HL incident on 2022-11-23 — TX

Operator
Phillips 66 Pipeline Llc
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$100
Incident datetime
2022-11-23 12:00
Report number
Location
TX
Narrative
While inspecting valve site contractor identified that a small weep was coming from the valve stem. Contractor contacted p66 employee and upon arrival and unsuccessful tightening of packing the control center was notified to shut down the pipeline and isolated. Repairs were made to packing and weep was stopped. Line started back up that same day. Valve has since been replaced. 1/25/2023--per the accident team recommendations were to update g-6 to reflect the block valve and the sub-cause to reflect the stem packing was leaking.
Detailed record list
Report Received Date
2022-12-22 00:00:00
Iyear
2022
Report Number
20220291
Supplemental Number
37627
Report Type
Supplemental Final
Operator Id
Name
Phillips 66 Pipeline Llc
Operator Street Address
2331 Citywest Blvd
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77042
Local Datetime
2022-11-23 12:00:00
Time Zone
Central
Daylight Savings Ind
No
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
0.54
Recovered Bbls
0.54
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2022-11-23 12:00:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2022-11-23 13:00:00
Restart Datetime
2022-11-23 13:30:00
Communication State Fed Ind
No
On Site Datetime
2022-11-23 13:00:00
Confirmed Discovery Datetime
2022-11-23 13:00:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Upstream Action Taken
Valve Closure
Upstream Valve Close Datetime
2022-11-23 13:30:00
Upstream Valve Type Ind
Remotely Controlled
Downstream Action Taken
Valve Closure
Downstream Vlv Close Datetime
2022-11-23 13:45:00
Downstream Valve Type Ind
Remotely Controlled
Notify Qualified Indiv Ind
No
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Borger Denver Pipeline
Segment Name
Bd-01
Onshore State Abbreviation
Ok
Onshore Postal Code
73933
Onshore City Name
Not Within A Municipality
Onshore County Name
Cimarron
Designated Location
Milepost
Designated Name
113.25
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Mainline
Valve Mainline Type
Gate
Valve Manufacturer
Bd-113.25-M
Installation Year
1971
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
50
Est Cost Prop Damage
100
Est Cost Emergency
0
Est Cost Environmental
1500
Est Cost Other
0
Prpty
1650
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
594
Mop Psig
1305
Mop Cfr Section
Internal Design Pressure �195.406(A)(1)
Maop Established Date
1971-01-01 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
147840
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The leak was minimal over time where scada or cpm detected the packing leak
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Block Valve Ind
Yes
Eq Additional Other Ind
Yes
Eq Additional Other Details
Valve Stem Packing
Preparer Name
T*** F****
Preparer Title
Director Dot Compliance
Preparer Email
T***********@p**.com
Preparer Telephone
832-765-1632
Prepared Date
2023-01-25 00:00:00
Local Contact Name
S**** T*******
Local Contact Email
S***************@p**.com
Local Contact Telephone
303-376-4391
Authorizer Name
T*** F****
Authorizer Telephone
832-765-1632
Authorizer Title
Director Dot Compliance
Authorizer Email
T***********@p**.com
Narrative
While inspecting valve site contractor identified that a small weep was coming from the valve stem. Contractor contacted p66 employee and upon arrival and unsuccessful tightening of packing the control center was notified to shut down the pipeline and isolated. Repairs were made to packing and weep was stopped. Line started back up that same day. Valve has since been replaced. 1/25/2023--per the accident team recommendations were to update g-6 to reflect the block valve and the sub-cause to reflect the stem packing was leaking.
Report Received Date 2022-12-22 00:00:00
Iyear 2022
Report Number 20220291
Supplemental Number 37627
Report Type Supplemental Final
Operator Id 31684 PHMSA Enforcement
Name Phillips 66 Pipeline Llc
Operator Street Address 2331 Citywest Blvd
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77042
Local Datetime 2022-11-23 12:00:00
Time Zone Central
Daylight Savings Ind No
Location Latitude 36.90538394 Google Maps OpenStreetMap
Location Longitude -102.587936 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 0.54
Recovered Bbls 0.54
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2022-11-23 12:00:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind Yes
Shutdown Datetime 2022-11-23 13:00:00
Restart Datetime 2022-11-23 13:30:00
Communication State Fed Ind No
On Site Datetime 2022-11-23 13:00:00
Confirmed Discovery Datetime 2022-11-23 13:00:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Upstream Action Taken Valve Closure
Upstream Valve Close Datetime 2022-11-23 13:30:00
Upstream Valve Type Ind Remotely Controlled
Downstream Action Taken Valve Closure
Downstream Vlv Close Datetime 2022-11-23 13:45:00
Downstream Valve Type Ind Remotely Controlled
Notify Qualified Indiv Ind No
Oil Spill Removal Org Ind No
Num Pub Evacuated 0
Pipe Fac Name Borger Denver Pipeline
Segment Name Bd-01
Onshore State Abbreviation Ok
Onshore Postal Code 73933
Onshore City Name Not Within A Municipality
Onshore County Name Cimarron
Designated Location Milepost
Designated Name 113.25
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Mainline
Valve Mainline Type Gate
Valve Manufacturer Bd-113.25-M
Installation Year 1971
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 50
Est Cost Prop Damage 100
Est Cost Emergency 0
Est Cost Environmental 1500
Est Cost Other 0
Prpty 1650
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 594
Mop Psig 1305
Mop Cfr Section Internal Design Pressure �195.406(A)(1) View CFR 49 §192
Maop Established Date 1971-01-01 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 147840
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The leak was minimal over time where scada or cpm detected the packing leak
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Malfunction Of Control/relief Equipment
Eq Failure Type Malfunction Of Control/relief Equipment
Block Valve Ind Yes
Eq Additional Other Ind Yes
Eq Additional Other Details Valve Stem Packing
Preparer Name T*** F****
Preparer Title Director Dot Compliance
Preparer Email T***********@p**.com
Preparer Telephone 832-765-1632
Prepared Date 2023-01-25 00:00:00
Local Contact Name S**** T*******
Local Contact Email S***************@p**.com
Local Contact Telephone 303-376-4391
Authorizer Name T*** F****
Authorizer Telephone 832-765-1632
Authorizer Title Director Dot Compliance
Authorizer Email T***********@p**.com
Narrative While inspecting valve site contractor identified that a small weep was coming from the valve stem. Contractor contacted p66 employee and upon arrival and unsuccessful tightening of packing the control center was notified to shut down the pipeline and isolated. Repairs were made to packing and weep was stopped. Line started back up that same day. Valve has since been replaced. 1/25/2023--per the accident team recommendations were to update g-6 to reflect the block valve and the sub-cause to reflect the stem packing was leaking.

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