GD incident on 2023-07-14 — TX

Operator
Atmos Energy Corporation - Mid-Tex
Cause
Other Outside Force Damage
Commodity
Natural Gas
Program
GD
Damage and Injuries
1 fatality 1 injury
Property damage (nominal)
$7,897
Incident datetime
2023-07-14 00:00 UTC
Report number
Location
TX, TARRANT
Narrative
On june 14, 2023, at approximately 6:12 pm, an atmos energy service tech received a phone call from dispatch informing him of a vehicle striking a meter. Upon arrival at the site at approximately 6:27 pm, the tech confirmed the address was 1025 w loop 820 n. The gas meter had been struck by a vehicle, and the fire department was present at the site when the tech arrived. The police report states: "[the vehicle] struck two metal post[s] and a natural gas pipeline. [the vehicle] came to rest on top of the natural gas pipeline. The natural gas pipeline ruptured and began leaking natural gas. [the vehicle] and the leaking natural gas caught fire." the tech requested additional operator resources. A construction crew arrived at approximately 7:03 pm. To eliminate the gas flow, the construction crew squeezed off the 6-inch poly main at approximately 8:03 pm. To restore service, the station was rebuilt in a different location, and service was restored at 2:15 pm on june 16, 2023.
Detailed record list
Report Received Date
2023-07-14 00:00:00
Iyear
2023.0
Report Number
20230035.0
Supplemental Number
39742.0
Report Type
Supplemental Final
Operator Id
Name
Atmos Energy Corporation - Mid-Tex
Operator Street Address
5430 Lbj Freeway Suite 1800
Operator City Name
Dallas
Operator State Abbreviation
TX
Operator Postal Code
75240.0
Time Zone
Central
Daylight Savings Ind
Yes
Location Street Address
1025 W Loop 820 N
Location City Name
Fort Worth
Location County Name
Tarrant
Location State Abbreviation
TX
Location Postal Code
76108.0
Location Latitude
Location Longitude
-97.47549768
Flow Cont Squeeze Off Ind
Yes
Nrc Rpt Num
Additional Nrc Report Numbers
1370268.0
Commodity Released Type
Natural Gas
Unintentional Release
88.0
Intentional Release
0.0
Fatality Ind
Yes
Num Emp Fatalities
0
Num Contr Fatalities
0
Num Er Fatalities
0
Num Worker Fatalities
0
Num Gp Fatalities
1
Fatal
1
Injury Ind
Yes
Num Emp Injuries
0
Num Contr Injuries
0
Num Er Injuries
0
Num Worker Injuries
0
Num Gp Injuries
1
Injure
1
Ignite Ind
Yes
How Extinguished
Operator/contractor
Gas Consumed By Fire In Mcf
88
Explode Ind
No
Num Pub Evacuated
0.0
Federal
No
Location Type
Utility Right-Of-Way / Easement
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance (E.g. Value Or Regulator Station, Outdoor Meter Set)
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Outside Meter/regulator Set
Installation Year
2006.0
Manufactured Year
2005.0
Customer Type
Non-Residential With Meter Capacity 1,000 Scfh Or Higher
Was Efv Installed Before Ind
No
Curb Valve Inst Before Inc Ind
No
Material Involved
Steel
Steel Seam Type
Seamless
Release Type
Mechanical Puncture
Puncture Axial
2.0
Puncture Circum
2.0
Class Location Type
Class 1 Location
Est Cost Oper Paid
18500.0
Est Cost Prop Damage
7897.0
Est Cost Emergency
5359.0
Est Cost Other
0.0
Gas Cost In Mcf
6.4084
Est Cost Unintentional Release
564.0
Est Cost Intentional Release
0.0
Prpty
32320.0
Commercial Affected
1.0
Industrial Affected
0.0
Residences Affected
0.0
Num Persons Hosp Not Ovnght
0.0
Num Injured Treated By Emt
1.0
Num Resident Building Affctd
0.0
Num Business Building Affctd
1.0
Accident Psig
29.0
Normal Psig
29.0
Mop Psig
60.0
Mop Cfr Section
192.619(A)(1)
Maop Established Date
2006-06-20 00:00:00
Accident Pressure
Pressure Did Not Exceed Maop
Gas Odorized System Type
Combination Of Odorization Types
Gas Odorized Level
5
Scada In Place Ind
No
Accident Identifier
Notification From Emergency Responder
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Other Outside Force Damage
Cause Details
Damage By Car, Truck, Or Other Motorized Vehicle/equipment Not Engaged In Excavation
Outside Force Type
Damage By Car, Truck, Or Other Motorized Vehicle/equipment Not Engaged In Excavation
Vehicle Subtype
Third Party
Driver Issued Citation Ind
Unknown
Driver In Control Ind
Unknown
Estimated Speed
Unknown
Vehicle Type
Passenger Car
Vehicle Travel From
Roadway
Vehicle Travel Distance Ft
30
Protections Installed Ind
Yes
Protection Bollards Post Ind
Yes
Preparer Name
S**** K****
Preparer Title
Field Supervisor
Preparer Email
W************@a**********.com
Preparer Telephone
469-261-2011
Local Contact Name
S**** K****
Local Contact Email
W************@a**********.com
Local Contact Telephone
469-261-2011
Authorizer Name
J*** K******
Authorizer Title
Sr. V.p. Technical Services
Authorizer Telephone
214-206-2701
Authorizer Email
J***********@a**********.com
Narrative
On june 14, 2023, at approximately 6:12 pm, an atmos energy service tech received a phone call from dispatch informing him of a vehicle striking a meter. Upon arrival at the site at approximately 6:27 pm, the tech confirmed the address was 1025 w loop 820 n. The gas meter had been struck by a vehicle, and the fire department was present at the site when the tech arrived. The police report states: "[the vehicle] struck two metal post[s] and a natural gas pipeline. [the vehicle] came to rest on top of the natural gas pipeline. The natural gas pipeline ruptured and began leaking natural gas. [the vehicle] and the leaking natural gas caught fire." the tech requested additional operator resources. A construction crew arrived at approximately 7:03 pm. To eliminate the gas flow, the construction crew squeezed off the 6-inch poly main at approximately 8:03 pm. To restore service, the station was rebuilt in a different location, and service was restored at 2:15 pm on june 16, 2023.
