Incident details
Operator, cause, commodity and consequences with raw source fields.
GD incident on 2023-10-06 — NM
Operator
New Mexico Gas Company
Cause
Pipe, Weld, Or Joint Failure
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$0
Incident datetime
2023-10-06 00:00 UTC
Report number
Location
NM, BERNALILLO
Narrative
On september 7, 2023, an explosion occurred at 14:18 at 4100 ridgeley ave ne in albuquerque, nm 87108. At 14:37, nmgc was notified by albuquerque fire and rescue of a house explosion. Nmgc arrived at the property at 14:52. Gas was escaping from the riser when the nmgc technician arrived. Gas was under control at 15:33 at the riser. Nmgc began probing for gas at 15:33. The nmgc responding crew discovered gas concentration readings of 100% gas in the street directly in front of 4100 ridgeley ave ne. Nmgc exposed the 2-inch pe pipe, where the section of main was offset with a dogleg that was installed in 2017. A 2x3-inch leak clamp was installed as a temporary repair. The section of main was squeezed off at 21:30 and capped as a permanent repair. There were two residents of 4100 ridgeley avenue who were treated for non-life threatening injuries and released. At 17:15, gas odorant testing with a heath odorometer was conducted revealing sufficient odorant at 0.50% gas-in-air (12.5% lel). Additional gas odorant testing with a heath odorometer was performed showing appropriate odorant levels. Laboratory tests were conducted on october 25, 2023 which revealed a lack of complete fusion on butt weld. Regarding questions part a #7 and part a #21c, the form does not allow an entry of "unknown" because a calculation cannot be performed due to limited or unknown information needed to perform the calculation.
Detailed record list
Report Received Date
2023-10-06 00:00:00
Iyear
2023.0
Report Number
20230057.0
Supplemental Number
39364.0
Report Type
Supplemental Final
Operator Id
6141
Name
New Mexico Gas Company
Operator Street Address
7120 Wyoming Blvd N.e. Suite 20
Operator City Name
Albuquerque
Operator State Abbreviation
NM
Operator Postal Code
87109.0
Time Zone
Mountain
Daylight Savings Ind
Yes
Location Street Address
4100 Ridgeley Dr Ne
Location City Name
Albuquerque
Location County Name
Bernalillo
Location State Abbreviation
NM
Location Postal Code
87108.0
Location Latitude
35.08043
Location Longitude
-106.598806
Flow Cont Squeeze Off Ind
Yes
Flow Cont Other Ind
Yes
Flow Cont Other Detail
2x3 Leak Clamp On Main And Plugged Off Riser
Nrc Rpt Num
1378470.0
Additional Nrc Report Numbers
1378626.0
Commodity Released Type
Natural Gas
Unintentional Release
1.0
Intentional Release
0.083
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
Yes
How Extinguished
Other
How Extinguished Other Detail
No Residual Fire After Initial Ignition Event.
Gas Consumed By Fire In Mcf
1
Explode Ind
Yes
Num Pub Evacuated
19.0
Federal
No
Location Type
Public Property
Incident Area Type
Underground
Incident Area Subtype
Under Pavement
Depth Of Cover
45.0
Other Underground Facilities
Yes
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Main
Installation Year
2017.0
Manufactured Year
2017.0
Pipe Diameter
2.0
Pipe Specification
Astm D2513
Pipe Manufacturer
Performance Pipe
Material Involved
Plastic
Plastic Type
Polyethylene (Pe)
Plastic Sdr
11
Material Pe Pipe Code
4710
Release Type
Leak
Leak Type
Other
Leak Type Other
Lack Of Complete Fusion
Class Location Type
Class 3 Location
Est Cost Oper Paid
500000.0
Est Cost Prop Damage
0.0
Est Cost Emergency
11250.0
Est Cost Other
0.0
Gas Cost In Mcf
4.99
Est Cost Unintentional Release
5.0
Est Cost Intentional Release
0.0
Prpty
511255.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
10.0
Num Persons Hosp Not Ovnght
2.0
Num Injured Treated By Emt
0.0
Num Resident Building Affctd
10.0
Num Business Building Affctd
0.0
Accident Psig
56.0
Normal Psig
56.0
Mop Psig
60.0
Mop Cfr Section
192.619(A)(3)
Maop Established Date
