Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2022-12-25 — TX
Operator
Mccain Pipeline Company
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$100,000
Incident datetime
2022-12-25 17:20
Report number
Location
TX
Narrative
Valve for draining water bottoms from floating roof breakout tank failed at bonnet gasket.
Detailed record list
Report Received Date
2022-12-26 00:00:00
Iyear
2022
Report Number
20220292
Supplemental Number
39897
Report Type
Supplemental Final
Operator Id
32174
Name
Mccain Pipeline Company
Operator Street Address
4635 Southwest Freeway, Suite 910
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77027
Local Datetime
2022-12-25 17:20:00
Time Zone
Central
Daylight Savings Ind
No
Location Latitude
32.48391
Location Longitude
-88.55891
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Other
Commodity Details
Jet A
Unintentional Release Bbls
569.36
Recovered Bbls
383.33
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2022-12-25 17:20:00
System Part Involved
Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
No
Shutdown Explain
Pipeline Was Not Transferring Fuel At Time Of Breakout Tank Failure.
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Initial Responder Com Datetime
2022-12-25 17:41:00
On Site Datetime
2022-12-25 19:30:00
Confirmed Discovery Datetime
2022-12-25 17:20:00
Nrc Rpt Datetime
2022-12-25 17:45:00
Nrc Rpt Num
1355931
Additional Nrc Report Numbers
1358654
Ignite Ind
No
Notify Qualified Indiv Ind
Yes
Qualified Indiv Notif Datetime
2022-12-25 17:30:00
Oil Spill Removal Org Ind
Yes
Osro Activated Datetime
2022-12-25 17:41:00
Osro Arrived On Site Dt
12/25/2022 19:30
Num Pub Evacuated
0
Pipe Fac Name
Mccain Pipeline Company
Segment Name
Terminal Facility
Onshore State Abbreviation
Ms
Onshore Postal Code
39335
Onshore City Name
Not Within A Municipality
Onshore County Name
Lauderdale
Designated Location
Survey Station No.
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Tank/vessel
Tank Vessel Subtype
Other
Tank Vessel Details
Valve
Tank Type
Atmospheric
Safe Fill Level
41
Safe Fill Level Exceeded Ind
No
Api Std Out Of Service Year
2020
Api Std In Service Year
2015
Installation Year
Unknown
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
Yes
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
98500
Est Cost Prop Damage
100000
Est Cost Emergency
150000
Est Cost Environmental
35000
Est Cost Other
0
Prpty
383500
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
15
Mop Psig
15
Mop Cfr Section
Subpart E Pressure Test �195.406(A)(3)
Maop Established Date
2022-12-25 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Other Equipment Failure
Eq Failure Type
Other Equipment Failure
Failure Details
Bonnet Gasket Failure On Floating Roof Breakout Tank Water Bottom Draw Off Valve.
Eq Additional Other Ind
Yes
Eq Additional Other Details
Bonnet Gasket Failure On Floating Roof Breakout Tank Water Bottom Draw Off Valve
Preparer Name
W****** P****
Preparer Email
W*****@b*******.com
Preparer Telephone
4074214660
Prepared Date
2024-08-14 00:00:00
Local Contact Name
J***** C****
Local Contact Email
M****@a**.com
Local Contact Telephone
601.632.1118
Authorizer Name
M*** R****
Authorizer Telephone
713.829.0065
Authorizer Title
President Pipeline And Terminal Management Inc.
Authorizer Email
M****@p***.us
Narrative
Valve for draining water bottoms from floating roof breakout tank failed at bonnet gasket.
