Incident details
Operator, cause, commodity and consequences with raw source fields.
GD incident on 2023-09-06 — WV
Operator
Mountaineer Gas Co
Cause
Excavation Issue
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$3,000
Incident datetime
2023-09-06 00:00 UTC
Report number
Location
WV, KANAWHA
Narrative
3j underground llc working for b n d services llc working for fiber management services llc/securenet fiber internet to install fiber conduit with a directional bore machine. 3j failed to hand-dig or spot the gas facilities while boring. On the first of two tries, the boring head punched through the center of the 4 steel main and gas migrated into a nearby damaged sewer line. 3j then bored a second hole above the mgc pipe and installed the plastic conduit, called mgc's locator directly to report an odor of gas, and left the scene before mgc locator arrived on scene and notified mgc dispatch. While mgc personnel were investigating the odor of gas, the house at 1321 virginia ave exploded and caught fire. Additional mgc personnel and equipment were called in to find and repair the damaged pipe. Damage to the pipe shows evidence of multiple points of contact.
Detailed record list
Report Received Date
2023-09-06 00:00:00
Iyear
2023.0
Report Number
20230049.0
Supplemental Number
39871.0
Report Type
Supplemental Final
Operator Id
12878
Name
Mountaineer Gas Co
Operator Street Address
501 56th St. Se
Operator City Name
Charleston
Operator State Abbreviation
WV
Operator Postal Code
25304.0
Time Zone
Eastern
Daylight Savings Ind
Yes
Location Street Address
1321 Virginia Ave
Location City Name
Dunbar
Location County Name
Kanawha
Location State Abbreviation
WV
Location Postal Code
25064.0
Location Latitude
38.36469
Location Longitude
-81.74176
Flow Cont Other Ind
Yes
Flow Cont Other Detail
Full Circle Leak Clamp
Nrc Rpt Num
1375509.0
Additional Nrc Report Numbers
1375718.0
Commodity Released Type
Natural Gas
Unintentional Release
209.0
Intentional Release
0.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
Yes
How Extinguished
Local/state/federal Emergency Responder
Gas Consumed By Fire In Mcf
0.56
Explode Ind
Yes
Num Pub Evacuated
3.0
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Federal
No
Location Type
Public Property
Incident Area Type
Underground
Incident Area Subtype
Under Pavement
Depth Of Cover
32.0
Other Underground Facilities
Yes
Crossing
Yes
Road Crossing Ind
Yes
Road Type
Uncased
Pipe Facility Type
Privately Owned
System Part Involved
Main
Installation Year
1968.0
Pipe Diameter
4.0
Pipe Specification
Unknown
Pipe Manufacturer
Unknown
Material Involved
Steel
Steel Seam Type
Other
Steel Seam Type Details
Unknown
Wt Steel
0.188
Release Type
Mechanical Puncture
Puncture Axial
8.5
Puncture Circum
4.0
Class Location Type
Class 3 Location
Est Cost Oper Paid
200000.0
Est Cost Prop Damage
3000.0
Est Cost Emergency
14000.0
Est Cost Other
10000.0
Est Cost Other Details
Emergency Responders
Gas Cost In Mcf
6.739
Est Cost Unintentional Release
1408.0
Est Cost Intentional Release
0.0
Prpty
228408.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
1.0
Num Persons Hosp Not Ovnght
1.0
Num Injured Treated By Emt
1.0
Num Resident Building Affctd
1.0
Num Business Building Affctd
0.0
Accident Psig
0.5
Normal Psig
0.5
Mop Psig
0.5
Mop Cfr Section
192.623
Maop Established Date
1968-01-01 00:00:00
Accident Pressure
Pressure Did Not Exceed Maop
Gas Odorized System Type
Injection Pump
Gas Odorized Level
2
Scada In Place Ind
No
Accident Identifier
Notification From Third Party That Caused The Incident