2015-11-19 00:00:00
Accident Pressure
Pressure Did Not Exceed Maop
Gas Odorized System Type
Injection Pump
Gas Odorized Level
12.5
Scada In Place Ind
No
Accident Identifier
Notification From Emergency Responder
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Existing scada equipment would have given no indication of an issue at this location.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Pipe, Weld, Or Joint Failure
Cause Details
Fusion Joint
Pwjf Failure Type
Fusion Joint
Plastic Joint Subtype
Butt, Heat Fusion
Fpw Installed Year
2017
Fpw First Plastic Type
Polyethylene (Pe)
Fpw Second Plastic Type
Polyethylene (Pe)
Additional Lack Fusion Ind
Yes
Result Construction Ind
Yes
Result Construction Subtype
Poor Workmanship
Hydrotest Conducted Ind
No
Preparer Name
R***** R S****
Preparer Title
Manager Psms Technical Training
Preparer Email
R***********@n****.com
Preparer Telephone
5056973169
Authorizer Name
A***** M*******
Authorizer Title
Director Safety Pipeline Safety Tech Training
Authorizer Telephone
5056973518
Authorizer Email
A**************@n****.com
Narrative
On september 7, 2023, an explosion occurred at 14:18 at 4100 ridgeley ave ne in albuquerque, nm 87108. At 14:37, nmgc was notified by albuquerque fire and rescue of a house explosion. Nmgc arrived at the property at 14:52. Gas was escaping from the riser when the nmgc technician arrived. Gas was under control at 15:33 at the riser. Nmgc began probing for gas at 15:33. The nmgc responding crew discovered gas concentration readings of 100% gas in the street directly in front of 4100 ridgeley ave ne. Nmgc exposed the 2-inch pe pipe, where the section of main was offset with a dogleg that was installed in 2017. A 2x3-inch leak clamp was installed as a temporary repair. The section of main was squeezed off at 21:30 and capped as a permanent repair. There were two residents of 4100 ridgeley avenue who were treated for non-life threatening injuries and released. At 17:15, gas odorant testing with a heath odorometer was conducted revealing sufficient odorant at 0.50% gas-in-air (12.5% lel). Additional gas odorant testing with a heath odorometer was performed showing appropriate odorant levels. Laboratory tests were conducted on october 25, 2023 which revealed a lack of complete fusion on butt weld. Regarding questions part a #7 and part a #21c, the form does not allow an entry of "unknown" because a calculation cannot be performed due to limited or unknown information needed to perform the calculation.
Report Received Date | 2023-10-06 00:00:00 |
---|---|
Iyear | 2023.0 |
Report Number | 20230057.0 |
Supplemental Number | 39364.0 |
Report Type | Supplemental Final |
Operator Id | 6141 PHMSA Enforcement |
Name | New Mexico Gas Company |
Operator Street Address | 7120 Wyoming Blvd N.e. Suite 20 |
Operator City Name | Albuquerque |
Operator State Abbreviation | NM |
Operator Postal Code | 87109.0 |
Time Zone | Mountain |
Daylight Savings Ind | Yes |
Location Street Address | 4100 Ridgeley Dr Ne |
Location City Name | Albuquerque |
Location County Name | Bernalillo |
Location State Abbreviation | NM |
Location Postal Code | 87108.0 |
Location Latitude | 35.08043 Google Maps OpenStreetMap |
Location Longitude | -106.598806 Google Maps OpenStreetMap |
Flow Cont Squeeze Off Ind | Yes |
Flow Cont Other Ind | Yes |
Flow Cont Other Detail | 2x3 Leak Clamp On Main And Plugged Off Riser |
Nrc Rpt Num | 1378470.0 NRC Report How to search |
Additional Nrc Report Numbers | 1378626.0 |
Commodity Released Type | Natural Gas |
Unintentional Release | 1.0 |
Intentional Release | 0.083 |
Fatality Ind | No |
Fatal | 0 |
Injury Ind | No |
Injure | 0 |
Ignite Ind | Yes |
How Extinguished | Other |
How Extinguished Other Detail | No Residual Fire After Initial Ignition Event. |
Gas Consumed By Fire In Mcf | 1 |
Explode Ind | Yes |
Num Pub Evacuated | 19.0 |
Federal | No |
Location Type | Public Property |