| Report Received Date | 2022-12-26 00:00:00 |
|---|---|
| Iyear | 2022 |
| Report Number | 20220292 |
| Supplemental Number | 39897 |
| Report Type | Supplemental Final |
| Operator Id | 32174 PHMSA Enforcement |
| Name | Mccain Pipeline Company |
| Operator Street Address | 4635 Southwest Freeway, Suite 910 |
| Operator City Name | Houston |
| Operator State Abbreviation | TX |
| Operator Postal Code | 77027 |
| Local Datetime | 2022-12-25 17:20:00 |
| Time Zone | Central |
| Daylight Savings Ind | No |
| Location Latitude | 32.48391 Google Maps OpenStreetMap |
| Location Longitude | -88.55891 Google Maps OpenStreetMap |
| Commodity Released Type | Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions |
| Commodity Subtype | Other |
| Commodity Details | Jet A |
| Unintentional Release Bbls | 569.36 |
| Recovered Bbls | 383.33 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Accident Identifier | Local Operating Personnel, Including Contractors |
| Operator Type | Operator Employee |
| Incident Identified Datetime | 2022-12-25 17:20:00 |
| System Part Involved | Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances |
| On Off Shore | Onshore |
| Status When Identified | Normal Operation, Includes Pauses Between Batches And During Maintenance |
| Shutdown Due Accident Ind | No |
| Shutdown Explain | Pipeline Was Not Transferring Fuel At Time Of Breakout Tank Failure. |
| Communication State Fed Ind | Yes |
| Party Initiated Communication | Operator |
| Initial Responder Com Datetime | 2022-12-25 17:41:00 |
| On Site Datetime | 2022-12-25 19:30:00 |
| Confirmed Discovery Datetime | 2022-12-25 17:20:00 |
| Nrc Rpt Datetime | 2022-12-25 17:45:00 |
| Nrc Rpt Num | 1355931 NRC Report How to search |
| Additional Nrc Report Numbers | 1358654 |
| Ignite Ind | No |
| Notify Qualified Indiv Ind | Yes |
| Qualified Indiv Notif Datetime | 2022-12-25 17:30:00 |
| Oil Spill Removal Org Ind | Yes |
| Osro Activated Datetime | 2022-12-25 17:41:00 |
| Osro Arrived On Site Dt | 12/25/2022 19:30 |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Mccain Pipeline Company |
| Segment Name | Terminal Facility |
| Onshore State Abbreviation | Ms |
| Onshore Postal Code | 39335 |
| Onshore City Name | Not Within A Municipality |
| Onshore County Name | Lauderdale |
| Designated Location | Survey Station No. |
| Designated Name | 0 |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Tank, Including Attached Appurtenances |
| Crossing | No |
| Pipe Facility Type | Intrastate |
| Item Involved | Tank/vessel |
| Tank Vessel Subtype | Other |
| Tank Vessel Details | Valve |
| Tank Type | Atmospheric |
| Safe Fill Level | 41 |
| Safe Fill Level Exceeded Ind | No |
| Api Std Out Of Service Year | 2020 |
| Api Std In Service Year | 2015 |
| Installation Year | Unknown |
| Manufactured Year | Unknown |
| Material Involved | Carbon Steel |
| Release Type | Leak |
| Leak Type | Seal Or Packing |
| Wildlife Impact Ind | No |
| Soil Contamination | Yes |
| Long Term Assessment | Yes |
| Remediation Ind | Yes |
| Soil Remed Ind | Yes |
| Water Contam Ind | No |
| Could Be Hca | No |
| Commodity Reached Hca | No |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 98500 |
| Est Cost Prop Damage | 100000 |
| Est Cost Emergency | 150000 |
| Est Cost Environmental | 35000 |
| Est Cost Other | 0 |
| Prpty | 383500 |
| Num Persons Hosp Not Ovnght | 0 |
| Num Injured Treated By Emt | 0 |
| Num Resident Building Affctd | 0 |
| Num Business Building Affctd | 0 |
| Accident Psig | 15 |
| Mop Psig | 15 |
| Mop Cfr Section | Subpart E Pressure Test �195.406(A)(3) View CFR 49 §192 |
| Maop Established Date | 2022-12-25 00:00:00 |
| Maop Reversal Flow Ind | No |
| Accident Pressure | Pressure Did Not Exceed Mop |
| Pressure Restriction Ind | No |
| Pipeline Function | < 20% Smys Regulated Transmission |
| Scada In Place Ind | No |
| Cpm In Place Ind | No |
| Investigation Status | No, the facility was not monitored by a controller(s) at the time of the accident |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Equipment Failure |
| Cause Details | Other Equipment Failure |
| Eq Failure Type | Other Equipment Failure |
| Failure Details | Bonnet Gasket Failure On Floating Roof Breakout Tank Water Bottom Draw Off Valve. |
| Eq Additional Other Ind | Yes |
| Eq Additional Other Details | Bonnet Gasket Failure On Floating Roof Breakout Tank Water Bottom Draw Off Valve |
| Preparer Name | W****** P**** |
| Preparer Email | W*****@b*******.com |
| Preparer Telephone | 4074214660 |
| Prepared Date | 2024-08-14 00:00:00 |
| Local Contact Name | J***** C**** |
| Local Contact Email | M****@a**.com |
| Local Contact Telephone | 601.632.1118 |
| Authorizer Name | M*** R**** |
| Authorizer Telephone | 713.829.0065 |
| Authorizer Title | President Pipeline And Terminal Management Inc. |
| Authorizer Email | M****@p***.us |
| Narrative | Valve for draining water bottoms from floating roof breakout tank failed at bonnet gasket. |
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