Incident details
Operator, cause, commodity and consequences with raw source fields.
GD incident on 2023-08-31 — IA
Operator
Midamerican Energy Company
Cause
Excavation Issue
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$2,000
Incident datetime
2023-08-31 00:00 UTC
Report number
Location
IA, POLK
Narrative
Hartco cable, inc. (third party contractor) bored into a 16-inch natural gas steel main while installing cable tv at 1400 nw 86th street in clive, iowa on august 2, 2023. The boring head punctured a four-inch by two-inch hole in the lower third of the main that was at a six-foot depth. No services were interrupted and there was no ignition or injuries. Due to the size and depth of the main, it took a significant amount of time to repair the damage and 6.771 mcf of natural gas was released to atmosphere. The nrc was initially notified (report 1375040) on august 2 and a 48-hour follow-up report was submitted (report 1375241).
Detailed record list
Report Received Date
2023-08-31 00:00:00
Iyear
2023.0
Report Number
20230046.0
Supplemental Number
38482.0
Report Type
Original Final
Operator Id
30750
Name
Midamerican Energy Company
Operator Street Address
401 Douglas Street Po Box 778
Operator City Name
Sioux City
Operator State Abbreviation
IA
Operator Postal Code
51101.0
Time Zone
Central
Daylight Savings Ind
Yes
Location Street Address
1400 Nw 86th Street
Location City Name
Clive
Location County Name
Polk
Location State Abbreviation
IA
Location Postal Code
50325.0
Location Latitude
41.60312
Location Longitude
-93.73654
Flow Cont Key Crit Ind
Yes
Flow Cont Main Valve Ind
Yes
Nrc Rpt Num
1375040.0
Additional Nrc Report Numbers
1375241.0
Commodity Released Type
Natural Gas
Unintentional Release
6771.0
Intentional Release
0.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Num Pub Evacuated
17.0
Federal
No
Location Type
Public Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
60.0
Other Underground Facilities
No
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Main
Installation Year
1968.0
Pipe Diameter
16.0
Pipe Specification
Unknown
Pipe Manufacturer
Unknown
Material Involved
Steel
Steel Seam Type
Other
Steel Seam Type Details
Unknown
Release Type
Mechanical Puncture
Puncture Axial
4.0
Puncture Circum
2.0
Class Location Type
Class 4 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
2000.0
Est Cost Emergency
36755.0
Est Cost Other
0.0
Gas Cost In Mcf
2.3395
Est Cost Unintentional Release
15841.0
Est Cost Intentional Release
0.0
Prpty
54596.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
0.0
Num Persons Hosp Not Ovnght
0.0
Num Injured Treated By Emt
0.0
Num Resident Building Affctd
0.0
Num Business Building Affctd
2.0
Accident Psig
90.0
Normal Psig
90.0
Mop Psig
125.0
Mop Cfr Section
192.619(A)(4)
Maop Established Date
1988-10-02 00:00:00
Accident Pressure
Pressure Did Not Exceed Maop
Gas Odorized System Type
Injection Pump
Gas Odorized Lvl Not Msrd Ind
Yes
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Notification From Emergency Responder
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
Yes
One Call System Ind
Yes
State Law Exempt Ind
No
Notify Cga Dirt
No
Public Row Ind
Yes
Public Subtype
City Street
Excavator Type
Contractor
Excavator Equipment
Boring
Work Performed
Cable Tv
One Call Notified Ind
Yes
One Call Ticket Num
232061755.0
Locator Type
Contract Locator
Visible Marks
Yes
Service Interruption
No
Root Cause Category
Excavation Issue
Root Cause Type
Improper Excavation Practice Not Listed Above
Preparer Name
C********** P****
Preparer Title
Gas Standards Engineer
Preparer Email
C**********@m**********.com
Preparer Telephone
7122777941
Preparer Fax
7122527369
Local Contact Name
C********** P****
Local Contact Email
C**********@m**********.com
Local Contact Telephone
7122777941
Authorizer Name
N*** N*****
Authorizer Title
Vice President Gas Delivery
Authorizer Telephone
5156973256
Authorizer Email
N**********@m**********.com
Narrative
Hartco cable, inc. (third party contractor) bored into a 16-inch natural gas steel main while installing cable tv at 1400 nw 86th street in clive, iowa on august 2, 2023. The boring head punctured a four-inch by two-inch hole in the lower third of the main that was at a six-foot depth. No services were interrupted and there was no ignition or injuries. Due to the size and depth of the main, it took a significant amount of time to repair the damage and 6.771 mcf of natural gas was released to atmosphere. The nrc was initially notified (report 1375040) on august 2 and a 48-hour follow-up report was submitted (report 1375241).
