Ind
No
Num Pub Evacuated
3.0
Federal
No
Location Type
Public Property
Incident Area Type
Underground
Incident Area Subtype
Under Pavement
Depth Of Cover
48.0
Other Underground Facilities
No
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Main
Installation Year
2001.0
Pipe Diameter
4.0
Pipe Specification
Astm D2513
Pipe Manufacturer
Uponor
Material Involved
Plastic
Plastic Type
Polyethylene (Pe)
Plastic Sdr
11.5
Material Pe Pipe Code
2406
Release Type
Mechanical Puncture
Puncture Axial
3.7
Puncture Circum
3.7
Class Location Type
Class 3 Location
Est Cost Oper Paid
300000.0
Est Cost Prop Damage
87500.0
Est Cost Emergency
68196.0
Est Cost Other
0.0
Gas Cost In Mcf
2.815
Est Cost Unintentional Release
1408.0
Est Cost Intentional Release
0.0
Prpty
457104.0
Commercial Affected
5.0
Industrial Affected
0.0
Residences Affected
0.0
Num Persons Hosp Not Ovnght
0.0
Num Injured Treated By Emt
0.0
Num Resident Building Affctd
0.0
Num Business Building Affctd
0.0
Accident Psig
40.0
Normal Psig
45.0
Mop Psig
60.0
Mop Cfr Section
192.619(A)(2)
Maop Established Date
2001-04-16 00:00:00
Accident Pressure
Pressure Did Not Exceed Maop
Gas Odorized System Type
Injection Pump
Gas Odorized Level
5.3
Scada In Place Ind
No
Accident Identifier
Notification From Emergency Responder
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
Yes
Num Contractors Tested
1
Num Contractors Failed
0
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
Yes
One Call System Ind
Yes
State Law Exempt Ind
No
Notify Cga Dirt
Yes
Public Row Ind
Yes
Public Subtype
City Street
Excavator Type
Contractor
Excavator Equipment
Directional Drilling
Work Performed
Traffic Signal
One Call Notified Ind
Yes
One Call Ticket Num
230731000000.0
Locator Type
Contract Locator
Visible Marks
Yes
Service Interruption
Yes
Service Interruption Hours
24.0
Root Cause Category
Excavation Issue
Root Cause Type
Improper Excavation Practice Not Listed Above
Io Follow Procedure Ind
Yes
Preparer Name
R**** M*******
Preparer Title
Principal Compliance Engineer
Preparer Email
R*******@s*********.com
Preparer Telephone
(404) 584-3733
Preparer Fax
(404) 584-4710
Authorizer Name
R*** L***
Authorizer Title
Director Compliance And Prm
Authorizer Telephone
(404) 584-3552
Authorizer Email
R****@s*********.com
Narrative
A third-party party excavator (cable east) struck and damaged an atlanta gas light company (aglc) 4-inch plastic gas main while directionally boring to install traffic signal conduit lines near 2049 sylvan road sw, atlanta. Escaping gas from the damage was ignited by an unknown ignition source and a subsequent fire occurred at the street resulting in significant property damage. At least one vehicle as well as a tractor and the directional boring rig were damaged in the fire; there was also heat damage to a large commercial sign and a diesel pump at a nearby chevron gasoline station. Upon arrival, aglc personnel secured the area and monitored the surrounding area for gas. Gas was shut-off to the damaged area at 12:06 pm by operating two (2) valves and performing one (1) squeeze off operation. A locate request was made on september 6, 2023, by cable east (excavator) to "locate the intersection of sr 166 ramps east bound off & on and sylvan rd sw 200' in all direction entire row". Aglc facilities were marked by stake center locating to satisfy this request on september 20, 2023, at 10:19 am. Investigation of the site revealed that the locate marks were not accurate at the point of damage; the nearest locate mark to where the 4-inch plastic main was damaged was approximately seven (7) feet away. Because the excavator did not verify the location of aglc facilities by pot holing and instead blindly crossed the marks on the ground which ran parallel to the actual location of the gas main, the gas main was damaged. Had the excavator potholed, it would have determined the location of the main was not consistent with the marks on the ground at the point of crossing and taken steps to determine the actual location of the gas main. Additional nrc report number 1379789 was created for the same event after a supplemental call was placed with the nrc to update the initial telephonic notice.