Report Received Date 2023-07-14 00:00:00
Iyear 2023.0
Report Number 20230035.0
Supplemental Number 39742.0
Report Type Supplemental Final
Operator Id 31348 PHMSA Enforcement
Name Atmos Energy Corporation - Mid-Tex
Operator Street Address 5430 Lbj Freeway Suite 1800
Operator City Name Dallas
Operator State Abbreviation TX
Operator Postal Code 75240.0
Time Zone Central
Daylight Savings Ind Yes
Location Street Address 1025 W Loop 820 N
Location City Name Fort Worth
Location County Name Tarrant
Location State Abbreviation TX
Location Postal Code 76108.0
Location Latitude 32.77815921 Google Maps OpenStreetMap
Location Longitude -97.47549768 Google Maps OpenStreetMap
Flow Cont Squeeze Off Ind Yes
Nrc Rpt Num 1370100.0 NRC Report How to search
Additional Nrc Report Numbers 1370268.0
Commodity Released Type Natural Gas
Unintentional Release 88.0
Intentional Release 0.0
Fatality Ind Yes
Num Emp Fatalities 0
Num Contr Fatalities 0
Num Er Fatalities 0
Num Worker Fatalities 0
Num Gp Fatalities 1
Fatal 1
Injury Ind Yes
Num Emp Injuries 0
Num Contr Injuries 0
Num Er Injuries 0
Num Worker Injuries 0
Num Gp Injuries 1
Injure 1
Ignite Ind Yes
How Extinguished Operator/contractor
Gas Consumed By Fire In Mcf 88
Explode Ind No
Num Pub Evacuated 0.0
Federal No
Location Type Utility Right-Of-Way / Easement
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance (E.g. Value Or Regulator Station, Outdoor Meter Set)
Crossing No
Pipe Facility Type Investor Owned
System Part Involved Outside Meter/regulator Set
Installation Year 2006.0
Manufactured Year 2005.0
Customer Type Non-Residential With Meter Capacity 1,000 Scfh Or Higher
Was Efv Installed Before Ind No
Curb Valve Inst Before Inc Ind No
Material Involved Steel
Steel Seam Type Seamless
Release Type Mechanical Puncture
Puncture Axial 2.0
Puncture Circum 2.0
Class Location Type Class 1 Location
Est Cost Oper Paid 18500.0
Est Cost Prop Damage 7897.0
Est Cost Emergency 5359.0
Est Cost Other 0.0
Gas Cost In Mcf 6.4084
Est Cost Unintentional Release 564.0
Est Cost Intentional Release 0.0
Prpty 32320.0
Commercial Affected 1.0
Industrial Affected 0.0
Residences Affected 0.0
Num Persons Hosp Not Ovnght 0.0
Num Injured Treated By Emt 1.0
Num Resident Building Affctd 0.0
Num Business Building Affctd 1.0
Accident Psig 29.0
Normal Psig 29.0
Mop Psig 60.0
Mop Cfr Section 192.619(A)(1) View CFR 49 §192
Maop Established Date 2006-06-20 00:00:00
Accident Pressure Pressure Did Not Exceed Maop
Gas Odorized System Type Combination Of Odorization Types
Gas Odorized Level 5
Scada In Place Ind No
Accident Identifier Notification From Emergency Responder
Investigation Status No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Other Outside Force Damage
Cause Details Damage By Car, Truck, Or Other Motorized Vehicle/equipment Not Engaged In Excavation
Outside Force Type Damage By Car, Truck, Or Other Motorized Vehicle/equipment Not Engaged In Excavation
Vehicle Subtype Third Party
Driver Issued Citation Ind Unknown
Driver In Control Ind Unknown
Estimated Speed Unknown
Vehicle Type Passenger Car
Vehicle Travel From Roadway
Vehicle Travel Distance Ft 30
Protections Installed Ind Yes
Protection Bollards Post Ind Yes
Preparer Name S**** K****
Preparer Title Field Supervisor
Preparer Email W************@a**********.com
Preparer Telephone 469-261-2011
Local Contact Name S**** K****
Local Contact Email W************@a**********.com
Local Contact Telephone 469-261-2011
Authorizer Name J*** K******
Authorizer Title Sr. V.p. Technical Services
Authorizer Telephone 214-206-2701
Authorizer Email J***********@a**********.com
Narrative On june 14, 2023, at approximately 6:12 pm, an atmos energy service tech received a phone call from dispatch informing him of a vehicle striking a meter. Upon arrival at the site at approximately 6:27 pm, the tech confirmed the address was 1025 w loop 820 n. The gas meter had been struck by a vehicle, and the fire department was present at the site when the tech arrived. The police report states: "[the vehicle] struck two metal post[s] and a natural gas pipeline. [the vehicle] came to rest on top of the natural gas pipeline. The natural gas pipeline ruptured and began leaking natural gas. [the vehicle] and the leaking natural gas caught fire." the tech requested additional operator resources. A construction crew arrived at approximately 7:03 pm. To eliminate the gas flow, the construction crew squeezed off the 6-inch poly main at approximately 8:03 pm. To restore service, the station was rebuilt in a different location, and service was restored at 2:15 pm on june 16, 2023.

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