HL incident on 2022-11-21 — TX

Operator
Dapl-Etco Operations Management, Llc
Cause
Material Failure Of Pipe Or Weld
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$30,268
Incident datetime
2022-11-21 10:21
Report number
Location
TX
Narrative
On 11/21/2022 at 10:21, operations personnel discovered a crude oil leak at the johnsons corner pump station building on the unit 3 suction piping. Station was shutdown to identify where leak was originating. Once found, unit 3 was isolated and locked out, and units 1 and 2 were restarted. Approximately 92 gallons of crude oil was released to a concrete floor inside an engine room. The released material was collected using a vacuum truck. Any residual oil left on the concrete surface was removed with absorbent pads. A visual examination determined the piping cracked just above the weld where the 2-inch drain line ties into the suction piping at the 6 oclock position. Operations performed segmented cutout and installed a 24-inch pup of pre-tested x-70 pipe. Due to initial assessment, operations went ahead and performed, like/kind, replacement of the other two systems due to susceptibility of similar events. The failed section of pipe was sent out for metallurgical analysis to determine failure mechanism. Upon receipt of laboratory report a supplemental 7000.1 report will be filed. Supplemental the results of the analysis indicate that the pipe leaked as a result of fatigue crack initiation and growth at the fillet weld of the reinforcement saddle. The fatigue crack initiated at the pipe side weld toe of the fillet weld that joined the reinforcement saddle to the suction pipe. The crack propagated through-wall, producing the leak. There was no evidence that metallurgical defects played a role in the failure. Other pump stations on the pipeline system were inspected for like and kind drain line installations and none were found.
Detailed record list
Report Received Date
2022-12-15 00:00:00
Iyear
2022
Report Number
20220285
Supplemental Number
38380
Report Type
Supplemental Final
Operator Id
Name
Dapl-Etco Operations Management, Llc
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2022-11-21 10:21:00
Time Zone
Central
Daylight Savings Ind
No
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
2.19
Recovered Bbls
2.19
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2022-11-21 10:21:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2022-11-21 10:30:00
Restart Datetime
2022-11-21 12:00:00
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Initial Responder Com Datetime
2022-11-21 14:31:00
On Site Datetime
2022-11-21 10:21:00
Confirmed Discovery Datetime
2022-11-21 10:21:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Notify Qualified Indiv Ind
Yes
Qualified Indiv Notif Datetime
2022-11-21 10:21:00
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Johnson's Corner Pump Station
Segment Name
Pump Unit 3
Onshore State Abbreviation
Nd
Onshore Postal Code
58854
Onshore City Name
Watford City
Onshore County Name
Mckenzie
Designated Location
Survey Station No.
Designated Name
0+00
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Inside A Building
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Weld, Including Heat-Affected Zone
Weld Subtype
Fillet Weld
Installation Year
2021
Manufactured Year
2019
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Crack
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
30268
Est Cost Emergency
2087
Est Cost Environmental
0
Est Cost Other
0
Prpty
32355
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
820
Mop Psig
1440
Mop Cfr Section
Subpart E Pressure Test �195.406(A)(3)
Maop Established Date
2021-06-07 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Design-, Construction-, Installation-, Or Fabrication-Related
Metallurgical Ind
Yes
Failure Type
Design-, Construction-, Installation-, Or Fabrication-Related
Fatigue Vibr Related
Yes
Failure Subtype
Mechanical Vibration
Additional Crack Ind
Yes
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
Yes
Exm Radiography Rcnt Year
2021
Exm Radiography Rcnt Ind
Yes
Preparer Name
T*** N*******
Preparer Title
Director - Regulatory Compliance
Preparer Email
T************@e*************.com
Preparer Telephone
713-989-7126
Prepared Date
2023-08-10 00:00:00
Authorizer Name
T*** N*******
Authorizer Telephone
713-989-7126
Authorizer Title
Director - Regulatory Compliance
Authorizer Email
T************@e*************.com
Narrative
On 11/21/2022 at 10:21, operations personnel discovered a crude oil leak at the johnsons corner pump station building on the unit 3 suction piping. Station was shutdown to identify where leak was originating. Once found, unit 3 was isolated and locked out, and units 1 and 2 were restarted. Approximately 92 gallons of crude oil was released to a concrete floor inside an engine room. The released material was collected using a vacuum truck. Any residual oil left on the concrete surface was removed with absorbent pads. A visual examination determined the piping cracked just above the weld where the 2-inch drain line ties into the suction piping at the 6 oclock position. Operations performed segmented cutout and installed a 24-inch pup of pre-tested x-70 pipe. Due to initial assessment, operations went ahead and performed, like/kind, replacement of the other two systems due to susceptibility of similar events. The failed section of pipe was sent out for metallurgical analysis to determine failure mechanism. Upon receipt of laboratory report a supplemental 7000.1 report will be filed. Supplemental the results of the analysis indicate that the pipe leaked as a result of fatigue crack initiation and growth at the fillet weld of the reinforcement saddle. The fatigue crack initiated at the pipe side weld toe of the fillet weld that joined the reinforcement saddle to the suction pipe. The crack propagated through-wall, producing the leak. There was no evidence that metallurgical defects played a role in the failure. Other pump stations on the pipeline system were inspected for like and kind drain line installations and none were found.
