GD incident on 2023-03-22 — TX

Operator
Atmos Energy Corporation - Mid-Tex
Cause
Locating Issue
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$113,589
Incident datetime
2023-03-22 00:00 UTC
Report number
Location
TX, BRAZOS
Narrative
On february 20, 2023, at 4pm, a third-party contractor was directional drilling at 2101 texas avenue / richards st, college station and bored into atmos energy's 2-inch poly main at a depth of 15 feet. The technician arrived on the scene and confirmed the leak at 4:30pm. College station fire department evacuated 8 structures and gas was subsequently turned off to 10 houses and 1 commercial entity on richards st. Upon arrival on the scene, atmos energy's crew worked continuously to conduct the necessary excavation to locate and repair the damaged line. On february 21, 2023 at 2:30pm, a squeeze tool was installed on the 2-inch poly pipe to stop gas flow where the pipe was damaged. At 5pm, the 2-inch main was replaced and gas service was restored to the 11 customers. Regarding part a question 22 - this number refers to the 8 structures that were evacuated and not people. The total of people that were evacuated is not known.
Detailed record list
Report Received Date
2023-03-22 00:00:00
Iyear
2023.0
Report Number
20230012.0
Supplemental Number
37877.0
Report Type
Supplemental Final
Operator Id
Name
Atmos Energy Corporation - Mid-Tex
Operator Street Address
5430 Lbj Freeway Suite 1800
Operator City Name
Dallas
Operator State Abbreviation
TX
Operator Postal Code
75240.0
Time Zone
Central
Daylight Savings Ind
No
Location Street Address
2101 Texas Ave
Location City Name
College Station
Location County Name
Brazos
Location State Abbreviation
TX
Location Postal Code
77840.0
Location Latitude
Location Longitude
-96.31471839
Flow Cont Squeeze Off Ind
Yes
Nrc Rpt Num
Additional Nrc Report Numbers
1360697.0
Commodity Released Type
Natural Gas
Unintentional Release
1058.34
Intentional Release
0.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Num Pub Evacuated
8.0
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Federal
No
Location Type
Utility Right-Of-Way / Easement
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
180.0
Other Underground Facilities
Yes
Crossing
Yes
Road Crossing Ind
Yes
Road Type
Cased
Pipe Facility Type
Investor Owned
System Part Involved
Main
Installation Year
2004.0
Pipe Diameter
2.0
Pipe Specification
Unknown
Pipe Manufacturer
Performance Pipe
Material Involved
Plastic
Plastic Type
Polyethylene (Pe)
Plastic Sdr
11.5
Material Pe Pipe Code
2406
Release Type
Mechanical Puncture
Puncture Axial
2.0
Puncture Circum
2.0
Class Location Type
Class 3 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
113589.0
Est Cost Emergency
14330.0
Est Cost Other
0.0
Gas Cost In Mcf
7.7224
Est Cost Unintentional Release
8173.0
Est Cost Intentional Release
0.0
Prpty
136092.0
Commercial Affected
1.0
Industrial Affected
0.0
Residences Affected
10.0
Num Persons Hosp Not Ovnght
0.0
Num Injured Treated By Emt
0.0
Num Resident Building Affctd
17.0
Num Business Building Affctd
1.0
Accident Psig
34.0
Normal Psig
34.0
Mop Psig
50.0
Mop Cfr Section
192.619(A)(2)
Maop Established Date
2004-10-14 00:00:00
Accident Pressure
Pressure Did Not Exceed Maop
Gas Odorized System Type
Odorized By Others
Gas Odorized Lvl Not Msrd Ind
Yes
Scada In Place Ind
No
Accident Identifier
Notification From Third Party That Caused The Incident
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
Yes
One Call System Ind
Yes
State Law Exempt Ind
No
Notify Cga Dirt
No
Public Row Ind
Yes
Public Subtype
State Highway
Excavator Type
Contractor
Excavator Equipment
Directional Drilling
Work Performed
Telecommunications
One Call Notified Ind
Yes
One Call Ticket Num
2354567778.0
One Call Center Name
Texas 811
Locator Type
Contract Locator
Visible Marks
Yes
Service Interruption
Yes
Service Interruption Hours
24.0
Root Cause Category
Locating Issue
Root Cause Type
Facility Not Marked Due To Incomplete Marks At Damage Location
Preparer Name
L*** C*******
Preparer Title
Compliance Supervisor
Preparer Email
L************@a**********.com
Preparer Telephone
979-324-8823
Authorizer Name
J*** K******
Authorizer Title
Sr Vp Technical And Operating Services
Authorizer Telephone
214-206-2701
Authorizer Email
J**************@a**********.com
Narrative
On february 20, 2023, at 4pm, a third-party contractor was directional drilling at 2101 texas avenue / richards st, college station and bored into atmos energy's 2-inch poly main at a depth of 15 feet. The technician arrived on the scene and confirmed the leak at 4:30pm. College station fire department evacuated 8 structures and gas was subsequently turned off to 10 houses and 1 commercial entity on richards st. Upon arrival on the scene, atmos energy's crew worked continuously to conduct the necessary excavation to locate and repair the damaged line. On february 21, 2023 at 2:30pm, a squeeze tool was installed on the 2-inch poly pipe to stop gas flow where the pipe was damaged. At 5pm, the 2-inch main was replaced and gas service was restored to the 11 customers. Regarding part a question 22 - this number refers to the 8 structures that were evacuated and not people. The total of people that were evacuated is not known.