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Incident caused by excavation damage.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
Yes
One Call System Ind
Yes
State Law Exempt Ind
No
Notify Cga Dirt
Yes
Public Row Ind
Yes
Public Subtype
City Street
Joint Trench Ind
No
Cross Bore Ind
Yes
Depth Of Grade
18� � 36�
Excavator Type
Utility
Excavator Equipment
Directional Drilling
Work Performed
Telecommunications
One Call Notified Ind
Yes
One Call Ticket Num
2321330168.0
White Lined Ind
Unknown
Locator Type
Facility Owner
Visible Marks
Yes
Service Interruption
No
Root Cause Category
Excavation Issue
Root Cause Type
Improper Excavation Practice Not Listed Above
Preparer Name
P***** K******
Preparer Title
Manager-Engineering And Compliance
Preparer Email
P************@m****.com
Preparer Telephone
8884204427
Local Contact Name
R**** D**
Local Contact Email
R*******@m****.com
Local Contact Telephone
8884204427
Authorizer Name
T***** W*******
Authorizer Title
Vp Gas Supply And Technical Services
Authorizer Telephone
8884204427
Authorizer Email
T*************@m****.com
Narrative
3j underground llc working for b n d services llc working for fiber management services llc/securenet fiber internet to install fiber conduit with a directional bore machine. 3j failed to hand-dig or spot the gas facilities while boring. On the first of two tries, the boring head punched through the center of the 4 steel main and gas migrated into a nearby damaged sewer line. 3j then bored a second hole above the mgc pipe and installed the plastic conduit, called mgc's locator directly to report an odor of gas, and left the scene before mgc locator arrived on scene and notified mgc dispatch. While mgc personnel were investigating the odor of gas, the house at 1321 virginia ave exploded and caught fire. Additional mgc personnel and equipment were called in to find and repair the damaged pipe. Damage to the pipe shows evidence of multiple points of contact.
Report Received Date | 2023-09-06 00:00:00 |
---|---|
Iyear | 2023.0 |
Report Number | 20230049.0 |
Supplemental Number | 39871.0 |
Report Type | Supplemental Final |
Operator Id | 12878 PHMSA Enforcement |
Name | Mountaineer Gas Co |
Operator Street Address | 501 56th St. Se |
Operator City Name | Charleston |
Operator State Abbreviation | WV |
Operator Postal Code | 25304.0 |
Time Zone | Eastern |
Daylight Savings Ind | Yes |
Location Street Address | 1321 Virginia Ave |
Location City Name | Dunbar |
Location County Name | Kanawha |
Location State Abbreviation | WV |
Location Postal Code | 25064.0 |
Location Latitude | 38.36469 Google Maps OpenStreetMap |
Location Longitude | -81.74176 Google Maps OpenStreetMap |
Flow Cont Other Ind | Yes |
Flow Cont Other Detail | Full Circle Leak Clamp |
Nrc Rpt Num | 1375509.0 NRC Report How to search |
Additional Nrc Report Numbers | 1375718.0 |
Commodity Released Type | Natural Gas |
Unintentional Release | 209.0 |
Intentional Release | 0.0 |
Fatality Ind | No |
Fatal | 0 |
Injury Ind | No |
Injure | 0 |
Ignite Ind | Yes |
How Extinguished | Local/state/federal Emergency Responder |
Gas Consumed By Fire In Mcf | 0.56 |
Explode Ind | Yes |
Num Pub Evacuated | 3.0 |
Communication State Fed Ind | Yes |
Party Initiated Communication | Operator |
Federal | No |
Location Type | Public Property |
Incident Area Type | Underground |
Incident Area Subtype | Under Pavement |
Depth Of Cover | 32.0 |
Other Underground Facilities | Yes |
Crossing | Yes |
Road Crossing Ind | Yes |
Road Type | Uncased |
Pipe Facility Type | Privately Owned |
System Part Involved | Main |