Incident Area Type | Underground |
Incident Area Subtype | Under Pavement |
Depth Of Cover | 45.0 |
Other Underground Facilities | Yes |
Crossing | No |
Pipe Facility Type | Investor Owned |
System Part Involved | Main |
Installation Year | 2017.0 |
Manufactured Year | 2017.0 |
Pipe Diameter | 2.0 |
Pipe Specification | Astm D2513 |
Pipe Manufacturer | Performance Pipe |
Material Involved | Plastic |
Plastic Type | Polyethylene (Pe) |
Plastic Sdr | 11 |
Material Pe Pipe Code | 4710 |
Release Type | Leak |
Leak Type | Other |
Leak Type Other | Lack Of Complete Fusion |
Class Location Type | Class 3 Location |
Est Cost Oper Paid | 500000.0 |
Est Cost Prop Damage | 0.0 |
Est Cost Emergency | 11250.0 |
Est Cost Other | 0.0 |
Gas Cost In Mcf | 4.99 |
Est Cost Unintentional Release | 5.0 |
Est Cost Intentional Release | 0.0 |
Prpty | 511255.0 |
Commercial Affected | 0.0 |
Industrial Affected | 0.0 |
Residences Affected | 10.0 |
Num Persons Hosp Not Ovnght | 2.0 |
Num Injured Treated By Emt | 0.0 |
Num Resident Building Affctd | 10.0 |
Num Business Building Affctd | 0.0 |
Accident Psig | 56.0 |
Normal Psig | 56.0 |
Mop Psig | 60.0 |
Mop Cfr Section | 192.619(A)(3) View CFR 49 §192 |
Maop Established Date | 2015-11-19 00:00:00 |
Accident Pressure | Pressure Did Not Exceed Maop |
Gas Odorized System Type | Injection Pump |
Gas Odorized Level | 12.5 |
Scada In Place Ind | No |
Accident Identifier | Notification From Emergency Responder |
Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
Investigation Status Details | Existing scada equipment would have given no indication of an issue at this location. |
Employee Drug Test Ind | No |
Contractor Drug Test Ind | No |
Cause | Pipe, Weld, Or Joint Failure |
Cause Details | Fusion Joint |
Pwjf Failure Type | Fusion Joint |
Plastic Joint Subtype | Butt, Heat Fusion |
Fpw Installed Year | 2017 |
Fpw First Plastic Type | Polyethylene (Pe) |
Fpw Second Plastic Type | Polyethylene (Pe) |
Additional Lack Fusion Ind | Yes |
Result Construction Ind | Yes |
Result Construction Subtype | Poor Workmanship |
Hydrotest Conducted Ind | No |
Preparer Name | R***** R S**** |
Preparer Title | Manager Psms Technical Training |
Preparer Email | R***********@n****.com |
Preparer Telephone | 5056973169 |
Authorizer Name | A***** M******* |
Authorizer Title | Director Safety Pipeline Safety Tech Training |
Authorizer Telephone | 5056973518 |
Authorizer Email | A**************@n****.com |
Narrative | On september 7, 2023, an explosion occurred at 14:18 at 4100 ridgeley ave ne in albuquerque, nm 87108. At 14:37, nmgc was notified by albuquerque fire and rescue of a house explosion. Nmgc arrived at the property at 14:52. Gas was escaping from the riser when the nmgc technician arrived. Gas was under control at 15:33 at the riser. Nmgc began probing for gas at 15:33. The nmgc responding crew discovered gas concentration readings of 100% gas in the street directly in front of 4100 ridgeley ave ne. Nmgc exposed the 2-inch pe pipe, where the section of main was offset with a dogleg that was installed in 2017. A 2x3-inch leak clamp was installed as a temporary repair. The section of main was squeezed off at 21:30 and capped as a permanent repair. There were two residents of 4100 ridgeley avenue who were treated for non-life threatening injuries and released. At 17:15, gas odorant testing with a heath odorometer was conducted revealing sufficient odorant at 0.50% gas-in-air (12.5% lel). Additional gas odorant testing with a heath odorometer was performed showing appropriate odorant levels. Laboratory tests were conducted on october 25, 2023 which revealed a lack of complete fusion on butt weld. Regarding questions part a #7 and part a #21c, the form does not allow an entry of "unknown" because a calculation cannot be performed due to limited or unknown information needed to perform the calculation. |
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