Report Received Date 2023-03-22 00:00:00
Iyear 2023.0
Report Number 20230012.0
Supplemental Number 37877.0
Report Type Supplemental Final
Operator Id 31348 PHMSA Enforcement
Name Atmos Energy Corporation - Mid-Tex
Operator Street Address 5430 Lbj Freeway Suite 1800
Operator City Name Dallas
Operator State Abbreviation TX
Operator Postal Code 75240.0
Time Zone Central
Daylight Savings Ind No
Location Street Address 2101 Texas Ave
Location City Name College Station
Location County Name Brazos
Location State Abbreviation TX
Location Postal Code 77840.0
Location Latitude 30.61195641 Google Maps OpenStreetMap
Location Longitude -96.31471839 Google Maps OpenStreetMap
Flow Cont Squeeze Off Ind Yes
Nrc Rpt Num 1360544.0 NRC Report How to search
Additional Nrc Report Numbers 1360697.0
Commodity Released Type Natural Gas
Unintentional Release 1058.34
Intentional Release 0.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind No
Num Pub Evacuated 8.0
Communication State Fed Ind Yes
Party Initiated Communication Operator
Federal No
Location Type Utility Right-Of-Way / Easement
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 180.0
Other Underground Facilities Yes
Crossing Yes
Road Crossing Ind Yes
Road Type Cased
Pipe Facility Type Investor Owned
System Part Involved Main
Installation Year 2004.0
Pipe Diameter 2.0
Pipe Specification Unknown
Pipe Manufacturer Performance Pipe
Material Involved Plastic
Plastic Type Polyethylene (Pe)
Plastic Sdr 11.5
Material Pe Pipe Code 2406
Release Type Mechanical Puncture
Puncture Axial 2.0
Puncture Circum 2.0
Class Location Type Class 3 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 113589.0
Est Cost Emergency 14330.0
Est Cost Other 0.0
Gas Cost In Mcf 7.7224
Est Cost Unintentional Release 8173.0
Est Cost Intentional Release 0.0
Prpty 136092.0
Commercial Affected 1.0
Industrial Affected 0.0
Residences Affected 10.0
Num Persons Hosp Not Ovnght 0.0
Num Injured Treated By Emt 0.0
Num Resident Building Affctd 17.0
Num Business Building Affctd 1.0
Accident Psig 34.0
Normal Psig 34.0
Mop Psig 50.0
Mop Cfr Section 192.619(A)(2) View CFR 49 §192
Maop Established Date 2004-10-14 00:00:00
Accident Pressure Pressure Did Not Exceed Maop
Gas Odorized System Type Odorized By Others
Gas Odorized Lvl Not Msrd Ind Yes
Scada In Place Ind No
Accident Identifier Notification From Third Party That Caused The Incident
Investigation Status No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind Yes
One Call System Ind Yes
State Law Exempt Ind No
Notify Cga Dirt No
Public Row Ind Yes
Public Subtype State Highway
Excavator Type Contractor
Excavator Equipment Directional Drilling
Work Performed Telecommunications
One Call Notified Ind Yes
One Call Ticket Num 2354567778.0
One Call Center Name Texas 811
Locator Type Contract Locator
Visible Marks Yes
Service Interruption Yes
Service Interruption Hours 24.0
Root Cause Category Locating Issue
Root Cause Type Facility Not Marked Due To Incomplete Marks At Damage Location
Preparer Name L*** C*******
Preparer Title Compliance Supervisor
Preparer Email L************@a**********.com
Preparer Telephone 979-324-8823
Authorizer Name J*** K******
Authorizer Title Sr Vp Technical And Operating Services
Authorizer Telephone 214-206-2701
Authorizer Email J**************@a**********.com
Narrative On february 20, 2023, at 4pm, a third-party contractor was directional drilling at 2101 texas avenue / richards st, college station and bored into atmos energy's 2-inch poly main at a depth of 15 feet. The technician arrived on the scene and confirmed the leak at 4:30pm. College station fire department evacuated 8 structures and gas was subsequently turned off to 10 houses and 1 commercial entity on richards st. Upon arrival on the scene, atmos energy's crew worked continuously to conduct the necessary excavation to locate and repair the damaged line. On february 21, 2023 at 2:30pm, a squeeze tool was installed on the 2-inch poly pipe to stop gas flow where the pipe was damaged. At 5pm, the 2-inch main was replaced and gas service was restored to the 11 customers. Regarding part a question 22 - this number refers to the 8 structures that were evacuated and not people. The total of people that were evacuated is not known.

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