GD incident on 2023-02-10 — ND

Operator
Montana - Dakota Utilities Co
Cause
Other Outside Force Damage
Commodity
Natural Gas
Program
GD
Damage and Injuries
1 fatality 1 injury
Property damage (nominal)
$270
Incident datetime
2023-02-10 00:00 UTC
Report number
Location
ND, MORTON
Narrative
On january 18, 2023, mdu responded to a structure fire/explosion at 4616 cortez circle in mandan, nd. An unintentional release and ignition of natural gas occurred. Mdu personnel secured the release by squeezing off the service line. On january 19, 2023, the mandan fire department and atf conducted an investigation at 4616 cortez circle in mandan, nd, with representatives from mdu and the nd psc present. During examination of the structure's interior, approximately ten (10) feet downstream of the gas meter, the non-jurisdictional gas piping was found to be separated at a connection point. A natural gas range and natural gas furnace were the only two fuel fired appliances located in the structure. The connections and piping to the range and furnace appeared to be intact. The heat source or cause of ignition was inconclusive. Following the investigation on january 19, 2023, mdu made attempts to coordinate the investigation of jurisdictional facilities with all parties. After failed attempts to coordinate, the company provided notification to all parties that an investigation would commence on august 15, 2023. Mdu and the north dakota gas pipeline safety program manager/inspector conducted an investigation of jurisdictional facilities at 4616 cortez circle in mandan, nd. A pressure test was performed on the service line. The pressure test passed, holding at system pressure. Above ground piping was intact up to the riser valve. There was a cracked nipple between the riser valve and the regulator. The analysis concludes that the nipple damage was due to an unknown outside force. It is unknown when the nipple damage occurred. Mdu was allowed to investigate jurisdictional facilities only. October 11, 2023 - corrected time in field a4. Updated from 12:26 to 11:57.
Detailed record list
Report Received Date
2023-02-10 00:00:00
Iyear
2023.0
Report Number
20230007.0
Supplemental Number
38650.0
Report Type
Supplemental Final
Operator Id
Name
Montana - Dakota Utilities Co
Operator Street Address
400 North Fourth Street
Operator City Name
Bismarck
Operator State Abbreviation
ND
Operator Postal Code
58501.0
Time Zone
Central
Daylight Savings Ind
No
Location Street Address
4616 Cortez Circle
Location City Name
Mandan
Location County Name
Morton
Location State Abbreviation
ND
Location Postal Code
58554.0
Location Latitude
Location Longitude
-100.9446269
Flow Cont Squeeze Off Ind
Yes
Nrc Rpt Num
Additional Nrc Report Numbers
1358143.0
Commodity Released Type
Natural Gas
Unintentional Release
8.21
Intentional Release
0.0
Fatality Ind
Yes
Num Emp Fatalities
0
Num Contr Fatalities
0
Num Er Fatalities
0
Num Worker Fatalities
0
Num Gp Fatalities
1
Fatal
1
Injury Ind
Yes
Num Emp Injuries
0
Num Contr Injuries
0
Num Er Injuries
0
Num Worker Injuries
0
Num Gp Injuries
1
Injure
1
Ignite Ind
Yes
How Extinguished
Local/state/federal Emergency Responder
Gas Consumed By Fire In Mcf
8.21
Explode Ind
Yes
Num Pub Evacuated
2.0
Federal
No
Location Type
Private Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance (E.g. Value Or Regulator Station, Outdoor Meter Set)
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Outside Meter/regulator Set
Installation Year
2017.0
Customer Type
Single Family Residential
Was Efv Installed Before Ind
No
Curb Valve Inst Before Inc Ind
No
Material Involved
Steel
Steel Seam Type
Seamless
Wt Steel
0.113
Release Type
Leak
Leak Type
Crack
Class Location Type
Class 3 Location
Est Cost Oper Paid
105000.0
Est Cost Prop Damage
270.0
Est Cost Emergency
1100.0
Est Cost Other
0.0
Gas Cost In Mcf
6.74
Est Cost Unintentional Release
55.0
Est Cost Intentional Release
0.0
Prpty
106425.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
1.0
Num Persons Hosp Not Ovnght
0.0
Num Injured Treated By Emt
0.0
Num Resident Building Affctd
2.0
Num Business Building Affctd
0.0
Accident Psig
30.0
Normal Psig
30.0
Mop Psig
60.0
Mop Cfr Section
192.619(A)(2)
Maop Established Date
1983-09-30 00:00:00
Accident Pressure
Pressure Did Not Exceed Maop
Gas Odorized System Type
Odorized By Others
Gas Odorized Level
15
Scada In Place Ind
No
Accident Identifier
Notification From Emergency Responder
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Other Outside Force Damage
Cause Details
Other Outside Force Damage
Outside Force Type
Other Outside Force Damage
Osf Other Details
There Was A Cracked Nipple Between The Riser Valve And The Regulator. The Analysis Concludes That The Nipple Damage Was Due To An Unknown Outside Force. It Is Unknown When The Nipple Damage Occurred.
