HL incident on 2022-11-10 — OK

Operator
Magellan Pipeline Company, Lp
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$30
Incident datetime
2022-11-10 05:46
Report number
Location
OK
Narrative
On november 10, 2022 at 05:46, magellan operations personnel discovered product releasing from a tank pump relief line where a 1/4" threaded connection had broken off. The leak source was isolated and cleanup activities were initiated. It was determined that the analog input module had failed which gave the transmitter a false, zero pressure reading causing the vfd to ramp up and operate the pump at the maximum rate creating excessive vibration and shearing of the 1/4" connection threads. The threaded connection was replaced and a new analog input module was installed.
Detailed record list
Report Received Date
2022-12-08 00:00:00
Iyear
2022
Report Number
20220275
Supplemental Number
37437
Report Type
Original Final
Operator Id
Name
Magellan Pipeline Company, Lp
Operator Street Address
100 West 5th Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2022-11-10 05:46:00
Time Zone
Mountain
Daylight Savings Ind
No
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
0.17
Recovered Bbls
0.12
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2022-11-10 05:46:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
No
Shutdown Explain
Leak Source Was Isolated
Communication State Fed Ind
No
On Site Datetime
2022-11-10 05:46:00
Confirmed Discovery Datetime
2022-11-10 05:46:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Notify Qualified Indiv Ind
Yes
Qualified Indiv Notif Datetime
2022-11-10 05:46:00
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
El Paso
Segment Name
191
Onshore State Abbreviation
Tx
Onshore Postal Code
79938
Onshore City Name
El Paso
Onshore County Name
El Paso
Designated Location
Milepost
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tap Fitting(Stopple, Thread-O-Ring, Weld-O-Let, Etc.)
Installation Year
2008
Manufactured Year
2008
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
20
Est Cost Prop Damage
30
Est Cost Emergency
0
Est Cost Environmental
300
Est Cost Other
0
Prpty
350
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
110
Mop Psig
275
Mop Cfr Section
Component Design Pressure �195.406(A)(2)
Maop Established Date
2007-06-11 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Due to the location of the release, no action was needed from ops control. Mainline valves and pipes were not affected.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Threaded Connection/coupling Failure
Eq Failure Type
Threaded Connection/coupling Failure
Other Stripped Ind
Pipe Nipple
Additional Vibration Ind
Yes
Eqf Control Releaf Ind
Yes
Preparer Name
C******* R******
Preparer Title
Strategic Data Engineer
Preparer Email
C***************@m**********.com
Preparer Telephone
9182315764
Prepared Date
2022-12-08 00:00:00
Authorizer Name
G**** R****
Authorizer Telephone
9185747165
Authorizer Title
Supv. Integrity Mgmt And Regulatory Compliance
Authorizer Email
G**********@m*********.com
Narrative
On november 10, 2022 at 05:46, magellan operations personnel discovered product releasing from a tank pump relief line where a 1/4" threaded connection had broken off. The leak source was isolated and cleanup activities were initiated. It was determined that the analog input module had failed which gave the transmitter a false, zero pressure reading causing the vfd to ramp up and operate the pump at the maximum rate creating excessive vibration and shearing of the 1/4" connection threads. The threaded connection was replaced and a new analog input module was installed.
Report Received Date 2022-12-08 00:00:00
Iyear 2022
Report Number 20220275
Supplemental Number 37437
Report Type Original Final
Operator Id 22610 PHMSA Enforcement
Name Magellan Pipeline Company, Lp
Operator Street Address 100 West 5th Street
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74103
Local Datetime 2022-11-10 05:46:00
Time Zone Mountain
Daylight Savings Ind No
Location Latitude 31.815924 Google Maps OpenStreetMap
Location Longitude -106.212277 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 0.17
Recovered Bbls 0.12
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2022-11-10 05:46:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind No
Shutdown Explain Leak Source Was Isolated
Communication State Fed Ind No
On Site Datetime 2022-11-10 05:46:00
Confirmed Discovery Datetime 2022-11-10 05:46:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Notify Qualified Indiv Ind Yes
Qualified Indiv Notif Datetime 2022-11-10 05:46:00
Oil Spill Removal Org Ind No
Num Pub Evacuated 0
Pipe Fac Name El Paso
Segment Name 191
Onshore State Abbreviation Tx
Onshore Postal Code 79938
Onshore City Name El Paso
Onshore County Name El Paso
Designated Location Milepost
Designated Name 0
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Tap Fitting(Stopple, Thread-O-Ring, Weld-O-Let, Etc.)
Installation Year 2008
Manufactured Year 2008
Material Involved Carbon Steel
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 20
Est Cost Prop Damage 30
Est Cost Emergency 0
Est Cost Environmental 300
Est Cost Other 0
Prpty 350
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 110
Mop Psig 275
Mop Cfr Section Component Design Pressure �195.406(A)(2) View CFR 49 §192
Maop Established Date 2007-06-11 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Due to the location of the release, no action was needed from ops control. Mainline valves and pipes were not affected.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Threaded Connection/coupling Failure
Eq Failure Type Threaded Connection/coupling Failure
Other Stripped Ind Pipe Nipple
Additional Vibration Ind Yes
Eqf Control Releaf Ind Yes
Preparer Name C******* R******
Preparer Title Strategic Data Engineer
Preparer Email C***************@m**********.com
Preparer Telephone 9182315764
Prepared Date 2022-12-08 00:00:00
Authorizer Name G**** R****
Authorizer Telephone 9185747165
Authorizer Title Supv. Integrity Mgmt And Regulatory Compliance
Authorizer Email G**********@m*********.com
Narrative On november 10, 2022 at 05:46, magellan operations personnel discovered product releasing from a tank pump relief line where a 1/4" threaded connection had broken off. The leak source was isolated and cleanup activities were initiated. It was determined that the analog input module had failed which gave the transmitter a false, zero pressure reading causing the vfd to ramp up and operate the pump at the maximum rate creating excessive vibration and shearing of the 1/4" connection threads. The threaded connection was replaced and a new analog input module was installed.

All rights reserved. Copyright © by ClearPHMSA