Report Received Date 2022-12-15 00:00:00
Iyear 2022
Report Number 20220285
Supplemental Number 38380
Report Type Supplemental Final
Operator Id 39205 PHMSA Enforcement
Name Dapl-Etco Operations Management, Llc
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2022-11-21 10:21:00
Time Zone Central
Daylight Savings Ind No
Location Latitude 47.79928474 Google Maps OpenStreetMap
Location Longitude -102.923979 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 2.19
Recovered Bbls 2.19
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2022-11-21 10:21:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind Yes
Shutdown Datetime 2022-11-21 10:30:00
Restart Datetime 2022-11-21 12:00:00
Communication State Fed Ind Yes
Party Initiated Communication Operator
Initial Responder Com Datetime 2022-11-21 14:31:00
On Site Datetime 2022-11-21 10:21:00
Confirmed Discovery Datetime 2022-11-21 10:21:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Notify Qualified Indiv Ind Yes
Qualified Indiv Notif Datetime 2022-11-21 10:21:00
Oil Spill Removal Org Ind No
Num Pub Evacuated 0
Pipe Fac Name Johnson's Corner Pump Station
Segment Name Pump Unit 3
Onshore State Abbreviation Nd
Onshore Postal Code 58854
Onshore City Name Watford City
Onshore County Name Mckenzie
Designated Location Survey Station No.
Designated Name 0+00
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Inside A Building
Crossing No
Pipe Facility Type Interstate
Item Involved Weld, Including Heat-Affected Zone
Weld Subtype Fillet Weld
Installation Year 2021
Manufactured Year 2019
Material Involved Carbon Steel
Release Type Leak
Leak Type Crack
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 30268
Est Cost Emergency 2087
Est Cost Environmental 0
Est Cost Other 0
Prpty 32355
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 820
Mop Psig 1440
Mop Cfr Section Subpart E Pressure Test �195.406(A)(3) View CFR 49 §192
Maop Established Date 2021-06-07 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Material Failure Of Pipe Or Weld
Cause Details Design-, Construction-, Installation-, Or Fabrication-Related
Metallurgical Ind Yes
Failure Type Design-, Construction-, Installation-, Or Fabrication-Related
Fatigue Vibr Related Yes
Failure Subtype Mechanical Vibration
Additional Crack Ind Yes
Collected Data Ind No
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind Yes
Exm Radiography Rcnt Year 2021
Exm Radiography Rcnt Ind Yes
Preparer Name T*** N*******
Preparer Title Director - Regulatory Compliance
Preparer Email T************@e*************.com
Preparer Telephone 713-989-7126
Prepared Date 2023-08-10 00:00:00
Authorizer Name T*** N*******
Authorizer Telephone 713-989-7126
Authorizer Title Director - Regulatory Compliance
Authorizer Email T************@e*************.com
Narrative On 11/21/2022 at 10:21, operations personnel discovered a crude oil leak at the johnsons corner pump station building on the unit 3 suction piping. Station was shutdown to identify where leak was originating. Once found, unit 3 was isolated and locked out, and units 1 and 2 were restarted. Approximately 92 gallons of crude oil was released to a concrete floor inside an engine room. The released material was collected using a vacuum truck. Any residual oil left on the concrete surface was removed with absorbent pads. A visual examination determined the piping cracked just above the weld where the 2-inch drain line ties into the suction piping at the 6 oclock position. Operations performed segmented cutout and installed a 24-inch pup of pre-tested x-70 pipe. Due to initial assessment, operations went ahead and performed, like/kind, replacement of the other two systems due to susceptibility of similar events. The failed section of pipe was sent out for metallurgical analysis to determine failure mechanism. Upon receipt of laboratory report a supplemental 7000.1 report will be filed. Supplemental the results of the analysis indicate that the pipe leaked as a result of fatigue crack initiation and growth at the fillet weld of the reinforcement saddle. The fatigue crack initiated at the pipe side weld toe of the fillet weld that joined the reinforcement saddle to the suction pipe. The crack propagated through-wall, producing the leak. There was no evidence that metallurgical defects played a role in the failure. Other pump stations on the pipeline system were inspected for like and kind drain line installations and none were found.

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