HL incident on 2022-11-14 — TX

Operator
Exxonmobil Pipeline Company Llc
Cause
Incorrect Operation
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$65
Incident datetime
2022-11-14 11:11
Report number
Location
TX
Narrative
Incident description: tank 2177 was being commissioned after repairs. The suction fill line (tank leg) is a 40" line with a 40" shell valve. The shell valve was removed to air gap the tank to allow for safe confined space work. After repairs were completed, the shell valve was reinstalled. Commissioning commenced on 11/14 at 10:44 a.M. Empco llc personnel and a contractor crew were staged at the tank valve along with containment tub under the valve to capture any potential drips. At 11:11 a.M., 27 minutes into the commissioning personnel noticed a drip at the bottom of the flange. Empco llc. Immediately instructed operations to shut down the delivery. Within one minute of the drip starting, gasoline began to release from the bottom of the flange into the containment tub. (4 o'clock to 8 o'clock position bottom of the flange) at 11:12 a.M. Operations manually closed the delivery valve. At that same time empco drove to the manifold to open a 6" water drain valve to remove all product from tank leg. Delivery valve was fully closed around 11:15 a.M. At approximately 11:46 product stopped leaking from flange. Root cause: adhesive was utilized to maintain gasket alignment but due to the tight spacing, the gar-loc gasket slipped out of alignment on the top of the flange during installation of the 40" valve. This caused the release of product from the top of the flange. Immediate corrective actions were taken to isolate and drain down the tank line. The root cause of this incident was that the installation technician did not use a self-centering gasket. Prevention of re-occurrence: below are the actions empco has taken to prevent the incident from happening again: -the bolt up procedure for this valve was updated to utilize a self-centering gasket. -gar-loc gasket maker will provide additional training to assist with self-centering gasket options for tight spaces. Updates to the initial report: -updated the time accident criteria was met -updated the time the qi was notified -updated the root cause of the incident -updated the costs for emergency response and environmental remediation -updated the narrative
Detailed record list
Report Received Date
2022-12-12 00:00:00
Iyear
2022
Report Number
20220282
Supplemental Number
37550
Report Type
Supplemental Final
Operator Id
Name
Exxonmobil Pipeline Company Llc
Operator Street Address
22777 Springwoods Village Parkway E2.2b-Emp
Operator City Name
Spring
Operator State Abbreviation
TX
Operator Postal Code
77389
Local Datetime
2022-11-14 11:11:00
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
17
Recovered Bbls
14
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2022-11-14 11:11:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Status When Identified
Post-Maintenance/repair
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Initial Responder Com Datetime
2022-11-14 11:11:00
On Site Datetime
2022-11-14 11:11:00
Confirmed Discovery Datetime
2022-11-14 14:05:00
Nrc Rpt Datetime
2022-11-14 14:43:00
Nrc Rpt Num
Additional Nrc Report Numbers
1352700
Ignite Ind
No
Notify Qualified Indiv Ind
Yes
Qualified Indiv Notif Datetime
2022-11-14 11:15:00
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Pasadena Station
Segment Name
Tank #2177 Fill Line
Onshore State Abbreviation
Tx
Onshore Postal Code
77503
Onshore City Name
Pasadena
Onshore County Name
Harris
Designated Location
Milepost
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Exposed Due To Excavation
Depth Of Cover
48
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
2022
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
1870
Est Cost Prop Damage
65
Est Cost Emergency
15000
Est Cost Environmental
18000
Est Cost Other
0
Prpty
34935
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
1
Mop Psig
125
Mop Cfr Section
Component Design Pressure �195.406(A)(2)
Maop Established Date
1975-01-01 00:00:00
Maop Reversal Flow Ind
Bi-Directional
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Control room actions were not a contributing factor to the release.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Equipment Not Installed Properly
Operation Type
Equipment Not Installed Properly
Related Inadequate Proc Ind
Yes
Category Type
Other Maintenance
Operator Qualification Ind
No
Eqf Non Threaded Ind
Yes
Preparer Name
R***** P S**********
Preparer Title
Pipeline Safety Advisor
Preparer Email
R*******************@e*********.com
Preparer Telephone
618-267-9641
Prepared Date
2023-01-06 00:00:00
Local Contact Name
R***** P S**********
Local Contact Email
R*******************@e*********.com
Local Contact Telephone
618-267-9641
Authorizer Name
T****** H* B*****
Authorizer Telephone
713-819-9504
Authorizer Title
Regulatory Compliance Supervisor
Authorizer Email
T***************@e*********.com
Narrative
Incident description: tank 2177 was being commissioned after repairs. The suction fill line (tank leg) is a 40" line with a 40" shell valve. The shell valve was removed to air gap the tank to allow for safe confined space work. After repairs were completed, the shell valve was reinstalled. Commissioning commenced on 11/14 at 10:44 a.M. Empco llc personnel and a contractor crew were staged at the tank valve along with containment tub under the valve to capture any potential drips. At 11:11 a.M., 27 minutes into the commissioning personnel noticed a drip at the bottom of the flange. Empco llc. Immediately instructed operations to shut down the delivery. Within one minute of the drip starting, gasoline began to release from the bottom of the flange into the containment tub. (4 o'clock to 8 o'clock position bottom of the flange) at 11:12 a.M. Operations manually closed the delivery valve. At that same time empco drove to the manifold to open a 6" water drain valve to remove all product from tank leg. Delivery valve was fully closed around 11:15 a.M. At approximately 11:46 