Report Received Date | 2023-08-31 00:00:00 |
---|---|
Iyear | 2023.0 |
Report Number | 20230046.0 |
Supplemental Number | 38482.0 |
Report Type | Original Final |
Operator Id | 30750 PHMSA Enforcement |
Name | Midamerican Energy Company |
Operator Street Address | 401 Douglas Street Po Box 778 |
Operator City Name | Sioux City |
Operator State Abbreviation | IA |
Operator Postal Code | 51101.0 |
Time Zone | Central |
Daylight Savings Ind | Yes |
Location Street Address | 1400 Nw 86th Street |
Location City Name | Clive |
Location County Name | Polk |
Location State Abbreviation | IA |
Location Postal Code | 50325.0 |
Location Latitude | 41.60312 Google Maps OpenStreetMap |
Location Longitude | -93.73654 Google Maps OpenStreetMap |
Flow Cont Key Crit Ind | Yes |
Flow Cont Main Valve Ind | Yes |
Nrc Rpt Num | 1375040.0 NRC Report How to search |
Additional Nrc Report Numbers | 1375241.0 |
Commodity Released Type | Natural Gas |
Unintentional Release | 6771.0 |
Intentional Release | 0.0 |
Fatality Ind | No |
Fatal | 0 |
Injury Ind | No |
Injure | 0 |
Ignite Ind | No |
Num Pub Evacuated | 17.0 |
Federal | No |
Location Type | Public Property |
Incident Area Type | Underground |
Incident Area Subtype | Under Soil |
Depth Of Cover | 60.0 |
Other Underground Facilities | No |
Crossing | No |
Pipe Facility Type | Investor Owned |
System Part Involved | Main |
Installation Year | 1968.0 |
Pipe Diameter | 16.0 |
Pipe Specification | Unknown |
Pipe Manufacturer | Unknown |
Material Involved | Steel |
Steel Seam Type | Other |
Steel Seam Type Details | Unknown |
Release Type | Mechanical Puncture |
Puncture Axial | 4.0 |
Puncture Circum | 2.0 |
Class Location Type | Class 4 Location |
Est Cost Oper Paid | 0.0 |
Est Cost Prop Damage | 2000.0 |
Est Cost Emergency | 36755.0 |
Est Cost Other | 0.0 |
Gas Cost In Mcf | 2.3395 |
Est Cost Unintentional Release | 15841.0 |
Est Cost Intentional Release | 0.0 |
Prpty | 54596.0 |
Commercial Affected | 0.0 |
Industrial Affected | 0.0 |
Residences Affected | 0.0 |
Num Persons Hosp Not Ovnght | 0.0 |
Num Injured Treated By Emt | 0.0 |
Num Resident Building Affctd | 0.0 |
Num Business Building Affctd | 2.0 |
Accident Psig | 90.0 |
Normal Psig | 90.0 |
Mop Psig | 125.0 |
Mop Cfr Section | 192.619(A)(4) View CFR 49 §192 |
Maop Established Date | 1988-10-02 00:00:00 |
Accident Pressure | Pressure Did Not Exceed Maop |
Gas Odorized System Type | Injection Pump |
Gas Odorized Lvl Not Msrd Ind | Yes |
Scada In Place Ind | Yes |
Scada Operating Ind | Yes |
Scada Functional Ind | Yes |
Scada Detection Ind | No |
Scada Conf Ind | No |
Accident Identifier | Notification From Emergency Responder |
Investigation Status | Yes, specify investigation result(s): (select all that apply) |
Invest Schedule Ind | Yes |
Invest No Control Room Ind | Yes |
Invest No Controller Ind | Yes |
Employee Drug Test Ind | No |
Contractor Drug Test Ind | No |
Cause | Excavation Damage |
Cause Details | Excavation Damage By Third Party |
Ex Party Type | Excavation Damage By Third Party |
Prior Notification Ind | Yes |
One Call System Ind | Yes |
State Law Exempt Ind | No |
Notify Cga Dirt | No |
Public Row Ind | Yes |
Public Subtype | City Street |
Excavator Type | Contractor |
Excavator Equipment | Boring |
Work Performed | Cable Tv |
One Call Notified Ind | Yes |
One Call Ticket Num | 232061755.0 |
Locator Type | Contract Locator |
Visible Marks | Yes |
Service Interruption | No |
Root Cause Category | Excavation Issue |
Root Cause Type | Improper Excavation Practice Not Listed Above |
Preparer Name | C********** P**** |
Preparer Title | Gas Standards Engineer |
Preparer Email | C**********@m**********.com |
Preparer Telephone | 7122777941 |
Preparer Fax | 7122527369 |
Local Contact Name | C********** P**** |
Local Contact Email | C**********@m**********.com |
Local Contact Telephone | 7122777941 |
Authorizer Name | N*** N***** |
Authorizer Title | Vice President Gas Delivery |
Authorizer Telephone | 5156973256 |
Authorizer Email | N**********@m**********.com |
Narrative | Hartco cable, inc. (third party contractor) bored into a 16-inch natural gas steel main while installing cable tv at 1400 nw 86th street in clive, iowa on august 2, 2023. The boring head punctured a four-inch by two-inch hole in the lower third of the main that was at a six-foot depth. No services were interrupted and there was no ignition or injuries. Due to the size and depth of the main, it took a significant amount of time to repair the damage and 6.771 mcf of natural gas was released to atmosphere. The nrc was initially notified (report 1375040) on august 2 and a 48-hour follow-up report was submitted (report 1375241). |
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