HL incident on 2022-11-04 — TX

Operator
Shell Pipeline Co., L.p.
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$5,000
Incident datetime
2022-11-04 20:00
Report number
Location
TX
Narrative
On 11/4/2022, the operations manager was making a round checking lighting in the facility. Upon making his rounds, he observed a significant puddle of crude around pump e. After further investigation, it was determined that a seal had failed and crews were dispatched to start the clean-up process.
Detailed record list
Report Received Date
2022-12-01 00:00:00
Iyear
2022
Report Number
20220268
Supplemental Number
37512
Report Type
Supplemental
Operator Id
Name
Shell Pipeline Co., L.p.
Operator Street Address
150 North Dairy Ashford Road Wck Bldg. A
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77079
Local Datetime
2022-11-04 19:40:00
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
30
Recovered Bbls
30
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Ground Patrol By Operator Or Its Contractor
Operator Type
Operator Employee
Incident Identified Datetime
2022-11-04 20:00:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2022-11-04 20:20:00
Restart Datetime
2022-11-05 03:00:00
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Initial Responder Com Datetime
2022-11-04 21:00:00
On Site Datetime
2022-11-04 19:35:00
Confirmed Discovery Datetime
2022-11-04 19:40:00
Nrc Rpt Datetime
2022-11-04 22:13:00
Nrc Rpt Num
Ignite Ind
No
Notify Qualified Indiv Ind
Yes
Qualified Indiv Notif Datetime
2022-11-04 20:00:00
Oil Spill Removal Org Ind
Yes
Osro Activated Datetime
2022-11-04 20:09:00
Osro Arrived On Site Dt
11/4/2022 20:39
Num Pub Evacuated
0
Pipe Fac Name
Gibson Station
Segment Name
Gibson
Onshore State Abbreviation
La
Onshore Postal Code
70079
Onshore City Name
Norco
Onshore County Name
Terrebone
Designated Location
Milepost
Designated Name
Gibson Sta.
Federal
No
Location Type
Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pump
Pump Type
Centrifugal
Pump Service Type
Mainline
Installation Year
1999
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
No
Est Cost Oper Paid
0
Est Cost Gas Released
2440
Est Cost Prop Damage
5000
Est Cost Emergency
86000
Est Cost Environmental
0
Est Cost Other
0
Prpty
93440
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
375
Mop Psig
980
Mop Cfr Section
Internal Design Pressure �195.406(A)(1)
Maop Established Date
2009-11-16 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
At the time of discovery, the leak volume was below the detectable limits of the scada and cpm. There were no indications for the controller to act upon and the correct actions were taken by the controller once contacted by field personnel.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Pump Or Pump-Related Equipment
Eq Failure Type
Pump Or Pump-Related Equipment
Other Pump Ind
Seal/packing Failure
Additional Vibration Ind
Yes
Preparer Name
J***** H*****
Preparer Title
Operations Support Coordinator
Preparer Email
J************@s****.com
Preparer Telephone
4095402781
Prepared Date
2022-12-23 00:00:00
Local Contact Name
J***** H*****
Local Contact Email
J************@s****.com
Local Contact Telephone
4095402781
Authorizer Name
D****** P****
Authorizer Telephone
832-762-2553
Authorizer Title
Integrity And Regulatory Services Manager
Authorizer Email
D************@s****.com
Narrative
On 11/4/2022, the operations manager was making a round checking lighting in the facility. Upon making his rounds, he observed a significant puddle of crude around pump e. After further investigation, it was determined that a seal had failed and crews were dispatched to start the clean-up process.
Report Received Date 2022-12-01 00:00:00
Iyear 2022
Report Number 20220268
Supplemental Number 37512
Report Type Supplemental
Operator Id 31174 PHMSA Enforcement
Name Shell Pipeline Co., L.p.
Operator Street Address 150 North Dairy Ashford Road Wck Bldg. A
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77079
Local Datetime 2022-11-04 19:40:00
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 29.629581 Google Maps OpenStreetMap
Location Longitude -90.933839 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 30
Recovered Bbls 30
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Ground Patrol By Operator Or Its Contractor
Operator Type Operator Employee
Incident Identified Datetime 2022-11-04 20:00:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind Yes
Shutdown Datetime 2022-11-04 20:20:00
Restart Datetime 2022-11-05 03:00:00
Communication State Fed Ind Yes
Party Initiated Communication Operator
Initial Responder Com Datetime 2022-11-04 21:00:00
On Site Datetime 2022-11-04 19:35:00
Confirmed Discovery Datetime 2022-11-04 19:40:00
Nrc Rpt Datetime 2022-11-04 22:13:00
Nrc Rpt Num 1351773 NRC Report How to search
Ignite Ind No
Notify Qualified Indiv Ind Yes
Qualified Indiv Notif Datetime 2022-11-04 20:00:00
Oil Spill Removal Org Ind Yes
Osro Activated Datetime 2022-11-04 20:09:00
Osro Arrived On Site Dt 11/4/2022 20:39
Num Pub Evacuated 0
Pipe Fac Name Gibson Station
Segment Name Gibson
Onshore State Abbreviation La
Onshore Postal Code 70079
Onshore City Name Norco
Onshore County Name Terrebone
Designated Location Milepost
Designated Name Gibson Sta.
Federal No
Location Type Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Pump
Pump Type Centrifugal
Pump Service Type Mainline
Installation Year 1999
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Other Pop Ind Yes
Other Pop Yes No No
Est Cost Oper Paid 0
Est Cost Gas Released 2440
Est Cost Prop Damage 5000
Est Cost Emergency 86000
Est Cost Environmental 0
Est Cost Other 0
Prpty 93440
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 375
Mop Psig 980
Mop Cfr Section Internal Design Pressure �195.406(A)(1) View CFR 49 §192
Maop Established Date 2009-11-16 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details At the time of discovery, the leak volume was below the detectable limits of the scada and cpm. There were no indications for the controller to act upon and the correct actions were taken by the controller once contacted by field personnel.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Pump Or Pump-Related Equipment
Eq Failure Type Pump Or Pump-Related Equipment
Other Pump Ind Seal/packing Failure
Additional Vibration Ind Yes
Preparer Name J***** H*****
Preparer Title Operations Support Coordinator
Preparer Email J************@s****.com
Preparer Telephone 4095402781
Prepared Date 2022-12-23 00:00:00
Local Contact Name J***** H*****
Local Contact Email J************@s****.com
Local Contact Telephone 4095402781
Authorizer Name D****** P****
Authorizer Telephone 832-762-2553
Authorizer Title Integrity And Regulatory Services Manager
Authorizer Email D************@s****.com
Narrative On 11/4/2022, the operations manager was making a round checking lighting in the facility. Upon making his rounds, he observed a significant puddle of crude around pump e. After further investigation, it was determined that a seal had failed and crews were dispatched to start the clean-up process.

All rights reserved. Copyright © by ClearPHMSA