product stopped leaking from flange. Root cause: adhesive was utilized to maintain gasket alignment but due to the tight spacing, the gar-loc gasket slipped out of alignment on the top of the flange during installation of the 40" valve. This caused the release of product from the top of the flange. Immediate corrective actions were taken to isolate and drain down the tank line. The root cause of this incident was that the installation technician did not use a self-centering gasket. Prevention of re-occurrence: below are the actions empco has taken to prevent the incident from happening again: -the bolt up procedure for this valve was updated to utilize a self-centering gasket. -gar-loc gasket maker will provide additional training to assist with self-centering gasket options for tight spaces. Updates to the initial report: -updated the time accident criteria was met -updated the time the qi was notified -updated the root cause of the incident -updated the costs for emergency response and environmental remediation -updated the narrative
Report Received Date 2022-12-12 00:00:00
Iyear 2022
Report Number 20220282
Supplemental Number 37550
Report Type Supplemental Final
Operator Id 4906 PHMSA Enforcement
Name Exxonmobil Pipeline Company Llc
Operator Street Address 22777 Springwoods Village Parkway E2.2b-Emp
Operator City Name Spring
Operator State Abbreviation TX
Operator Postal Code 77389
Local Datetime 2022-11-14 11:11:00
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 29.717072 Google Maps OpenStreetMap
Location Longitude -95.163308 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 17
Recovered Bbls 14
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2022-11-14 11:11:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Status When Identified Post-Maintenance/repair
Communication State Fed Ind Yes
Party Initiated Communication Operator
Initial Responder Com Datetime 2022-11-14 11:11:00
On Site Datetime 2022-11-14 11:11:00
Confirmed Discovery Datetime 2022-11-14 14:05:00
Nrc Rpt Datetime 2022-11-14 14:43:00
Nrc Rpt Num 1352552 NRC Report How to search
Additional Nrc Report Numbers 1352700
Ignite Ind No
Notify Qualified Indiv Ind Yes
Qualified Indiv Notif Datetime 2022-11-14 11:15:00
Oil Spill Removal Org Ind No
Num Pub Evacuated 0
Pipe Fac Name Pasadena Station
Segment Name Tank #2177 Fill Line
Onshore State Abbreviation Tx
Onshore Postal Code 77503
Onshore City Name Pasadena
Onshore County Name Harris
Designated Location Milepost
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Exposed Due To Excavation
Depth Of Cover 48
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year 2022
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 1870
Est Cost Prop Damage 65
Est Cost Emergency 15000
Est Cost Environmental 18000
Est Cost Other 0
Prpty 34935
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 1
Mop Psig 125
Mop Cfr Section Component Design Pressure �195.406(A)(2) View CFR 49 §192
Maop Established Date 1975-01-01 00:00:00
Maop Reversal Flow Ind Bi-Directional
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Control room actions were not a contributing factor to the release.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Equipment Not Installed Properly
Operation Type Equipment Not Installed Properly
Related Inadequate Proc Ind Yes
Category Type Other Maintenance
Operator Qualification Ind No
Eqf Non Threaded Ind Yes
Preparer Name R***** P S**********
Preparer Title Pipeline Safety Advisor
Preparer Email R*******************@e*********.com
Preparer Telephone 618-267-9641
Prepared Date 2023-01-06 00:00:00
Local Contact Name R***** P S**********
Local Contact Email R*******************@e*********.com
Local Contact Telephone 618-267-9641
Authorizer Name T****** H* B*****
Authorizer Telephone 713-819-9504
Authorizer Title Regulatory Compliance Supervisor
Authorizer Email T***************@e*********.com
Narrative Incident description: tank 2177 was being commissioned after repairs. The suction fill line (tank leg) is a 40" line with a 40" shell valve. The shell valve was removed to air gap the tank to allow for safe confined space work. After repairs were completed, the shell valve was reinstalled. Commissioning commenced on 11/14 at 10:44 a.M. Empco llc personnel and a contractor crew were staged at the tank valve along with containment tub under the valve to capture any potential drips. At 11:11 a.M., 27 minutes into the commissioning personnel noticed a drip at the bottom of the flange. Empco llc. Immediately instructed operations to shut down the delivery. Within one minute of the drip starting, gasoline began to release from the bottom of the flange into the containment tub. (4 o'clock to 8 o'clock position bottom of the flange) at 11:12 a.M. Operations manually closed the delivery valve. At that same time empco drove to the manifold to open a 6" water drain valve to remove all product from tank leg. Delivery valve was fully closed around 11:15 a.M. At approximately 11:46 product stopped leaking from flange. Root cause: adhesive was utilized to maintain gasket alignment but due to the tight spacing, the gar-loc gasket slipped out of alignment on the top of the flange during installation of the 40" valve. This caused the release of product from the top of the flange. Immediate corrective actions were taken to isolate and drain down the tank line. The root cause of this incident was that the installation technician did not use a self-centering gasket. Prevention of re-occurrence: below are the actions empco has taken to prevent the incident from happening again: -the bolt up procedure for this valve was updated to utilize a self-centering gasket. -gar-loc gasket maker will provide additional training to assist with self-centering gasket options for tight spaces. Updates to the initial report: -updated the time accident criteria was met -updated the time the qi was notified -updated the root cause of the incident -updated the costs for emergency response and environmental remediation -updated the narrative

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