Installation Year | 1968.0 |
Pipe Diameter | 4.0 |
Pipe Specification | Unknown |
Pipe Manufacturer | Unknown |
Material Involved | Steel |
Steel Seam Type | Other |
Steel Seam Type Details | Unknown |
Wt Steel | 0.188 |
Release Type | Mechanical Puncture |
Puncture Axial | 8.5 |
Puncture Circum | 4.0 |
Class Location Type | Class 3 Location |
Est Cost Oper Paid | 200000.0 |
Est Cost Prop Damage | 3000.0 |
Est Cost Emergency | 14000.0 |
Est Cost Other | 10000.0 |
Est Cost Other Details | Emergency Responders |
Gas Cost In Mcf | 6.739 |
Est Cost Unintentional Release | 1408.0 |
Est Cost Intentional Release | 0.0 |
Prpty | 228408.0 |
Commercial Affected | 0.0 |
Industrial Affected | 0.0 |
Residences Affected | 1.0 |
Num Persons Hosp Not Ovnght | 1.0 |
Num Injured Treated By Emt | 1.0 |
Num Resident Building Affctd | 1.0 |
Num Business Building Affctd | 0.0 |
Accident Psig | 0.5 |
Normal Psig | 0.5 |
Mop Psig | 0.5 |
Mop Cfr Section | 192.623 View CFR 49 §192 |
Maop Established Date | 1968-01-01 00:00:00 |
Accident Pressure | Pressure Did Not Exceed Maop |
Gas Odorized System Type | Injection Pump |
Gas Odorized Level | 2 |
Scada In Place Ind | No |
Accident Identifier | Notification From Third Party That Caused The Incident |
Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
Investigation Status Details | Incident caused by excavation damage. |
Employee Drug Test Ind | No |
Contractor Drug Test Ind | No |
Cause | Excavation Damage |
Cause Details | Excavation Damage By Third Party |
Ex Party Type | Excavation Damage By Third Party |
Prior Notification Ind | Yes |
One Call System Ind | Yes |
State Law Exempt Ind | No |
Notify Cga Dirt | Yes |
Public Row Ind | Yes |
Public Subtype | City Street |
Joint Trench Ind | No |
Cross Bore Ind | Yes |
Depth Of Grade | 18� � 36� |
Excavator Type | Utility |
Excavator Equipment | Directional Drilling |
Work Performed | Telecommunications |
One Call Notified Ind | Yes |
One Call Ticket Num | 2321330168.0 |
White Lined Ind | Unknown |
Locator Type | Facility Owner |
Visible Marks | Yes |
Service Interruption | No |
Root Cause Category | Excavation Issue |
Root Cause Type | Improper Excavation Practice Not Listed Above |
Preparer Name | P***** K****** |
Preparer Title | Manager-Engineering And Compliance |
Preparer Email | P************@m****.com |
Preparer Telephone | 8884204427 |
Local Contact Name | R**** D** |
Local Contact Email | R*******@m****.com |
Local Contact Telephone | 8884204427 |
Authorizer Name | T***** W******* |
Authorizer Title | Vp Gas Supply And Technical Services |
Authorizer Telephone | 8884204427 |
Authorizer Email | T*************@m****.com |
Narrative | 3j underground llc working for b n d services llc working for fiber management services llc/securenet fiber internet to install fiber conduit with a directional bore machine. 3j failed to hand-dig or spot the gas facilities while boring. On the first of two tries, the boring head punched through the center of the 4 steel main and gas migrated into a nearby damaged sewer line. 3j then bored a second hole above the mgc pipe and installed the plastic conduit, called mgc's locator directly to report an odor of gas, and left the scene before mgc locator arrived on scene and notified mgc dispatch. While mgc personnel were investigating the odor of gas, the house at 1321 virginia ave exploded and caught fire. Additional mgc personnel and equipment were called in to find and repair the damaged pipe. Damage to the pipe shows evidence of multiple points of contact. |
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