Preparer Name
S******* C*******
Preparer Title
Manager Policy And Procedure
Preparer Email
S****************@m**.com
Preparer Telephone
208-509-2140
Local Contact Name
S******* C*******
Local Contact Email
S****************@m**.com
Local Contact Telephone
208-509-2140
Authorizer Name
J*** S******
Authorizer Title
Director Policy And Procedure
Authorizer Telephone
701-222-7773
Authorizer Email
J***********@m**.com
Narrative
On january 18, 2023, mdu responded to a structure fire/explosion at 4616 cortez circle in mandan, nd. An unintentional release and ignition of natural gas occurred. Mdu personnel secured the release by squeezing off the service line. On january 19, 2023, the mandan fire department and atf conducted an investigation at 4616 cortez circle in mandan, nd, with representatives from mdu and the nd psc present. During examination of the structure's interior, approximately ten (10) feet downstream of the gas meter, the non-jurisdictional gas piping was found to be separated at a connection point. A natural gas range and natural gas furnace were the only two fuel fired appliances located in the structure. The connections and piping to the range and furnace appeared to be intact. The heat source or cause of ignition was inconclusive. Following the investigation on january 19, 2023, mdu made attempts to coordinate the investigation of jurisdictional facilities with all parties. After failed attempts to coordinate, the company provided notification to all parties that an investigation would commence on august 15, 2023. Mdu and the north dakota gas pipeline safety program manager/inspector conducted an investigation of jurisdictional facilities at 4616 cortez circle in mandan, nd. A pressure test was performed on the service line. The pressure test passed, holding at system pressure. Above ground piping was intact up to the riser valve. There was a cracked nipple between the riser valve and the regulator. The analysis concludes that the nipple damage was due to an unknown outside force. It is unknown when the nipple damage occurred. Mdu was allowed to investigate jurisdictional facilities only. October 11, 2023 - corrected time in field a4. Updated from 12:26 to 11:57.
Report Received Date 2023-02-10 00:00:00
Iyear 2023.0
Report Number 20230007.0
Supplemental Number 38650.0
Report Type Supplemental Final
Operator Id 12684 PHMSA Enforcement
Name Montana - Dakota Utilities Co
Operator Street Address 400 North Fourth Street
Operator City Name Bismarck
Operator State Abbreviation ND
Operator Postal Code 58501.0
Time Zone Central
Daylight Savings Ind No
Location Street Address 4616 Cortez Circle
Location City Name Mandan
Location County Name Morton
Location State Abbreviation ND
Location Postal Code 58554.0
Location Latitude 46.86667512 Google Maps OpenStreetMap
Location Longitude -100.9446269 Google Maps OpenStreetMap
Flow Cont Squeeze Off Ind Yes
Nrc Rpt Num 1357989.0 NRC Report How to search
Additional Nrc Report Numbers 1358143.0
Commodity Released Type Natural Gas
Unintentional Release 8.21
Intentional Release 0.0
Fatality Ind Yes
Num Emp Fatalities 0
Num Contr Fatalities 0
Num Er Fatalities 0
Num Worker Fatalities 0
Num Gp Fatalities 1
Fatal 1
Injury Ind Yes
Num Emp Injuries 0
Num Contr Injuries 0
Num Er Injuries 0
Num Worker Injuries 0
Num Gp Injuries 1
Injure 1
Ignite Ind Yes
How Extinguished Local/state/federal Emergency Responder
Gas Consumed By Fire In Mcf 8.21
Explode Ind Yes
Num Pub Evacuated 2.0
Federal No
Location Type Private Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance (E.g. Value Or Regulator Station, Outdoor Meter Set)
Crossing No
Pipe Facility Type Investor Owned
System Part Involved Outside Meter/regulator Set