Report Received Date 2023-10-20 00:00:00
Iyear 2023.0
Report Number 20230059.0
Supplemental Number 38679.0
Report Type Original Final
Operator Id 792 PHMSA Enforcement
Name Atlanta Gas Light Co
Operator Street Address 10 Peachtree Place Ne
Operator City Name Atlanta
Operator State Abbreviation GA
Operator Postal Code 30309.0
Time Zone Eastern
Daylight Savings Ind Yes
Location Street Address 2049 Sylvan Road Sw
Location City Name Atlanta
Location County Name Fulton
Location State Abbreviation GA
Location Postal Code 30310.0
Location Latitude 33.698291 Google Maps OpenStreetMap
Location Longitude -84.418228 Google Maps OpenStreetMap
Flow Cont Key Crit Ind Yes
Flow Cont Main Valve Ind Yes
Flow Cont Squeeze Off Ind Yes
Nrc Rpt Num 1379609.0 NRC Report How to search
Additional Nrc Report Numbers 1379789.0
Commodity Released Type Natural Gas
Unintentional Release 500.0
Intentional Release 0.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind Yes
How Extinguished Local/state/federal Emergency Responder
Gas Consumed By Fire In Mcf 500
Explode Ind No
Num Pub Evacuated 3.0
Federal No
Location Type Public Property
Incident Area Type Underground
Incident Area Subtype Under Pavement
Depth Of Cover 48.0
Other Underground Facilities No
Crossing No
Pipe Facility Type Investor Owned
System Part Involved Main
Installation Year 2001.0
Pipe Diameter 4.0
Pipe Specification Astm D2513
Pipe Manufacturer Uponor
Material Involved Plastic
Plastic Type Polyethylene (Pe)
Plastic Sdr 11.5
Material Pe Pipe Code 2406
Release Type Mechanical Puncture
Puncture Axial 3.7
Puncture Circum 3.7
Class Location Type Class 3 Location
Est Cost Oper Paid 300000.0
Est Cost Prop Damage 87500.0
Est Cost Emergency 68196.0
Est Cost Other 0.0
Gas Cost In Mcf 2.815
Est Cost Unintentional Release 1408.0
Est Cost Intentional Release 0.0
Prpty 457104.0
Commercial Affected 5.0
Industrial Affected 0.0
Residences Affected 0.0
Num Persons Hosp Not Ovnght 0.0
Num Injured Treated By Emt 0.0
Num Resident Building Affctd 0.0
Num Business Building Affctd 0.0
Accident Psig 40.0
Normal Psig 45.0
Mop Psig 60.0
Mop Cfr Section 192.619(A)(2) View CFR 49 §192
Maop Established Date 2001-04-16 00:00:00
Accident Pressure Pressure Did Not Exceed Maop
Gas Odorized System Type Injection Pump
Gas Odorized Level 5.3
Scada In Place Ind No
Accident Identifier Notification From Emergency Responder
Investigation Status No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind No
Contractor Drug Test Ind Yes
Num Contractors Tested 1
Num Contractors Failed 0
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind Yes
One Call System Ind Yes
State Law Exempt Ind No
Notify Cga Dirt Yes
Public Row Ind Yes
Public Subtype City Street
Excavator Type Contractor
Excavator Equipment Directional Drilling
Work Performed Traffic Signal
One Call Notified Ind Yes
One Call Ticket Num 230731000000.0
Locator Type Contract Locator
Visible Marks Yes
Service Interruption Yes
Service Interruption Hours 24.0
Root Cause Category Excavation Issue
Root Cause Type Improper Excavation Practice Not Listed Above
Io Follow Procedure Ind Yes
Preparer Name R**** M*******
Preparer Title Principal Compliance Engineer
Preparer Email R*******@s*********.com
Preparer Telephone (404) 584-3733
Preparer Fax (404) 584-4710
Authorizer Name R*** L***
Authorizer Title Director Compliance And Prm
Authorizer Telephone (404) 584-3552
Authorizer Email R****@s*********.com
Narrative A third-party party excavator (cable east) struck and damaged an atlanta gas light company (aglc) 4-inch plastic gas main while directionally boring to install traffic signal conduit lines near 2049 sylvan road sw, atlanta. Escaping gas from the damage was ignited by an unknown ignition source and a subsequent fire occurred at the street resulting in significant property damage. At least one vehicle as well as a tractor and the directional boring rig were damaged in the fire; there was also heat damage to a large commercial sign and a diesel pump at a nearby chevron gasoline station. Upon arrival, aglc personnel secured the area and monitored the surrounding area for gas. Gas was shut-off to the damaged area at 12:06 pm by operating two (2) valves and performing one (1) squeeze off operation. A locate request was made on september 6, 2023, by cable east (excavator) to "locate the intersection of sr 166 ramps east bound off & on and sylvan rd sw 200' in all direction entire row". Aglc facilities were marked by stake center locating to satisfy this request on september 20, 2023, at 10:19 am. Investigation of the site revealed that the locate marks were not accurate at the point of damage; the nearest locate mark to where the 4-inch plastic main was damaged was approximately seven (7) feet away. Because the excavator did not verify the location of aglc facilities by pot holing and instead blindly crossed the marks on the ground which ran parallel to the actual location of the gas main, the gas main was damaged. Had the excavator potholed, it would have determined the location of the main was not consistent with the marks on the ground at the point of crossing and taken steps to determine the actual location of the gas main. Additional nrc report number 1379789 was created for the same event after a supplemental call was placed with the nrc to update the initial telephonic notice.

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