Installation Year 2017.0
Customer Type Single Family Residential
Was Efv Installed Before Ind No
Curb Valve Inst Before Inc Ind No
Material Involved Steel
Steel Seam Type Seamless
Wt Steel 0.113
Release Type Leak
Leak Type Crack
Class Location Type Class 3 Location
Est Cost Oper Paid 105000.0
Est Cost Prop Damage 270.0
Est Cost Emergency 1100.0
Est Cost Other 0.0
Gas Cost In Mcf 6.74
Est Cost Unintentional Release 55.0
Est Cost Intentional Release 0.0
Prpty 106425.0
Commercial Affected 0.0
Industrial Affected 0.0
Residences Affected 1.0
Num Persons Hosp Not Ovnght 0.0
Num Injured Treated By Emt 0.0
Num Resident Building Affctd 2.0
Num Business Building Affctd 0.0
Accident Psig 30.0
Normal Psig 30.0
Mop Psig 60.0
Mop Cfr Section 192.619(A)(2) View CFR 49 §192
Maop Established Date 1983-09-30 00:00:00
Accident Pressure Pressure Did Not Exceed Maop
Gas Odorized System Type Odorized By Others
Gas Odorized Level 15
Scada In Place Ind No
Accident Identifier Notification From Emergency Responder
Investigation Status No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Other Outside Force Damage
Cause Details Other Outside Force Damage
Outside Force Type Other Outside Force Damage
Osf Other Details There Was A Cracked Nipple Between The Riser Valve And The Regulator. The Analysis Concludes That The Nipple Damage Was Due To An Unknown Outside Force. It Is Unknown When The Nipple Damage Occurred.
Preparer Name S******* C*******
Preparer Title Manager Policy And Procedure
Preparer Email S****************@m**.com
Preparer Telephone 208-509-2140
Local Contact Name S******* C*******
Local Contact Email S****************@m**.com
Local Contact Telephone 208-509-2140
Authorizer Name J*** S******
Authorizer Title Director Policy And Procedure
Authorizer Telephone 701-222-7773
Authorizer Email J***********@m**.com
Narrative On january 18, 2023, mdu responded to a structure fire/explosion at 4616 cortez circle in mandan, nd. An unintentional release and ignition of natural gas occurred. Mdu personnel secured the release by squeezing off the service line. On january 19, 2023, the mandan fire department and atf conducted an investigation at 4616 cortez circle in mandan, nd, with representatives from mdu and the nd psc present. During examination of the structure's interior, approximately ten (10) feet downstream of the gas meter, the non-jurisdictional gas piping was found to be separated at a connection point. A natural gas range and natural gas furnace were the only two fuel fired appliances located in the structure. The connections and piping to the range and furnace appeared to be intact. The heat source or cause of ignition was inconclusive. Following the investigation on january 19, 2023, mdu made attempts to coordinate the investigation of jurisdictional facilities with all parties. After failed attempts to coordinate, the company provided notification to all parties that an investigation would commence on august 15, 2023. Mdu and the north dakota gas pipeline safety program manager/inspector conducted an investigation of jurisdictional facilities at 4616 cortez circle in mandan, nd. A pressure test was performed on the service line. The pressure test passed, holding at system pressure. Above ground piping was intact up to the riser valve. There was a cracked nipple between the riser valve and the regulator. The analysis concludes that the nipple damage was due to an unknown outside force. It is unknown when the nipple damage occurred. Mdu was allowed to investigate jurisdictional facilities only. October 11, 2023 - corrected time in field a4. Updated from 12:26 to 11:57.

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